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    Strange Behavior , after "Pause" 'Cancel ""print again"

    Scheduled Pinned Locked Moved Solved
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    • moth4017undefined
      moth4017 @gloomyandy
      last edited by moth4017

      @gloomyandy

      M906 pre test X,y,Z 1000ma
      after Cancel print
      M906Motor current (mA) - X:1000, Y:1000, Z:1000, E:1400, idle factor 10%

      <

      gloomyandyundefined 1 Reply Last reply Reply Quote 0
      • gloomyandyundefined
        gloomyandy @moth4017
        last edited by

        @moth4017 Very odd? Do you always get those driver temperature errors when you have this problem?

        moth4017undefined 1 Reply Last reply Reply Quote 0
        • moth4017undefined
          moth4017 @gloomyandy
          last edited by

          @gloomyandy
          Hi Yes , but i can print ok if i send new G code , it only hppend after the above sequency

          <

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          • moth4017undefined
            moth4017 @Phaedrux
            last edited by moth4017

            @phaedrux
            If i add the cancel.g file when pressing "cancel" button the cancel.g file does not run, cancel.g file in system directory

            
            ;cancel.g
            M98 P/macros/home_max_Z
            
            ; home_max_Z
            M400                                                ; make sure everything has stopped before we make changes
            ;G91                                 				; relative positioning
            ;;M915 P0.4:0.5:0.6 S3 F0 R0                          ; Configure Z-Axis Stall Detection
            ;M913 Z80                                     		; Lower motor current by 50%
            ;M574 Z2 S4                                       	; Configure Z-Axis stall detection homing
            ;G91  												; relative positioning
            M98 P/macros/sensorless_Z      
            G1 F3000											; 
            G1 H1 Z350                           				; Home Z-Axis actuators independently
            M400                                             	; make sure everything has stopped before we make changes
            M913 Z100                                    		; Reset motor current
            G90                                  				; absolute positioning
            G92 Z290
            
            ;sensorless_z
            M915 P0.4:0.5:0.6 S3 F0 R0                          ; Configure Z-Axis Stall Detection
            M906 Z300	                                  		; Lower motor current by 50%
            M574 Z2 S4                                       	; Configure Z-Axis stall detection homing
            M400                                             	; make sure everything has stopped before we make changes
            M906 Z1000	                                  		; Reset motor current
            M400                
            
            

            <

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            • Phaedruxundefined
              Phaedrux Moderator
              last edited by

              Can you share the results of sending M122 and M98 P"config.g" ?

              Z-Bot CoreXY Build | Thingiverse Profile

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              • moth4017undefined
                moth4017 @Phaedrux
                last edited by

