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DUEX 5 V0.8 TO DUEX 5 V0.11

Scheduled Pinned Locked Moved
Duet Hardware and wiring
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  • undefined
    paolozampini1973 @droftarts
    last edited by 21 Mar 2022, 13:50

    @droftarts 21/3/2022, 14:42:59 M122
    === Diagnostics ===
    RepRapFirmware for Duet 2 WiFi/Ethernet version 3.3 (2021-06-15 21:44:54) running on Duet WiFi 1.02 or later + DueX2
    Board ID: 0JD0M-9P6M2-NW4SN-6J1DD-3SJ6K-KAURK
    Used output buffers: 3 of 24 (24 max)
    === RTOS ===
    Static ram: 23876
    Dynamic ram: 77448 of which 0 recycled
    Never used RAM 13092, free system stack 184 words
    Tasks: NETWORK(ready,15.8%,233) HEAT(delaying,0.0%,330) Move(notifyWait,0.1%,319) DUEX(notifyWait,0.0%,24) MAIN(running,81.5%,413) IDLE(ready,2.6%,29), total 100.0%
    Owned mutexes: WiFi(NETWORK)
    === Platform ===
    Last reset 00:00:29 ago, cause: power up
    Last software reset at 2022-03-20 12:12, reason: User, GCodes spinning, available RAM 13092, slot 0
    Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
    Error status: 0x00
    Aux0 errors 0,0,0
    Step timer max interval 0
    MCU temperature: min 24.0, current 27.5, max 27.7
    Supply voltage: min 25.6, current 25.7, max 25.8, under voltage events: 0, over voltage events: 0, power good: yes
    Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
    Driver 0: position 0, standstill, SG min/max not available
    Driver 1: position 0, standstill, SG min/max not available
    Driver 2: position 0, standstill, SG min/max not available
    Driver 3: position 0, standstill, SG min/max not available
    Driver 4: position 0, standstill, SG min/max not available
    Driver 5: position 0, standstill, SG min/max not available
    Driver 6: position 0, standstill, SG min/max not available
    Driver 7: position 0
    Driver 8: position 0
    Driver 9: position 0
    Driver 10: position 0
    Driver 11: position 0
    Date/time: 2022-03-21 14:42:57
    Cache data hit count 1127564131
    Slowest loop: 10.85ms; fastest: 0.18ms
    I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
    === Storage ===
    Free file entries: 10
    SD card 0 detected, interface speed: 20.0MBytes/sec
    SD card longest read time 1.0ms, write time 0.0ms, max retries 0
    === Move ===
    DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
    === MainDDARing ===
    Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
    === AuxDDARing ===
    Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
    === Heat ===
    Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
    Heater 1 is on, I-accum = 0.0
    === GCodes ===
    Segments left: 0
    Movement lock held by null
    HTTP is idle in state(s) 0
    Telnet is idle in state(s) 0
    File is idle in state(s) 0
    USB is idle in state(s) 0
    Aux is idle in state(s) 0
    Trigger is idle in state(s) 0
    Queue is idle in state(s) 0
    LCD is idle in state(s) 0
    Daemon is idle in state(s) 0
    Autopause is idle in state(s) 0
    Code queue is empty.
    === Filament sensors ===
    Extruder 0 sensor: no filament
    Extruder 1 sensor: ok
    Extruder 2 sensor: no filament
    Extruder 3 sensor: ok
    === DueX ===
    Read count 1, 2.04 reads/min
    === Network ===
    Slowest loop: 41.04ms; fastest: 0.00ms
    Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
    HTTP sessions: 1 of 8

    • WiFi -
      Network state is active
      WiFi module is connected to access point
      Failed messages: pending 0, notready 0, noresp 0
      WiFi firmware version 1.26
      WiFi MAC address 40:f5:20:0d:6b:49
      WiFi Vcc 3.37, reset reason Turned on by main processor
      WiFi flash size 4194304, free heap 23760
      WiFi IP address 192.168.1.5
      WiFi signal strength -64dBm, mode 802.11n, reconnections 0, sleep mode modem
      Clock register 00002002
      Socket states: 0 0 0 0 0 0 0 0
      21/3/2022, 14:42:46 Connected to 192.168.1.5
    undefined 1 Reply Last reply 21 Mar 2022, 13:50 Reply Quote 0
    • undefined
      droftarts administrators @paolozampini1973
      last edited by 21 Mar 2022, 13:50

      @paolozampini1973 Great! Now config.g.

