Reboots/resets randomly - RRF 3.5.0-b4
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@dc42 here is my config.g. my reboots happened right after boot up but in certain homed states. it was combinations of homing individual axis vs a homeall which would crash and not complete successfully. and i was experimenting with adding K11 and removing K11 vs K1 from my M669. i dont recall which i was using at the time. they all rebooted, but some worse than others in terms of repeating over and over.
M669 K11 X1:0:0:0 Y1:-1:0:-1 Z0:0:1:0 U0:0:0:1
; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"V-Core3" ; set printer name ;M669 K11 Y1:-1:0:-1 ; Dual Markforged Kinematics https://forum.duet3d.com/topic/7796/haq-xy/125 https://forum.duet3d.com/topic/21021/dual-markforged-kinematics?_=1672244913067 ;M669 K1 X1:0:0:0 Y1:-1:0:-1 Z0:0:1:0 U0:0:0:1 ; Matrix mapping for Axis - X:Y:Z:U M669 X1:0:0:0 Y1:-1:0:-1 Z0:0:1:0 U0:0:0:1 ; Matrix mapping for Axis - X:Y:Z:U G21 ; Set Units to Millimeters ; Network M552 S2 ; enable network, note P0.0.0.0 sets auto DHCP M553 P255.255.255.0 ; set subnet mask M554 P192.168.1.20 ; set gateway M586 P0 S1 ; enable HTTP M586 P1 S0 ; disable FTP M586 P2 S0 ; disable Telnet G4 S2 ; wait for expansion boards to start ; Drives M569 P0.0 S0 D2 ; Left Z physical drive 0.0 goes forwards M569 P0.1 S0 D2 ; Rear Z physical drive 0.1 goes forwards M569 P0.2 S0 D2 ; Right Z physical drive 0.2 goes forwards M569 P0.3 S1 D2 ; Right U toolhead drive 0.3 goes forwards M569 P0.4 S1 D2 ; Left X toolhead drive 0.4 goes forwards M569 P0.5 S0 D2 ; Left Y drive 0.5 goes forwards M569 P0.6 S1 D2 ; Right Y drive 0.6 goes reverse M569 P20.0 S1 D2 ; Extruder physical drive 20.0 goes forwards Toolboard 1LC M569 P21.0 S1 D2 ; Extruder physical drive 21.0 goes forwards Toolboard 1LC M569 P1.0 S0 D2 ; Extruder physical drive 1.0 goes forwards Expansion 3HC M569 P1.1 S0 D2 ; Extruder physical drive 1.1 goes forwards Expansion 3HC M569 P1.2 S1 D2 ; Extruder physical drive 1.2 goes forwards Expansion 3HC M584 Z0.0:0.1:0.2 Y0.5:0.6 X0.4 U0.3 E20.0:21.0:1.0:1.1 ; set drive mapping M350 U16 X16 Y16 Z16 E16:16:16:16 I1 ; configure microstepping with interpolation M92 U80.0 X80.00 Y80.00 Z800.00 E690:690:690:690 ; set steps per mm M906 U2000 X2000 Y2000 Z1800 E1000:1000:1000:1000 I30 ; set motor currents (mA) and motor idle factor in per cent -- safe for Duet 3 mini 5+ M84 S30 ; Set idle timeout ;M98 P"0:/sys/setspeeds.g" ; Set speed and acceleration M566 U500.00 X500.00 Y500.00 Z60.00 E300:300:300:300 P1 ;E300:300 P1 ;X1500.00 Y1500.00 Z6.00 E300 P1 ;E120.00 P1 ; set maximum instantaneous speed changes (mm/min) M203 U30000.00 X30000.00 Y30000.00 Z1000.00 E7200:7200:7200:7200 ;E7200:3600 ;E3600.00 ; set maximum speeds (mm/min) M201 U10000.00 X10000.00 Y10000.00 Z100.00 E10000:10000:10000:10000 ;E10000:3600 ;E3600.00 ; set accelerations (mm/s^2) M207 S0.6 F7200 Z0.2 ; firmware retraction orbiter 2.0 ; Axis Limits M208 X-70 U0 Y0 Z0 S1 ; set axis minima M208 X300 U380 Y306 Z300 S0 ; X310 ; set axis maxima ;M208 X-70:310 Y0:308 U0:308 Z0:300 ; Endstops M574 X1 S1 P"20.io2.in" ; configure active high endstops Toolhead 1 X low end M574 U2 S1 P"21.io2.in" ; configure active high endstops Toolhead 2 U high end M574 Y2 S1 P"io2.in" ; configure