                @phaedrux ```
                3/11/2022, 11:01:06 AM M122
                === Diagnostics ===
                RepRapFirmware for Duet 3 Mini 5+ version 3.4.0rc2 (2022-02-22 17:07:31) running on Duet 3 Mini5plus WiFi (standalone mode)
                Board ID: 3R9YY-6T9RL-D65J0-40KMN-2UW2Z-RHYT0
                Used output buffers: 3 of 40 (15 max)
                === RTOS ===
                Static ram: 103652
                Dynamic ram: 110396 of which 0 recycled
                Never used RAM 27592, free system stack 132 words
                Tasks: NETWORK(ready,49.2%,228) HEAT(notifyWait,0.1%,356) Move(notifyWait,0.0%,292) CanReceiv(notifyWait,0.0%,942) CanSender(notifyWait,0.0%,356) CanClock(delaying,0.0%,339) TMC(notifyWait,3.6%,114) MAIN(running,44.5%,428) IDLE(ready,0.0%,29) AIN(delaying,2.5%,264), total 100.0%
                Owned mutexes: WiFi(NETWORK)
                === Platform ===
                Last reset 02:17:44 ago, cause: power up
                Last software reset at 2022-03-09 19:21, reason: User, GCodes spinning, available RAM 24040, slot 2
                Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                Error status: 0x00
                MCU revision 3, ADC conversions started 8264987, completed 8264987, timed out 0, errs 0
                Step timer max interval 754
                MCU temperature: min 28.5, current 30.2, max 32.7
                Supply voltage: min 23.8, current 23.9, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                Events: 0 queued, 0 completed
                Driver 0: pos 0, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 30414, writes 9, timeouts 0, DMA errors 0, CC errors 0
                Driver 1: pos 0, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 30414, writes 9, timeouts 0, DMA errors 0, CC errors 0
                Driver 2: pos 96320, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 30414, writes 9, timeouts 0, DMA errors 0, CC errors 0
                Driver 3: pos 0, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 30413, writes 9, timeouts 0, DMA errors 0, CC errors 0
                Driver 4: pos 0, standstill, SG min 174, read errors 0, write errors 0, ifcnt 16, reads 30407, writes 16, timeouts 0, DMA errors 0, CC errors 0
                Driver 5: pos 0, standstill, SG min 16, read errors 0, write errors 0, ifcnt 16, reads 30407, writes 16, timeouts 0, DMA errors 0, CC errors 0
                Driver 6: pos 0, standstill, SG min 26, read errors 0, write errors 0, ifcnt 16, reads 30407, writes 16, timeouts 0, DMA errors 0, CC errors 0
                Date/time: 2022-03-11 11:01:05
                Cache data hit count 4294967295
                Slowest loop: 5.52ms; fastest: 0.13ms
                === Storage ===
                Free file entries: 10
                SD card 0 detected, interface speed: 22.5MBytes/sec
                SD card longest read time 14.1ms, write time 0.0ms, max retries 0
                === Move ===
                DMs created 83, segments created 3, maxWait 624ms, bed compensation in use: none, comp offset 0.000
                === MainDDARing ===
                Scheduled moves 2, completed 2, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                === AuxDDARing ===
                Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                === Heat ===
                Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                === GCodes ===
                Segments left: 0
                Movement lock held by null
                HTTP is idle in state(s) 0
                Telnet is idle in state(s) 0
                File is idle in state(s) 0
                USB is idle in state(s) 0
                Aux is idle in state(s) 0
                Trigger is idle in state(s) 0
                Queue is idle in state(s) 0
                LCD is idle in state(s) 0
                SBC is idle in state(s) 0
                Daemon is idle in state(s) 0
                Aux2 is idle in state(s) 0
                Autopause is idle in state(s) 0
                Code queue is empty
                === CAN ===
                Messages queued 74382, received 0, lost 0, boc 0
                Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 18 (min 18), ts 41325/0/0
                Tx timeouts 0,0,41324,0,0,33056 last cancelled message type 30 dest 127
                === Network ===
                Slowest loop: 16.87ms; fastest: 0.00ms
                Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                HTTP sessions: 1 of 8

                • WiFi -
                  Network state is active
                  WiFi module is connected to access point
                  Failed messages: pending 0, notready 0, noresp 0
                  WiFi firmware version 1.25
                  WiFi MAC address f0:08:d1:02:a1:0b
                  WiFi Vcc 3.34, reset reason Power up
                  WiFi flash size 2097152, free heap 25512
                  WiFi IP address 192.168.0.19
                  WiFi signal strength -49dBm, mode 802.11n, reconnections 0, sleep mode modem
                  Clock register 00002002
                  Socket states: 0 0 0 0 0 0 0 0
                HTTP is enabled on port 80
                FTP is disabled
                TELNET is disabled

                <

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                • moth4017undefined
                  moth4017 @Phaedrux
                  last edited by

                  @phaedrux
                  hi any thourghts?

                  <

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                  • Phaedruxundefined
                    Phaedrux Moderator @moth4017
                    last edited by

                    @moth4017 said in Strange Behavior , after "Pause" 'Cancel ""print again":

                    @phaedrux
                    If i add the cancel.g file when pressing "cancel" button the cancel.g file does not run, cancel.g file in system directory

                    
                    ;cancel.g
                    M98 P/macros/home_max_Z
                    
                    ; home_max_Z
                    M400                                                ; make sure everything has stopped before we make changes
                    ;G91                                 				; relative positioning
                    ;;M915 P0.4:0.5:0.6 S3 F0 R0                          ; Configure Z-Axis Stall Detection
                    ;M913 Z80                                     		; Lower motor current by 50%
                    ;M574 Z2 S4                                       	; Configure Z-Axis stall detection homing
                    ;G91  												; relative positioning
                    M98 P/macros/sensorless_Z      
                    G1 F3000											; 
                    G1 H1 Z350                           				; Home Z-Axis actuators independently
                    M400                                             	; make sure everything has stopped before we make changes
                    M913 Z100                                    		; Reset motor current
                    G90                                  				; absolute positioning
                    G92 Z290
                    
                    ;sensorless_z
                    M915 P0.4:0.5:0.6 S3 F0 R0                          ; Configure Z-Axis Stall Detection
                    M906 Z300	                                  		; Lower motor current by 50%
                    M574 Z2 S4                                       	; Configure Z-Axis stall detection homing
                    M400                                             	; make sure everything has stopped before we make changes
                    M906 Z1000	                                  		; Reset motor current
                    M400                
                    
