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    RRF Update to 3.3 just killed my FW

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    • droftartsundefined
      droftarts administrators @Andy Cohen
      last edited by

      @andy-cohen if the firmware did update to 3.3 (connect via USB, send M115) send

      M997 S1 P”0:/sys/DuetWiFiServer.bin”
      

      Otherwise it will look in the /firmware folder, which doesn’t exist, and you’ll get an error message. 3.3 and later keeps firmware updates out of the sys folder.

      Ian

      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

      1 Reply Last reply Reply Quote 1
      • Andy Cohenundefined
        Andy Cohen
        last edited by

        Unfortunately... nothing seems to work at all. It acts like it cannot see the SD card and the extruder fan goes on. The update looks like it killed my whole setup!
        Can't I simply take the SD card out and make changes?

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        • Phaedruxundefined
          Phaedrux Moderator
          last edited by

          There are config changes required between 3.0 and above. Can you post your current config.g?

          You can remove the SD card from the Duet and check the config.g on your PC.

          A firmware update can't kill anything. We just need you to connect the board via USB terminal to see what is actually going on.

          Z-Bot CoreXY Build | Thingiverse Profile

          Andy Cohenundefined 1 Reply Last reply Reply Quote 0
          • Andy Cohenundefined
            Andy Cohen @Phaedrux
            last edited by

            @phaedrux I was able top get the wifiserver running thanks to your post.
            It looks like quite a bit of the config is no longer working. Great.

            1 Reply Last reply Reply Quote 0
            • Phaedruxundefined
              Phaedrux Moderator
              last edited by

              The changes between 3.0 and up are pretty minor.

              The change between RRF2 and RRF3 are more substantial. What firmware were you running before?

              You can get an example config updated for 3.3 from the config tool to compare against. https://configtool.reprapfirmware.org/Start

              Z-Bot CoreXY Build | Thingiverse Profile

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              • Andy Cohenundefined
                Andy Cohen
                last edited by

                @phaedrux I started with a late v2 and I'm lost with the new approach with the M950. Is there a web app I can use to gen the gcode?

                Phaedruxundefined 1 Reply Last reply Reply Quote 0
                • Phaedruxundefined
                  Phaedrux Moderator @Andy Cohen
                  last edited by

                  @andy-cohen said in RRF Update to 3.3 just killed my FW:

                  Is there a web app I can use to gen the gcode?

                  Yes. I linked it in my last post.

                  You can get an example config updated for 3.3 from the config tool to compare against. https://configtool.reprapfirmware.org/Start

                  Here's what I normally tell people when they want to update from RRF2

                  If you still have access to DWC. Upload these 3 zip files, one at a time in the system tab. Don't extract them first. Reboot after each. Use M115 in the gcode console to verify the firmware has been applied.
                  https://github.com/Duet3D/RepRapFirmware/releases/download/2.05.1/Duet2Firmware-2.05.1.zip
                  https://github.com/Duet3D/RepRapFirmware/releases/download/3.0/Duet2and3Firmware-3.0.zip
                  https://github.com/Duet3D/RepRapFirmware/releases/download/3.3/Duet2and3Firmware-3.3.zip
                  That will get your firmware and DWC up to date.

                  You can see the change logs here:
                  https://github.com/Duet3D/RepRapFirmware/wiki/Changelog-RRF-3.x

                  For your config, might be a good idea to run through the configurator tool and generate a fresh set for RRF3.
                  https://configtool.reprapfirmware.org/Start

                  Backup your existing config files in the sys folder in case you want to switch back to RRF2. It’s easy to switch back and forth, just upload the zip file for the version you want and then upload your config files.

                  These documents will come in handy during the conversion.
                  https://duet3d.dozuki.com/Wiki/RepRapFirmware_3_overview
                  https://duet3d.dozuki.com/Wiki/Gcode

                  Z-Bot CoreXY Build | Thingiverse Profile

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                  • Andy Cohenundefined
                    Andy Cohen
                    last edited by Andy Cohen

                    Thanks for the help.
                    I was able to get it to kinda work. It still does not see my extruder heater, only the bed heater. This is the heater gcode in the config file I generated:

                    ; Heaters
                    M308 S0 P"bedtemp" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin bedtemp
                    M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0
                    M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
                    M140 H0 ; map heated bed to heater 0
                    M143 H0 S120 ; set temperature limit for heater 0 to 120C
                    M308 S1 P"e0temp" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin e0temp
                    M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1
                    M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
                    M143 H1 S280 ; set temperature limit for heater 1 to 280C

                    Andy Cohenundefined Phaedruxundefined 2 Replies Last reply Reply Quote 0
                    • Andy Cohenundefined
                      Andy Cohen @Andy Cohen
                      last edited by

                      @andy-cohen Here's the tool def:
                      ; Tools
                      M563 P0 D0 H1 F0 ; define tool 0
                      G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                      G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

                      Andy Cohenundefined 1 Reply Last reply Reply Quote 0
                      • Phaedruxundefined
                        Phaedrux Moderator @Andy Cohen
                        last edited by Phaedrux

                        @andy-cohen said in RRF Update to 3.3 just killed my FW:

                        It still does not see my extruder heater, only the bed heater.