active high endstops Y. IO0 and IO1 also are UART, so do not put endstops on them, use them elsewhere to free up UART. M574 Z1 S2 M671 X-71:155:381 Y-1.5:305:-1.5 S5 ; NEW WIDEBOI WITH EXTRUSION SUPPORT LEADSCREW POSITIONS define positions of Z leadscrews or bed levelling screws ;M671 X-4.5:155:304.5 Y-4.5:305:-4.5 S5 ; OLD NON-WIDEBOI EXTRUION SUPPORT LEADSCREW POSITIONS define positions of Z leadscrews or bed levelling screws ;M557 X30:280 Y20:300 P5 ; define 5x5 mesh grid M557 X30:270 Y20:270 P5 ; Heaters M308 S0 P"temp0" Y"thermistor" T100000 B3950 A"Keenevo 600W Bed" ; configure sensor 0 as thermistor on pin temp0 M950 H0 C"out0" T0 Q10 ; Define Heater0 as the heated bed, bind to Sensor0 M140 H0 P0 ; Define Heated Bed M307 H0 R0.602 K0.401:0.000 D2.44 E1.35 S1.00 B0 ; PID Tuning for Heater0, Heated Bed (100C) M143 H0 S140 T0 A0 ; Set temperature limit for Heater0 to 120C M308 S1 P"20.temp0" Y"thermistor" T100000 B4725 C7.060000e-8 A"Slice Hotend 0" ;Slice Engineering 300C thermistor, settings are online M950 H1 C"20.out0" T1 Q100 ; Define Heater1 as Extruder0 heater, bind to Sensor1 M307 H1 R2.808 K0.368:0.000 D4.56 E1.35 S1.00 B0 V23.8 ; PID Tuning for Heater1, Extruder0 (240C) M143 H1 S325 T1 A0 ; Set temperature limit for heater 1 to 285C M308 S2 P"temp1" Y"thermistor" T100000 B3950 C7.060000e-8 A"Chamber" ; configure sensor 2 as thermistor on pin temp1 M950 H2 C"out1" T2 ;Q10 ; create chamber heater output on out1 and map it to sensor 2 M307 H2 R0.01 K0.200:0.000 D60 E1.35 S1.00 B1 ; enable bang-bang mode for the chamber heater and set PWM limit M141 H2 ; map chamber to heater 2 M143 H2 S120 T2 A0 ; set temperature limit for heater 2 to 60C M308 S3 P"21.temp0" Y"pt1000" A"Slice Hotend 1" ;Slice Engineering RTD PT1000 450C, settings are online M950 H3 C"21.out0" T3 Q100 ; Define Heater1 as Extruder0 heater, bind to Sensor1 M307 H3 R2.808 K0.368:0.000 D4.56 E1.35 S1.00 B0 V23.8 ; PID Tuning for Heater1, Extruder0 (240C) M143 H3 S425 T3 A0 ; S325 ; Set temperature limit for heater 1 to 285C M308 S4 P"20.temp1" Y"thermistor" A"Cooling Block" T100000 B3950 C7.060000e-8 ; Define Sensor as Chamber temperature M308 S5 Y"drivers" A"4028 Power" ; 4028 power using spare heater M308 S6 Y"mcu-temp" A"Mini 5+ MCU" ; Define Sensor3 as the integrated MCU temperature sensor M308 S7 Y"drivers" A"Mini 5+ TMC Drivers" ; Define Sensor4 as the TMC overheat sensor M308 S8 Y"mcu-temp" P"20.dummy" A"Toolboard0 MCU" M308 S9 Y"drivers" P"20.dummy" A"1LC0 Stepper" M308 S10 Y"mcu-temp" P"21.dummy" A"Toolboard1 MCU" M308 S11 Y"drivers" P"21.dummy" A"1LC1 Stepper" M308 S12 Y"mcu-temp" P"1.dummy" A"3HC MCU" M308 S13 Y"drivers" P"1.dummy" A"3HC TMC Drivers" M308 S14 P"temp2" Y"thermistor" T100000 B3950 C7.060000e-8 A"Orbiter Motor" ; configure sensor 9 as thermistor on pin temp2 M308 S15 P"spi.cs1" Y"thermocouple-max31856" K"K" A"TC0 Chamber Heater"; define temperature sensor number 10 as a K Type thermocouple on the first port of a temperature daughter board plugged into the expansion board with CAN bus address 3. M308 S16 P"spi.cs2" Y"thermocouple-max31856" K"K" A"TC1 Chamber Fins"; define temperature sensor number11 as a T Type thermocouple on the first port of a temperature daughter board plugged into the expansion board with CAN bus address 