                    

                    Can you try a simplified cancel.g? Maybe just a G28 XY

                    Z-Bot CoreXY Build | Thingiverse Profile

                    moth4017undefined 1 Reply Last reply Reply Quote 0
                    • moth4017undefined
                      moth4017 @Phaedrux
                      last edited by

                      @phaedrux

                      ;cancel.g
                      G28 X Y

                      The console displayed this after cancel print:-
                      M0
                      Printing paused at X128.9 Y78.9 Z0.3
                      Cancelled printing file 0:/gcodes/shark-v2-0-a_0.35mm_PLA__2h32m.gcode, print time was 0h 5m

                      the Cancel.g file didnt run, so i put "G28 X Y" in the command line , this ran perfectly , but then i got this error in the console , only happens when i do the "Cancel"

                      3/16/2022, 7:56:33 PM Error: Driver 0.4 error: over temperature shutdown
                      3/16/2022, 7:56:33 PM Emergency stop, attemping to reconnect...
                      3/16/2022, 7:56:31 PM Error: Driver 0.6 error: over temperature shutdown
                      3/16/2022, 7:56:31 PM Error: Driver 0.5 error: over temperature shutdown
                      3/16/2022, 7:56:30 PM Error: Driver 0.4 error: over temperature shutdown

                      <

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                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        It seems like it's not picking up your files.

                        Can you get a fresh SD card out and set it up with fresh files entirely? Get a clean basic config from the config tool.

                        Maybe post some screen shots of your file structure? Or zip up your entire SD card minus the gcodes folder and post that?

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • moth4017undefined
                          moth4017 @Phaedrux
                          last edited by moth4017

                          @phaedrux
                          Is there a reason it would not read the cancel.g only as if i change any macro files they are being read.

                          i will try i new install though

                          <

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                          • moth4017undefined
                            moth4017 @Phaedrux
                            last edited by

                            @phaedrux

                            So to check if the SD card was writing/reading i put the "G28 X Y" into the pause.g file to test it was working, and yes the pause.g did the "G28 X Y" but it still does not read the cancel.g file i have alsso updated to the new 3.4.0 version released today

                            <

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                            • moth4017undefined
                              moth4017
                              last edited by

                              @phaedrux
                              new Firmware loaded
                              M122
                              === Diagnostics ===
                              RepRapFirmware for Duet 3 Mini 5+ version 3.4.0 (2022-03-15 18:59:15) running on Duet 3 Mini5plus WiFi (standalone mode)
                              Board ID: 3R9YY-6T9RL-D65J0-40KMN-2UW2Z-RHYT0
                              Used output buffers: 3 of 40 (19 max)
                              === RTOS ===
                              Static ram: 103684
                              Dynamic ram: 110484 of which 0 recycled
                              Never used RAM 27472, free system stack 132 words
                              Tasks: NETWORK(ready,11.6%,202) HEAT(notifyWait,0.0%,342) Move(notifyWait,0.0%,292) CanReceiv(notifyWait,0.0%,942) CanSender(notifyWait,0.0%,356) CanClock(delaying,0.0%,337) TMC(delaying,1.1%,114) MAIN(running,86.1%,428) IDLE(ready,0.2%,29) AIN(delaying,0.8%,264), total 100.0%
                              Owned mutexes: WiFi(NETWORK)
                              === Platform ===
                              Last reset 00:01:36 ago, cause: software
                              Last software reset at 2022-03-18 15:14, reason: User, GCodes spinning, available RAM 23704, slot 0
                              Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                              Error status: 0x00
                              MCU revision 3, ADC conversions started 96385, completed 96385, timed out 0, errs 0
                              Step timer max interval 751
                              MCU temperature: min 35.9, current 36.4, max 41.2
                              Supply voltage: min 23.7, current 23.9, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
                              Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                              Events: 0 queued, 0 completed
                              Driver 0: standstill, SG min 0, read errors 0, write errors 1, ifcnt 26, reads 8712, writes 9, timeouts 0, DMA errors 0, CC errors 0
                              Driver 1: standstill, SG min 2, read errors 0, write errors 1, ifcnt 26, reads 8712, writes 9, timeouts 0, DMA errors 0, CC errors 0
                              Driver 2: standstill, SG min 0, read errors 0, write errors 1, ifcnt 19, reads 8712, writes 9, timeouts 0, DMA errors 0, CC errors 0
                              Driver 3: standstill, SG min 2, read errors 0, write errors 1, ifcnt 25, reads 8712, writes 9, timeouts 0, DMA errors 0, CC errors 0
                              Driver 4: standstill, SG min 46, read errors 0, write errors 1, ifcnt 53, reads 8706, writes 15, timeouts 0, DMA errors 0, CC errors 0
                              Driver 5: standstill, SG min 14, read errors 0, write errors 1, ifcnt 55, reads 8705, writes 16, timeouts 0, DMA errors 0, CC errors 0
                              Driver 6: standstill, SG min 74, read errors 0, write errors 1, ifcnt 51, reads 8705, writes 16, timeouts 0, DMA errors 0, CC errors 0
                              Date/time: 2022-03-18 15:16:32
                              Cache data hit count 187991149
                              Slowest loop: 5.91ms; fastest: 0.13ms
                              === Storage ===
                              Free file entries: 10
                              SD card 0 detected, interface speed: 22.5MBytes/sec
                              SD card longest read time 1.0ms, write time 0.0ms, max retries 0
                              === Move ===
                              DMs created 83, segments created 3, maxWait 624ms, bed compensation in use: none, comp offset 0.000
                              === MainDDARing ===
                              Scheduled moves 2, completed 2, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                              === AuxDDARing ===
                              Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                              === Heat ===
                              Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                              === GCodes ===
                              Segments left: 0
                              Movement lock held by null
                              HTTP is idle in state(s) 0
                              Telnet is idle in state(s) 0
                              File is idle in state(s) 0
                              USB is idle in state(s) 0
                              Aux is idle in state(s) 0
                              Trigger is idle in state(s) 0
                              Queue is idle in state(s) 0
                              LCD is idle in state(s) 0
                              SBC is idle in state(s) 0
                              Daemon is idle in state(s) 0
                              Aux2 is idle in state(s) 0
                              Autopause is idle in state(s) 0
                              Code queue is empty
                              === CAN ===
                              Messages queued 864, received 0, lost 0, boc 0
                              Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 18 (min 18), ts 481/0/0
                              Tx timeouts 0,0,480,0,0,382 last cancelled message type 30 dest 127
                              === Network ===
                              Slowest loop: 138.62ms; fastest: 0.00ms
                              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                              HTTP sessions: 1 of 8