      Ian

      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

      undefined 3 Replies Last reply 21 Mar 2022, 13:51 Reply Quote 0
      • undefined
        paolozampini1973 @droftarts
        last edited by 21 Mar 2022, 13:51

        @droftarts config (17).g

        1 Reply Last reply Reply Quote 0
        • undefined
          paolozampini1973 @droftarts
          last edited by paolozampini1973 21 Mar 2022, 13:55

          @droftarts I am sending you a photo to make you understand the axes are made up entirely with sfU 1204 and 15 mm linear guides
          4 ESTRUDE .jpeg

          undefined 1 Reply Last reply 21 Mar 2022, 14:04 Reply Quote 0
          • undefined
            droftarts administrators @paolozampini1973
            last edited by 21 Mar 2022, 14:04

            @paolozampini1973 There are a lot of errors in you config.g. Just to start...

            ; Drives
            M569 P0 S0 R-1 ;T2.5:2.5:6:5 ; X physical drive 0 goes forwards
            M569 P1 S1 R-1 ;T2.5:2.5:6:5 ; Y physical drive 1 goes forwards
            M569 P2 S1 R1 T5:5:5:5 ; Z physical drive 2 goes forwards
            M569 P3 S0 ; E0 physical drive 3 goes forwards
            M569 P4 S0 ; E1 physical drive 4 goes forwards
            M569 P5 S0 ; E2 physical drive 5 goes forwards
            M569 P6 S0 ; E3 physical drive 6 goes forwards
            M569 P7 S0 R1 T2:2:2:5 ; E4 X physical drive 7 goes forwards
            M569 P8 S1 R1 T2:2:2:5 ; E5 Y physical drive 8 goes forwards
            M569 P9 S1 R1 T5:5:5:5 ; E6 Z physical drive 9 goes forwards
            M584 X7 Y8 Z2:9 E3:4:5:6:7:8:9 S0 ; set drive mapping

            Don't set timings for internal TMC drivers. (M569 P2 S1 R1 T5:5:5:5)
            Your timings for the external drivers are very short.
            Your M584 should not have the X, Y and Z2 drivers mapped to E. S0 is not needed. Change to:

            M584 X7 Y8 Z2:9 E3:4:5:6
            

            For M350, M92, M566, M203, M201 and M906 commands, make sure E has 4 parameters, eg

            M350 X16 Y16 Z16 E16:16:16:16 I1
            

            Ian

            Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

            undefined 1 Reply Last reply 21 Mar 2022, 14:07 Reply Quote 0
            • undefined
              paolozampini1973 @droftarts
              last edited by 21 Mar 2022, 14:04

              @droftarts what idea did you get what you think?

              1 Reply Last reply Reply Quote 0
              • undefined
                paolozampini1973 @droftarts
                last edited by paolozampini1973 21 Mar 2022, 14:07

                @droftarts Then send me the correct file as you think you are right and I will load it and do the tests you think that for this I lose the steps?

                at this point what do I do I reassemble the v08 or I leave the V 011 I am willing to do any test Thank you please fill in the config file for me and I will load it exactly as you give it to me and I will let you know

                undefined 2 Replies Last reply 21 Mar 2022, 14:20 Reply Quote 0
                • undefined
                  droftarts administrators @paolozampini1973
                  last edited by 21 Mar 2022, 14:20

                  @paolozampini1973 What exact thermistors are you using? You have set the default, which will not be correct, and probably why temperature is incorrect.

                  M308 S0 P"bedtemp" Y"thermistor" T100000 B4138
                  

                  And you need to move Z2 from driver 9 on DueX to driver 0 or 1 on Duet 2. You DueX is being recognised as a DueX2, so probably driver 9 is not working. If it is using an external driver, don't do that; drives on a shared axis need to be identical.