                        What does not see it?

                        Can you send M122 and M98 P"config.g" in the gcode console or USB terminal and share the results?

                        Z-Bot CoreXY Build | Thingiverse Profile

                        Andy Cohenundefined 1 Reply Last reply Reply Quote 0
                        • Andy Cohenundefined
                          Andy Cohen @Andy Cohen
                          last edited by

                          @andy-cohen Yeah... I see it... The web app did not make the P1 tool.

                          1 Reply Last reply Reply Quote 0
                          • Andy Cohenundefined
                            Andy Cohen @Phaedrux
                            last edited by

                            @phaedrux OK... heaters and fans seem OK.
                            Now the motors. They won't home. Comparing with my original config, I see nothing that can be incorrect. Any ideas?
                            ; Drives
                            M569 P0 S1 ; physical drive 0 goes forwards
                            M569 P1 S1 ; physical drive 1 goes forwards
                            M569 P2 S0 ; physical drive 2 goes forwards
                            M569 P3 S1 ; physical drive 3 goes forwards
                            M584 X0 Y1 Z2 E3 ; set drive mapping
                            M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
                            M92 X88.57 Y88.57 Z400.00 E125.459271 ; set steps per mm
                            M566 X900.00 Y900.00 Z12.00 E120.00 ; set maximum instantaneous speed changes (mm/min)
                            M203 X6000.00 Y6000.00 Z180.00 E1200.00 ; set maximum speeds (mm/min)
                            M201 X1000.00 Y1000.00 Z20.00 E250.00 ; set accelerations (mm/s^2)
                            M906 X800 Y800 Z400 E800 I30 ; set motor currents (mA) and motor idle factor in per cent
                            M84 S30 ; Set idle timeout

                            ; Axis Limits
                            M208 X0 Y0 Z0 S1 ; set axis minima
                            M208 X300 Y195 Z210 S0 ; set axis maxima

                            ; Endstops
                            M574 X2 S0 P"xstop" ; configure switch-type (e.g. microswitch) endstop for high end on X via pin xstop
                            M574 Y2 S0 P"ystop" ; configure switch-type (e.g. microswitch) endstop for high end on Y via pin ystop
                            M574 Z1 S0 P"zstop" ; configure switch-type (e.g. microswitch) endstop for low end on Z via pin zstop

                            Phaedruxundefined 1 Reply Last reply Reply Quote 0
                            • Phaedruxundefined
                              Phaedrux Moderator @Andy Cohen
                              last edited by

                              @andy-cohen said in RRF Update to 3.3 just killed my FW:

                              M574 X2 S0 P"xstop" ; configure switch-type (e.g. microswitch) endstop for high end on X via pin xstop
                              M574 Y2 S0 P"ystop" ; configure switch-type (e.g. microswitch) endstop for high end on Y via pin ystop
                              M574 Z1 S0 P"zstop" ; configure switch-type (e.g. microswitch) endstop for low end on Z via pin zstop

                              S0 is incorrect.

                              If the signal needs to be inverted, use S1 and add a ! to the front of the pin name.

                              M574 X2 S1 P"!xstop"

                              Z-Bot CoreXY Build | Thingiverse Profile

                              Andy Cohenundefined 1 Reply Last reply Reply Quote 0
                              • Andy Cohenundefined
                                Andy Cohen @Phaedrux
                                last edited by

                                @phaedrux It moves but the limit switches are ignored. When told to Home X it moves it on an angle. It's a coreXY machine so I got something wrong..
                                Why oh WHY was soooo much changed?!?

                                1 Reply Last reply Reply Quote 0
                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  You'll have to share your config and homing files at this point for any meaningful feedback.

                                  Are you sure it's set to corexy kinematic?

                                  Z-Bot CoreXY Build | Thingiverse Profile

                                  Andy Cohenundefined 1 Reply Last reply Reply Quote 0
                                  • Andy Cohenundefined
                                    Andy Cohen @Phaedrux
                                    last edited by

                                    @phaedrux Heck... at this point I'm not sure of anything!
                                    I also suspect the wifiserver FW needs to be updated as well as the ManelDue.