                              • WiFi -
                                Network state is active
                                WiFi module is connected to access point
                                Failed messages: pending 0, notready 0, noresp 0
                                WiFi firmware version 1.25
                                WiFi MAC address f0:08:d1:02:a1:0b
                                WiFi Vcc 3.34, reset reason Power up
                                WiFi flash size 2097152, free heap 25512
                                WiFi IP address 192.168.0.19
                                WiFi signal strength -53dBm, mode 802.11n, reconnections 0, sleep mode modem
                                Clock register 00002002
                                Socket states: 0 0 0 0 0 0 0 0

                              Still getting this error after "Pause" "Cancel" "print again"

                              Cancelled printing file 0:/gcodes/shark-v2-0-a_0.35mm_PLA__2h32m.gcode, print time was 0h 0m
                              Error: Failed to home axes
                              Error: Driver 0.5 error: over temperature shutdown
                              Error: Driver 0.4 error: over temperature shutdown
                              Error: Driver 0.5 error: over temperature shutdown
                              Error: Driver 0.4 error: over temperature shutdown
                              Error: Driver 0.5 error: over temperature shutdown

                              <

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                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by

                                Can you upload your actual files for pause.g and cancel.g?

                                Z-Bot CoreXY Build | Thingiverse Profile

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                                • moth4017undefined
                                  moth4017 @Phaedrux
                                  last edited by moth4017

                                  @phaedrux
                                  ;cancel.g
                                  G28 X Y

                                  ; pause.g
                                  ; called when a print from SD card is paused
                                  ;
                                  ; generated by RepRapFirmware Configuration Tool v3.3.10 on Thu Dec 30 2021 11:07:38 GMT+1300 (New Zealand Daylight Time)
                                  M83 ; relative extruder moves
                                  G1 E-10 F3600 ; retract 10mm of filament
                                  G91 ; relative positioning
                                  G1 Z5 F360 ; lift Z by 5mm
                                  G90 ; absolute positioning
                                  G1 X0 Y0 F6000 ; go to X=0 Y=0
                                  G28 X Y

                                  The G28 X Y works on pause.g but still not on cancel.g

                                  <

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                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by Phaedrux

                                    Can you drag and drop the actual files to upload them? That way we can see if there are any non-standard characters or something like that in the file itself.

                                    And since it's calling some homing files, perhaps you can share those as well. Maybe there is something happening in homex and homey.