                  Ian

                  Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                  undefined 2 Replies Last reply 21 Mar 2022, 14:22 Reply Quote 0
                  • undefined
                    paolozampini1973 @droftarts
                    last edited by 21 Mar 2022, 14:22

                    @droftarts Yes I set it to DUEX2 because the axes moved when I turned on the electronics Now I can't on DUEX5 Thanks for the dictation problems but for now it is more important to solve the problem of pitch loss and axis movement

                    1 Reply Last reply Reply Quote 0
                    • undefined
                      paolozampini1973 @droftarts
                      last edited by 21 Mar 2022, 14:23

                      @droftarts Yes I know that the engines must be identical and are identical

                      1 Reply Last reply Reply Quote 0
                      • undefined
                        droftarts administrators @paolozampini1973
                        last edited by 21 Mar 2022, 14:23

                        @paolozampini1973 said in DUEX 5 V0.8 TO DUEX 5 V0.11:

                        @droftarts Then send me the correct file as you think you are right and I will load it and do the tests you think that for this I lose the steps?

                        at this point what do I do I reassemble the v08 or I leave the V 011 I am willing to do any test Thank you please fill in the config file for me and I will load it exactly as you give it to me and I will let you know

                        It will have to be later, I have other things I must do.

                        I'd keep the V011 in for now.

                        Please show how you have wired the 74HC level shifters. Wiring diagram and/or photo.

                        Ian

                        Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                        undefined 3 Replies Last reply 21 Mar 2022, 14:25 Reply Quote 0
                        • undefined
                          paolozampini1973 @droftarts
                          last edited by paolozampini1973 21 Mar 2022, 14:25

                          @droftarts Listen to the 74hc I have to take it apart Because it gives me more problems it practically skips the steps at the entrance I have to give it three times and 8 and it doesn't skip my steps but if I give it 5 volts it skips my steps it practically gets worse

                          I did as you told me but the axes move by themselves without command Both X and Y

                          undefined 1 Reply Last reply 21 Mar 2022, 14:56 Reply Quote 0
                          • undefined
                            paolozampini1973 @droftarts
                            last edited by paolozampini1973 21 Mar 2022, 14:35

                            @droftarts I would like to leave V 011 but the Y x move without giving it the command so it is useless to talk about other problems there is to solve the first This is the problem Okay I'll wait when you get free I'll publish the config file thanks