                                    ; Configuration file for Duet WiFi (firmware version 3.3)
                                    ; executed by the firmware on start-up
                                    ;
                                    ; generated by RepRapFirmware Configuration Tool v3.3.10 on Mon Jan 31 2022 16:37:49 GMT-0800 (PST)

                                    ; General preferences
                                    G90 ; send absolute coordinates...
                                    M83 ; ...but relative extruder moves
                                    M550 P"My Printer" ; set printer name

                                    ; Network
                                    M550 P"CloneDuet" ; Set machine name

                                    M552 S1 ; Enable network

                                    M586 P0 S1 ; Enable HTTP
                                    M586 P1 S0 ; Disable FTP
                                    M586 P2 S0 ; Disable Telnet

                                    M552 S1 ; enable network
                                    M586 P0 S1 ; enable HTTP
                                    M586 P1 S0 ; disable FTP
                                    M586 P2 S0 ; disable Telnet

                                    ; Drives
                                    M569 P0 S1 ; physical drive 0 goes forwards
                                    M569 P1 S1 ; physical drive 1 goes forwards
                                    M569 P2 S0 ; physical drive 2 goes forwards
                                    M569 P3 S1 ; physical drive 3 goes forwards
                                    M584 X0 Y1 Z2 E3 ; set drive mapping
                                    M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
                                    M92 X88.57 Y88.57 Z400.00 E125.459271 ; set steps per mm
                                    M566 X900.00 Y900.00 Z12.00 E120.00 ; set maximum instantaneous speed changes (mm/min)
                                    M203 X6000.00 Y6000.00 Z180.00 E1200.00 ; set maximum speeds (mm/min)
                                    M201 X1000.00 Y1000.00 Z20.00 E250.00 ; set accelerations (mm/s^2)
                                    M906 X800 Y800 Z400 E800 I30 ; set motor currents (mA) and motor idle factor in per cent
                                    M84 S30 ; Set idle timeout

                                    ; Axis Limits
                                    M208 X0 Y0 Z0 S1 ; set axis minima
                                    M208 X300 Y195 Z210 S0 ; set axis maxima

                                    ; Endstops
                                    M574 X2 S1 P"!xstop" ; configure switch-type (e.g. microswitch) endstop for high end on X via pin xstop
                                    M574 Y2 S1 P"!ystop" ; configure switch-type (e.g. microswitch) endstop for high end on Y via pin ystop
                                    M574 Z1 S1 P"!zstop" ; configure switch-type (e.g. microswitch) endstop for low end on Z via pin zstop

                                    ; Z-Probe
                                    M558 P1 C"zprobe.in" H5 F120 T6000 ; set Z probe type to unmodulated and the dive height + speeds
                                    G31 P500 X0 Y0 Z2.5 ; set Z probe trigger value, offset and trigger height
                                    M557 X10:300 Y-16.0:195 S20 ; define mesh grid

                                    ; Heaters
                                    M308 S0 P"bedtemp" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin bedtemp
                                    M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0
                                    M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
                                    M140 H0 ; map heated bed to heater 0
                                    M143 H0 S120 ; set temperature limit for heater 0 to 120C
                                    M308 S1 P"e0temp" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin e0temp
                                    M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1
                                    M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
                                    M143 H1 S280 ; set temperature limit for heater 1 to 280C

                                    ; Fans
                                    M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency
                                    M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
                                    M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency
                                    M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on

                                    ; Tools
                                    M563 P0 D0 H1 F0 ; define tool 0
                                    G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                                    G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C
                                    M563 P1 ; Define tool 1
                                    G10 P1 X35 Y0 Z0 ; Set tool 1 axis offsets
                                    G10 P1 R0 S0 ; Set initial tool 1 active and standby temperatures to 0C

                                    ; Custom settings are not defined

                                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                    • Andy Cohenundefined
                                      Andy Cohen
                                      last edited by

                                      Yeah... you were correct.
                                      There's no
                                      "M669 K1 ; switch to CoreXY mode"
                                      I added it and now it seems to work.

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                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        Can you send m122 and share the results?

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        Andy Cohenundefined 1 Reply Last reply Reply Quote 0
                                        • Andy Cohenundefined
                                          Andy Cohen @Phaedrux
                                          last edited by

                                          @phaedrux Attached.
                                          In the meantime the PanelDue is a 5.0i but it does not seem to want to update via the Duet. It's 3 years old. Think I'll need to remove it from it's containment and hit a resent button?