                                    Z-Bot CoreXY Build | Thingiverse Profile

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                                    • moth4017undefined
                                      moth4017 @Phaedrux
                                      last edited by

                                      @phaedrux ```

                                      ;cancel.g
                                      G28 X Y 
                                      
                                      ; homex.g
                                      ; called to home the X axis
                                      ;M98 P/macros/sensorless_Z
                                      G91               		; relative positioning
                                      G1 H1 X-235 F12000 		; move quickly to X axis endstop and stop there (first pass)
                                      G1 H2 X15 F6000    		; go back a few mm
                                      G1 H1 X-235 F360  		; move slowly to X axis endstop once more (second pass)
                                      ;G1 H2 Z-5 F12000   		; lower Z again
                                      G90  					; absolute positioning
                                      G1 X20 F6000			; go to X 0 print area
                                      G92 X0					; set X to 0 position
                                      
                                      ;sensorless_z
                                      M915 P0.4:0.5:0.6 S3 F0 R0                          ; Configure Z-Axis Stall Detection
                                      M906 Z300	                                  		; Lower motor current by 50%
                                      M574 Z2 S4                                       	; Configure Z-Axis stall detection homing
                                      M400                                             	; make sure everything has stopped before we make changes
                                      M906 Z1000	                                  		; Reset motor current
                                      M400               
                                      
                                      ; homey.g
                                      ; called to home the Y axis
                                      ;
                                      ; generated by RepRapFirmware Configuration Tool v3.3.10 on Thu Dec 30 2021 11:07:38 GMT+1300 (New Zealand Daylight Time)
                                      M98 P/macros/sensorless_Z
                                      G91               			; relative positioning
                                      G1 H1 Y315 F12000 			; move quickly to Y axis endstop and stop there (first pass)
                                      G1 H2 Y15 F12000    		; go back a few mm
                                      G1 H1 Y315 F360  			; move slowly to Y axis endstop once more (second pass)
                                      ;G1 H2 Z-5 F12000   			; higher Z again
                                      G90               			; absolute positioning
                                      G1 Y0 F6000					; go to X 0 print area
                                      G92 Y0						; set X to 0 position```
                                      
                                      
                                      ; pause.g
                                      ; called when a print from SD card is paused
                                      ;
                                      ; generated by RepRapFirmware Configuration Tool v3.3.10 on Thu Dec 30 2021 11:07:38 GMT+1300 (New Zealand Daylight Time)
                                      M83            ; relative extruder moves
                                      G1 E-10 F3600  ; retract 10mm of filament
                                      G91            ; relative positioning
                                      G1 Z5 F360     ; lift Z by 5mm
                                      G90            ; absolute positioning
                                      G1 X0 Y0 F6000 ; go to X=0 Y=0
                                      G28 X Y 
                                      
                                      

                                      <

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                                      • Phaedruxundefined
                                        Phaedrux Moderator @moth4017
                                        last edited by

                                        @moth4017 said in Strange Behavior , after "Pause" 'Cancel ""print again":

                                        M98 P/macros/sensorless_Z

                                        You may need to start quoting your file names when calling macros. It should be fine in standalone mode, but in SBC mode it is required and may be required in standalone in the future.

                                        It's a long shot, but still worth a shot.

                                        M98 P"/macros/sensorless_Z"

                                        Z-Bot CoreXY Build | Thingiverse Profile

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                                        • moth4017undefined
                                          moth4017 @Phaedrux
                                          last edited by

                                          @phaedrux
                                          No change

                                          Cancelled printing file 0:/gcodes/Body1_0.35mm_ABS__17m.gcode, print time was 0h 0m
                                          Error: Failed to home axes
                                          Error: Driver 0.4 error: over temperature shutdown
                                          Error: Driver 0.5 error: over temperature shutdown
                                          Error: Driver 0.4 error: over temperature shutdown
                                          Error: Driver 0.5 error: over temperature shutdown
                                          Error: Driver 0.4 error: over temperature shutdown
                                          Error: Driver 0.5 error: over temperature shutdown
                                          Error: Driver 0.4 error: over temperature shutdown
                                          Error: Driver 0.5 error: over temperature shutdown
                                          Warning: Driver 0.5 warning: over temperature warning
                                          Warning: Driver 0.4 warning: over temperature warning

                                          <

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                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            Are your drivers actually getting hot to the touch or are they spurious warnings? Printing is working correctly, right?

                                            Z-Bot CoreXY Build | Thingiverse Profile

                                            moth4017undefined 1 Reply Last reply Reply Quote 0
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