                            21/3/2022, 15:38:13 Error: short-to-ground reported by driver(s) 7 8
                            Error: over temperature shutdown reported by driver(s) 7 8
                            21/3/2022, 15:38:08 Error: short-to-ground reported by driver(s) 7 8
                            Error: over temperature shutdown reported by driver(s) 7 8
                            21/3/2022, 15:38:04 Error: short-to-ground reported by driver(s) 7 8
                            Error: over temperature shutdown reported by driver(s) 7 8
                            21/3/2022, 15:37:59 Error: short-to-ground reported by driver(s) 7 8
                            Error: over temperature shutdown reported by driver(s) 7 8
                            21/3/2022, 15:37:55 Error: short-to-ground reported by driver(s) 7 8
                            Error: over temperature shutdown reported by driver(s) 7 8
                            21/3/2022, 15:37:50 Error: short-to-ground reported by driver(s) 7 8
                            Error: over temperature shutdown reported by driver(s) 7 8
                            21/3/2022, 15:37:49 M122
                            === Diagnostics ===
                            RepRapFirmware for Duet 2 WiFi/Ethernet version 3.3 (2021-06-15 21:44:54) running on Duet WiFi 1.02 or later + DueX5
                            Board ID: 0JD0M-9P6M2-NW4SN-6J1DD-3SJ6K-KAURK
                            Used output buffers: 3 of 24 (20 max)
                            === RTOS ===
                            Static ram: 23876
                            Dynamic ram: 77448 of which 0 recycled
                            Never used RAM 13092, free system stack 184 words
                            Tasks: NETWORK(ready,10.4%,231) HEAT(delaying,0.1%,330) Move(notifyWait,0.1%,319) DUEX(notifyWait,0.0%,24) MAIN(running,86.5%,411) IDLE(ready,3.0%,29), total 100.0%
                            Owned mutexes:
                            === Platform ===
                            Last reset 00:00:25 ago, cause: software
                            Last software reset at 2022-03-21 15:37, reason: User, GCodes spinning, available RAM 13092, slot 1
                            Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                            Error status: 0x00
                            Aux0 errors 0,0,0
                            Step timer max interval 0
                            MCU temperature: min 29.3, current 30.0, max 30.3
                            Supply voltage: min 25.6, current 25.7, max 25.8, under voltage events: 0, over voltage events: 0, power good: yes
                            Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                            Driver 0: position 0, standstill, SG min/max not available
                            Driver 1: position 0, standstill, SG min/max not available
                            Driver 2: position 0, standstill, SG min/max not available
                            Driver 3: position 0, standstill, SG min/max not available
                            Driver 4: position 0, standstill, SG min/max not available
                            Driver 5: position 0, standstill, SG min/max not available
                            Driver 6: position 0, standstill, SG min/max not available
                            Driver 7: position 0, temperature-shutdown! short-to-ground, standstill, SG min/max not available
                            Driver 8: position 0, temperature-shutdown! short-to-ground, standstill, SG min/max not available
                            Driver 9: position 0, standstill, SG min/max not available
                            Driver 10: position 0
                            Driver 11: position 0
                            Date/time: 2022-03-21 15:37:49
                            Cache data hit count 981081507
                            Slowest loop: 6.48ms; fastest: 0.19ms
                            I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                            === Storage ===
                            Free file entries: 10
                            SD card 0 detected, interface speed: 20.0MBytes/sec
                            SD card longest read time 1.0ms, write time 0.0ms, max retries 0
                            === Move ===
                            DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                            === MainDDARing ===
                            Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                            === AuxDDARing ===
                            Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                            === Heat ===
                            Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                            Heater 1 is on, I-accum = 0.0
                            === GCodes ===
                            Segments left: 0
                            Movement lock held by null
                            HTTP is idle in state(s) 0
                            Telnet is idle in state(s) 0
                            File is idle in state(s) 0
                            USB is idle in state(s) 0
                            Aux is idle in state(s) 0
                            Trigger is idle in state(s) 0
                            Queue is idle in state(s) 0
                            LCD is idle in state(s) 0
                            Daemon is idle in state(s) 0
                            Autopause is idle in state(s) 0
                            Code queue is empty.
                            === Filament sensors ===
                            Extruder 0 sensor: no filament
                            Extruder 1 sensor: ok
                            Extruder 2 sensor: no filament
                            Extruder 3 sensor: ok
                            === DueX ===
                            Read count 1, 2.36 reads/min
                            === Network ===
                            Slowest loop: 39.88ms; fastest: 0.00ms
                            Responder states: HTTP(2) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                            HTTP sessions: 1 of 8

                            • WiFi -
                              Network state is active
                              WiFi module is connected to access point
                              Failed messages: pending 0, notready 0, noresp 0
                              WiFi firmware version 1.26
                              WiFi MAC address 40:f5:20:0d:6b:49
                              WiFi Vcc 3.37, reset reason Turned on by main processor
                              WiFi flash size 4194304, free heap 20888
                              WiFi IP address 192.168.1.5
                              WiFi signal strength -64dBm, mode 802.11n, reconnections 0, sleep mode modem
                              Clock register 00002002
                              Socket states: 0 4 0 0 0 0 0 0
                              21/3/2022, 15:37:46 Error: short-to-ground reported by driver(s) 7 8
                              Error: over temperature shutdown reported by driver(s) 7 8
                              21/3/2022, 15:37:41 Error: short-to-ground reported by driver(s) 7 8
                              Error: over temperature shutdown reported by driver(s) 7 8
                              21/3/2022, 15:37:39 Connected to 192.168.1.5
                              config (18).g
                            1 Reply Last reply Reply Quote 0
                            • undefined
                              droftarts administrators @paolozampini1973
                              last edited by 21 Mar 2022, 14:56

                              @paolozampini1973 said in DUEX 5 V0.8 TO DUEX 5 V0.11:

                              I did as you told me but the axes move by themselves without command Both X and Y

                              Is that in both DueX2 mode and DueX5 mode?