3. ;M308 S17 P"21.temp1" Y"thermistor" T4500000 B5315 C3.219245e-9 A"BLUE MELLOW" ; blue Mellow high temp thermistor (toolboard)https://duet3d.dozuki.com/Wiki/Connecting_thermistors_or_PT1000_temperature_sensors#Section_RepRapFirmware_3_x ;M308 S17 P"21.temp1" Y"pt1000" T500000 B4666 C1.117125e-7 A"WHITE MELLOW" ; white Mellow high temp pt1000 (toolboard)https://duet3d.dozuki.com/Wiki/Connecting_thermistors_or_PT1000_temperature_sensors#Section_RepRapFirmware_3_x ; Fans M950 H4 C"!out2" T2 Q10 ;H2 ; Define Heater2 as the 4028 fan power, bind to Sensor3 M143 H4 P2 S200 A0 ; Needed M143 to set max temp so the graph scaled correctly M950 F0 C"!20.out1+out1.tach" Q25000 ;Q500 ; create fan 0 on pin out4 and set its frequency M106 P0 C"T0 Layer Fan" L0.0 X1.0 S0 H-1 B0.1 ; set fan 0 name and value. Thermostatic control is turned off M950 F1 C"20.out2+out2.tach" Q500 ; Fan 1 uses out3, and using out3.tach as a tacho input M106 P1 C"T0 Hotend Fan" S0 H1 T45 ; For M106 the H is sensor # and NOT heater #. set fan 1 name and value. Thermostatic control turned on for Hotend M950 F2 C"out5" Q500 ; create fan 1 on pin out5 and set its frequency M106 P2 C"Mini 5+ Board Fan" S0 H5:6:7 T45 ; set fan 1 name and value. Thermostatic control turned on for Hotend M950 F3 C"!out3+out3.tach" Q25000 ; Q500 ; Chamber Heater Fan Noctua NF-F12 Industrial M106 P3 C"Chamber Heater Fan" H15 T30 ; H15 S0.3 L0.3 X0.6 B0.1 T30:40 ; set fan 1 name and value. Thermostatic control turned on for Hotend. M950 F4 C"1.out3" Q500 ; ; out6 on old mini 5+ ; create fan 4 for Water Cooling 12V Fan 4 on pin out4 and set its frequency M106 P4 C"Radiator Cooling Fan" S0 H4 T35 ; set fan 1 name and value. Thermostatic control turned on for liquid cooling hotend M950 F5 C"!out4+out4.tach" Q25000 ;Q500 ; create fan 4 for Water Cooling 12V Fan 4 on pin out4 and set its frequency M106 P5 C"Liquid Cooling Pump" L0.0 X1.0 S0.5 H4 ;S0.0 T20 ; set fan 4 name and value. Thermostatic control turned on for liquid cooling hotend M950 F6 C"!21.out1+out1.tach" Q25000 ;Q500 ; create fan 6 on pin out4 and set its frequency M106 P6 C"T1 Layer Fan" L0.0 X1.0 S0 H-1 B0.1 ; set fan 6 name and value. Thermostatic control is turned off M950 F7 C"21.out2+out2.tach" Q500 ; Fan 7 uses out3, and using out3.tach as a tacho input M106 P7 C"T1 Hotend Fan" S0 H3 T45 ; set fan 7 name and value. Thermostatic control turned on for Hotend M950 F8 C"1.out6" Q500 ; create fan 1 on pin out5 and set its frequency M106 P8 C"3HC Board Fan" S0 H12:13 T45 ; set fan 1 name and value. Thermostatic control turned on for Hotend M950 F9 C"!1.out4+out4.tach" Q25000 ;Q500 4028 filter fan ; create fan 0 on pin out4 and set its frequency M106 P9 C"Testing Chamber Fan" H-1 T30 ; Tool 0 X Axis M563 P0 D0 H1 X0 F0 S"Mosquito Mag Liquid" ; define tool 0 G10 P0 X0 Y0 Z-0.54 ; Z-0.54 S210 R175 ; set tool 0 axis offsets, set initial tool 0 active 60C and standby temperatures to 0C M568 P0 S210 R175 ; Tool 1 U Axis M563 P1 D1 H3 X3 F6 S"Mosquito Mag Air" ; define tool 0 G10 P1 U0 X0 Y0 Z0 ; S210 R175 ; L1 ; set tool 1 axis offsets, set initial tool 1 active 60C and standby temperatures to 0C M568 P1 S210 R175 ; Tool 2-- Toolhead 2 with ROME 1 M563 P2 D1:2 H3 X3 F6 S"ROME 1" ; tool 2 uses both extruders and hot end heaters, maps