                                          M122
                                          === Diagnostics ===
                                          RepRapFirmware for Duet 2 WiFi/Ethernet version 3.3 (2021-06-15 21:44:54) running on Duet WiFi 1.02 or later
                                          Board ID: 08DGM-917DA-G4MS8-6JKD0-3S06N-K9TVB
                                          Used output buffers: 3 of 24 (12 max)
                                          === RTOS ===
                                          Static ram: 23876
                                          Dynamic ram: 75052 of which 0 recycled
                                          Never used RAM 15488, free system stack 184 words
                                          Tasks: NETWORK(ready,14.4%,244) HEAT(delaying,0.0%,326) Move(notifyWait,0.1%,364) MAIN(running,85.2%,417) IDLE(ready,0.4%,29), total 100.0%
                                          Owned mutexes: WiFi(NETWORK)
                                          === Platform ===
                                          Last reset 00:04:26 ago, cause: power up
                                          Last software reset at 2022-01-31 19:16, reason: StuckInSpinLoop, GCodes spinning, available RAM 12280, slot 0
                                          Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f80f BFAR 0xe000ed38 SP 0x2000254c Task MAIN Freestk 900 ok
                                          Stack: 004534c9 00455180 810f0000 00000000 3f000000 369dc3a0 3edbc06f 3331bb4c 40000000 b5ddd98d 388ab355 bb360b61 3e2aaaab 3f800000 00000000 00000000 4354c416 00000000 00000000 60000010 004534c1 200080c8 00408da7 00000000 200182c8 20004c8c 0041872b
                                          Error status: 0x00
                                          Step timer max interval 0
                                          MCU temperature: min 37.4, current 39.2, max 39.6
                                          Supply voltage: min 23.9, current 24.1, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
                                          Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                                          Driver 0: position 0, standstill, SG min/max not available
                                          Driver 1: position 0, standstill, SG min/max not available
                                          Driver 2: position 0, standstill, SG min/max not available
                                          Driver 3: position 0, standstill, SG min/max not available
                                          Driver 4: position 0, standstill, SG min/max not available
                                          Driver 5: position 0
                                          Driver 6: position 0
                                          Driver 7: position 0
                                          Driver 8: position 0
                                          Driver 9: position 0
                                          Driver 10: position 0
                                          Driver 11: position 0
                                          Date/time: 2022-01-31 19:26:17
                                          Cache data hit count 4294967295
                                          Slowest loop: 7.69ms; fastest: 0.17ms
                                          I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                                          === Storage ===
                                          Free file entries: 10
                                          SD card 0 detected, interface speed: 20.0MBytes/sec
                                          SD card longest read time 1.1ms, write time 0.0ms, max retries 0
                                          === Move ===
                                          DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                                          === MainDDARing ===
                                          Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                          === AuxDDARing ===
                                          Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                          === Heat ===
                                          Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                          === GCodes ===
                                          Segments left: 0
                                          Movement lock held by null
                                          HTTP is idle in state(s) 0
                                          Telnet is idle in state(s) 0
                                          File is idle in state(s) 0
                                          USB is idle in state(s) 0
                                          Aux is idle in state(s) 0
                                          Trigger is idle in state(s) 0
                                          Queue is idle in state(s) 0
                                          LCD is idle in state(s) 0
                                          Daemon is idle in state(s) 0
                                          Autopause is idle in state(s) 0
                                          Code queue is empty.
                                          === Network ===
                                          Slowest loop: 182.04ms; fastest: 0.00ms
                                          Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                                          HTTP sessions: 1 of 8

                                          • WiFi -
                                            Network state is active
                                            WiFi module is connected to access point
                                            Failed messages: pending 0, notready 0, noresp 0
                                            WiFi firmware version 1.26
                                            WiFi MAC address bc:dd:c2:89:a2:9b
                                            WiFi Vcc 3.38, reset reason Turned on by main processor
                                            WiFi flash size 4194304, free heap 24160
                                            WiFi IP address 192.168.1.92
                                            WiFi signal strength -37dBm, mode 802.11n, reconnections 0, sleep mode modem
                                            Clock register 00002002
                                            Socket states: 0 0 0 0 0 0 0 0
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                                          • Phaedruxundefined
                                            Phaedrux Moderator @Andy Cohen
                                            last edited by Phaedrux

                                            @andy-cohen said in RRF Update to 3.3 just killed my FW:

                                            In the meantime the PanelDue is a 5.0i but it does not seem to want to update via the Duet. It's 3 years old. Think I'll need to remove it from it's containment and hit a resent button?

                                            I think you'll need to update it's firmware via usb as well so that it can communicate with RRF3 as well. I think the latest firmware is 3.4 for the paneldue. I think once you have it up to date with the firmware you'll actually be able to update it via DWC in the future.

                                            https://duet3d.dozuki.com/Wiki/PanelDue_Firmware_update#Section_Firmware_update_via_USB

                                            It looks like your main firmware and wifi firmware are up to date now. Can you confirm that DWC is also at 3.3?

                                            Z-Bot CoreXY Build | Thingiverse Profile

                                            Andy Cohenundefined 1 Reply Last reply Reply Quote 0
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