                              Ian

                              Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                              undefined 4 Replies Last reply 21 Mar 2022, 14:58 Reply Quote 0
                              • undefined
                                paolozampini1973 @droftarts
                                last edited by 21 Mar 2022, 14:56

                                @droftarts As you can see the errors alone are only when AND IN DUEX MODE 5 DRIVER 7+ DRIVER 8 ARE OFF IN DUEX 2 MODE IT DOESN'T GIVE SHORT-CIRCUIT ERRORS SO IT IS NOT NORMAL IN MY MEETING

                                1 Reply Last reply Reply Quote 0
                                • undefined
                                  paolozampini1973 @droftarts
                                  last edited by 21 Mar 2022, 14:58

                                  @droftarts No in DUEX2 MODE they do not move by themselves they move only with the command IN DUEX5 MODE THE MOVEMENT HAS BEEN ALONE WITHOUT COMMAND

                                  tekkydaveundefined 1 Reply Last reply 21 Mar 2022, 15:08 Reply Quote 0
                                  • undefined
                                    paolozampini1973 @droftarts
                                    last edited by 21 Mar 2022, 15:04

                                    @droftarts from my experience it tells me that this expansion has problems but I think they are more software problems and not hardware problems Tell me what you think
                                    Also because I'm sorry if I always repeat the same thing but I find myself with so many problems that I did not have Maybe some of these problems are not aware I will tell you more I tried to disconnect everything on the problem outputs it gives the same so on all the drivers I am disconnected disconnected nothing is connected and it still gives problems in duex 5 mode

                                    1 Reply Last reply Reply Quote 0
                                    • tekkydaveundefined
                                      tekkydave @paolozampini1973
                                      last edited by tekkydave 21 Mar 2022, 15:08

                                      @paolozampini1973 You need to run the Duex in Duex2 mode. In this way it will disable the internal drivers on 7,8,9 allowing you to have external drivers on 7 & 8 for your X & Y axes.
                                      If you have it in Duex5 mode BOTH the internal and external drivers are connected which is causing the movement without commands.

                                      ~ tekkydave ~
                                      D-Bot: 300x300mm | Duet WiFi + Duex2 | 3 independent z motors | X,Y & Z linear rails | E3D Titan Aero + V6 | Precision Piezo z-probe
                                      FreeCAD, PrusaSlicer

                                      undefined 1 Reply Last reply 21 Mar 2022, 15:10 Reply Quote 0
                                      • undefined
                                        paolozampini1973 @droftarts
                                        last edited by 21 Mar 2022, 15:09

                                        @droftarts Listen to me when I say something and before I say something I think about it I don't talk to Ugh the problem now that I still have to solve the problem But you have to understand you are a hardware problem or a software problem as I said before for me it is a software problem and obviously before I had a small problem now I have big problems so what I ask you and please please please at least try to understand if it is a hardware problem or a software problem because otherwise I am forced to upgrade to version 0.8

                                        unless I could print with some pitch loss problem but at least I could print now I have practically the printer stopped

                                        1 Reply Last reply Reply Quote 0
                                        • undefined
                                          paolozampini1973 @tekkydave
                                          last edited by 21 Mar 2022, 15:10

                                          @tekkydave Excuse me but if I do as you say or three motors that I cannot use then I still have a big problem So what is the advantage of having bought the 011 version because I have these problems that I have with the 011 I did not have them so explain to me you this solution that you recommend me maybe I don't understand Thanks very kind

                                          tekkydaveundefined 1 Reply Last reply 21 Mar 2022, 15:15 Reply Quote 0
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