X to both X and U, and uses both print cooling fans G10 P2 U-2.31 X0 Y0.24 Z0.00 ; Z0.04 S210 R175 ; L1 ; set tool 0 axis offsets, set initial tool 0 active 60C and standby temperatures to 0C M567 P2 E1:1 ; set mix ratio 100% on both extruders for copy mode M568 P2 S210 R175 ; Tool 3-- Toolhead 2 with ROME 2 M563 P3 D1:3 H3 X3 F6 S"ROME 2" ; tool 2 uses both extruders and hot end heaters, maps X to both X and U, and uses both print cooling fans G10 P3 U-2.31 X0 Y0.24 Z0.00 ; Z0.04 S210 R175 ; L1 ; set tool 0 axis offsets, set initial tool 0 active 60C and standby temperatures to 0C M567 P3 E1:1 ; set mix ratio 100% on both extruders for copy mode M568 P3 S210 R175 ; Tool 4-- copy mode ;M563 P4 D0:1 H1:3 X0:3 F0:6 S"copy mode" ; tool 2 uses both extruders and hot end heaters, maps X to both X and U, and uses both print cooling fans ;G10 P4 U-77.5 X77.5 Y0 S210 R175 ; set tool offsets and temperatures for tool 2 ;M567 P4 E1:1 ; set mix ratio 100% on both extruders for copy mode ; Tool 5-- mirror mode ;M563 P5 D0:1 H1:3 X0:3 F0:6 S"mirror mode" ; tool for mirror mode ;G10 P5 U-77.5 X77.5 Y0 S210 R175 ; tool offset for mirror mode (flipped X offset) ;M567 P5 E1:1 ; set mix ratio 100% on both extruders for mirror mode ; Z-Probe Euclid Probe ;M558 P5 C"20.io0.in" H5 F400 T5000 ; set Z probe type to unmodulated and the dive height + speeds M558 P8 C"^20.io0.in" H8 F400 T9000 A1 ; S0.01 ; set Z probe type to unmodulated and the dive height + speeds G31 P1000 X-28 Y-20 Z9.71 ; Z9.21 ; K0 ; set Z probe trigger value, offset and trigger height, more Z means closer to the bed ;; BLTouch ; M950 S0 C"io7.out" ; Create a servo pin on io7 ; M558 P9 C"io7.in" H5 F240 T10800 A5 ; set Z probe type to unmodulated and the dive height + speeds ; G31 P25 X-28.00 Y-13.00 Z0.78 ; set Z probe trigger value, offset and trigger height, more Z means closer to the bed ;Accelerometer M955 P20.0 I14 ;Input Shaper M593 P"zvdd" F31 ; for 10k acceleration ;M593 P"mzv" F42.5 ; for 15k acceleration ;Filament Sensor0 ;M591 D0 P3 C"20.io1.in" S1 ;M591 D0 L27 R10:190 ;ROME Filament Sensor0 ;M591 D2 P1 C"21.io0.in" S1 ;M591 D2 L27 R10:190 ;M574 U2 S1 P"21.io0.in" ; configure active high endstops Toolhead 2 ROME toolhead filament sensor ;M577 wait until endstop is triggered. Does equivalent exist for a general IO sensor? M950 J0 C"^!21.io0.in" ;PanelDue 5i M575 P1 S1 B57600 ;NeoPixels x3 M150 X3 Q4000000 ;R128 U128 B128 P128 S2 F0 M150 X3 R255 U255 B255 W255 P255 S2 F0 ; display led ; Custom settings G29 S1 M572 D0:1:2:3 S0.045 ; set Pressure Advance K-factor M501 M376 H3 ;M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss global daemonLoop = true ; init filament sensor error global variables if !exists(global.filamentTimestamp) global filamentCounter = 0 global filamentTimestamp = state.Uptime ; init print time logging if !exists(global.runtime) M98 P"runtime.g" ; init LED variables if !exists(global.warmUp) global warmUp = false ; Select default tool M404 N1.75 ; Define filament diameter for print monitor T0
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@RogerPodacter thanks. Can you confirm that you have no daemon.g file in /sys on the SD card?
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@dc42 said in Reboots/resets randomly - RRF 3.5.0-beta4:
@Exerqtor in reply to your question in the firmware announcement thread, you are already running wifi firmware 2.1beta4 according to your M122 reports - but please check that you haven't inadvertently downgraded to 2.1beta3.
Yup, no problem I know intermittent issues can suck to track down
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@dc42 ah yes, here is my daemon.g.
daemon.g
while global.daemonLoop ;----------------------------------------------------------------------------- ;Heater Checks and Safety ;----------------------------------------------------------------------------- ;check if Chamber heater fans are running ; if fans[3].rpm < 100 ; M141 H2 S-273.1 ; disable chamber heater ;----------------------------------------------------------------------------- ;Keeps a lifetime running print time variable for the printer ;----------------------------------------------------------------------------- ;if global.warmUp = true ; echo "setLEDbyTemp = true" ; M98 P"0:/macros/set_LED_while_heating.gcode" if state.status == "processing" if exists(global.runtime) set global.runtime = {global.runtime + 10} echo >"runtime.g" "global runtime = " ^ {global.runtime} ^ " ; seconds AUTO GENERATED by daemon.g" ;echo >"runtime.g" "minutes = "^{global.runtime}/60 ;echo >"runtime.g" "hours = "^{global.runtime}/60/60 ;echo >"runtime.g" "days = "^{global.runtime}/60/60/24 ;----------------------------------------------------------------------------- ;LED Controls ;----------------------------------------------------------------------------- if {state.status} == "paused" M150 R255 B255 P255 S2 ; purple M300 S4000 P50 G4 P300 M300 S4000 P50 ; double beep elif {state.status} == "processing" || {state.status} == "busy" M150 R255 U255 B255 W255 P255 S2 ; white elif {heat.heaters[0].current} > 50 || {heat.heaters[1].current} > 70 M150 R255 U0 B0 W0 P255 S2 ; red elif {state.status} == "idle" M150 R0 U255 B0 W0 P255 S2 ; green else M150 R150 U0 B150 W0 P255 S2 ; purple G4 S10 ;there is a delay of 10 seconds between consecutive executions of daemon.g. This is to avoid SD ; card access contention between daemon.g and a file being printed. If you need a smaller delay, put ; all that code inside a while-loop, and include a shorter delay (e.g. G4 S1) at the end of the loop. ;ADD SOMETHING LIKE THIS FOR HEATER SAFETY. USE REALLY USEFUL EXAMPLE GCODE DAEMON.G FILES. ;if fans[1].rpm < 100 && heat[1].heaters > 50 ; abort "No fan motion detected, stopping all macros, jobs, and disabling heaters" ; M140 P-273.1 ; disable bed heater ; M568 P0 A0; set tool 0 to off ;############ from dc42 ;while true ;while iterations<10 ; ; while iterations < #sensors.analog ; var red = sensors.analog[iterations].lastReading ; var green = 255 - var.red ; var blue = var.green ; M150 R{var.red} U{var.green} B{var.blue} S2 F{min(#sensors.analog-iterations-1,1)} ; ; G4 S3 ; ;############# ; ; daemeon.g ; ; Adafruit #1426 8 led neopixel ; ; M150 X1 ; ; if heat.heaters[1].current > 50 ; temp ; M150 R0 U255 B0 P255 S2 F1 ;M150 R{var.redValue} U{var.greenValue} B{var.blueValue} P{var.setBrightness} S{var.pixelsPerTool} F{var.F} ; ; elif heat.heaters[1].current <= 50 ; M150 R0 U0 B255 P255 S2 F1
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@RogerPodacter thanks.
- Please also provide your homing files, since you said the machine resets during homing.
- Although this doesn't explain the reset, I can see a problem in your config.g file. Your M669 command to set the kinematics at line 7 refers to the U axis, however the U axis doesn't exist until it is created in the M584 command at line 35. You should move the M669 command to be after the M584 command.
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@dc42
Just as a little update, i have as of today not had any more resets. I'm trying to turn out some small parts, just to see if anything can trigger a reset, but so far no luck =/ -
@Exerqtor thanks for the update. I have not yet had a reset either using your files or the file from @RogerPodacter (although I am still waiting for his homing files, and he reported that the reset occurred when homing).
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@dc42 apologies for the delay. here are my homing files. my printer kinematics didnt work correctly, so i dont know if that was related while i was attempting the homings...
homeall.g
if (move.axes[0].homed && move.axes[1].homed && move.axes[2].homed && move.axes[3].homed) echo "already homed, skipping" else ;T0 G91 ; Relative positioning G1 Z15 F6000 H2 ; Lift Z relative to current position G1 Y999 F3000 H1 ; Move X and Y-axes to the endstops and stop (first pass) G1 Y-4 F600 ; Move Y-axis to the endstop and stop (first pass) G1 Y15 F600 H1 ; Move X-axis to the endstop once more (second pass) G1 X-999 F3000 H1 ; coarse home X, Y and U G1 X4 F600 ; move 4mm away from the homing switches G1 X-15 H1 ; fine home X, Y and U G1 U999 F3000 H1 ; coarse home X, Y and U G1 U-4 F600 ; move 4mm away from the homing switches G1 U15 H1 ; fine home X, Y and U G90 ; Absolute positioning M401 ; deploy Z probe (omit if using bltouch) ; Home Z using the Z-Probe M290 R0 S0 ; Reset baby-stepping to 0 G1 X183 Y170 F6000 ; Move T0 to probing point (X150, Y150), including probe offset G30 ; Probe the bed and set Z to the probe offset M402 ; retract probe (omit if using bltouch)
homex.g
M201 X500.00 U500.00 ; Reduce acceleration for homing moves G91 ; Relative positioning G1 H2 Z5 F6000 ; Lift Z relative to current position G1 H1 X-625 F3000 ; Move quickly to X endstop and stop there (first pass) G1 X3 F600 ; Go back a few mm G1 H1 X-625 F360 ; Move slowly to X endstop once more (second pass) ;G1 H1 U625 F1800 ;G1 U-3 F600 ;G1 H1 U625 F360 M201 X3000 U6000 ; Return to full acceleration G1 H2 Z-5 F6000 ; Lower Z relative to current position G90 ; Absolute positioning
homey.g
M201 X500.00 Y500.00 ; Reduce acceleration for homing moves G91 ; Relative positioning G1 H2 Z5 F6000 ; Lift Z relative to current position G1 H1 Y605 F3000 ; Move quickly to Y endstop and stop there (first pass) G1 Y-3 F600 ; Go back a few mm G1 H1 Y605 F360 ; Move slowly to Y endstop once more (second pass) M201 X3000 Y6000 ; Return to full acceleration G1 H2 Z-5 F6000 ; Lower Z relative to current position G90 ; Absolute positioning
homez.g
; *********************************************************** ; Euclid Probe homez.g Example Macro ; RRF3.X Firmware Example ; saveas system/homez.g ; comments and echo statements throughout are provided for convenience ; *********************************************************** if !move.axes[0].homed || !move.axes[1].homed ; If the printer hasn't been homed, home it M98 P"0:/sys/homexy.g" M561 ; clear any bed transform M290 S0 R0 ; clear baby steps G91 ; relative positioning G1 H2 Z15 F6000 ; lift Z relative to current position to clear any obstructions M400 G1 U380 F2000 ; make sure the U carriage is out of the way G90 ; absolute positioning ; echo "Call deployprobe.g macro" M401 P0 ; This runs macro file deployprobe ; echo "Return" G1 X155 Y155 F9000 ; go to center of bed in advance of probe that point M400 ; echo "G30 Command" G30 ; Probe the bed at the current XY position. When the probe is triggered, ; adjust the Z offset of the current tool to make the current position Z=0. ;G1 Z10 ; raise Z=10 ;M400 ;G4 P500 ; echo "Call bed4point.g macro" ;M98 P"0:/sys/bed.g" ; tram bed ; echo "Return" ;G1 X145 Y162.5 F9000 ; go back to the first probe point and reprobe 0 in case it moved ;G30 ; echo "Call retractprobe.g macro" M402 P0 ; retract probe echo "Return" ;G1 Z10 F600 ; lift Z relative to current position G90 ; absolute positioning M564 S1 H0 ; reset the bounding limits ; G1 X150 Y0 F9000 ; move carriage to center front
homeu.g
M201 U500.00 Y500.00 ; Reduce acceleration for homing moves G91 ; Relative positioning G1 H2 Z5 F6000 ; Lift Z relative to current position G1 H1 U625 F3000 ; Move quickly to X endstop and stop there (first pass) G1 U-3 F600 ; Go back a few mm G1 H1 U625 F360 ; Move slowly to X endstop once more (second pass) M201 U3000 Y6000 ; Return to full acceleration G1 H2 Z-5 F6000 ; Lower Z relative to current position G90 ; Absolute positioning
bed.g
M290 R0 S0 ; clear baby stepping M561 ; reset all bed adjustments M400 ; flush move queue ; echo "Running bed4point.g" ;M558 F60 A6 ;A3 ; fix probe speed to 1mm/s ;G90 ;G4 P250 if !move.axes[0].homed || !move.axes[1].homed || !move.axes[2].homed echo "not all axes homed, homing axes first" G28 G1 U380 F2000 ; make sure the U carriage is out of the way M401 ; deploy Z probe (omit if using bltouch) G30 P0 X46 Y20 Z-99999 ; X41 X30 Y20 Z-99999 ; probe near a leadscrew G30 P1 X155 Y276 Z-99999 ;Y282 Z-99999 ; probe near a leadscrew G30 P2 X270 Y20 Z-99999 S3 ; probe near a leadscrew and calibrate 3 motors echo "Current rough pass deviation: " ^ move.calibration.initial.deviation while move.calibration.initial.deviation > 0.005 if iterations >= 5 echo "Error: Max attemps failed. Deviation: " ^ move.calibration.initial.deviation break echo "Deviation over threshold. Executing pass" , iterations+1, "deviation", move.calibration.initial.deviation G30 P0 X46 Y20 Z-99999 ; probe near a leadscrew G30 P1 X155 Y276 Z-99999 ; probe near a leadscrew G30 P2 X270 Y20 Z-99999 S3 ; probe near a leadscrew and calibrate 3 motors echo "Current deviation: " ^ move.calibration.initial.deviation continue echo "Final deviation: " ^ move.calibration.initial.deviation G0 X155 Y155 Z20 F9000 G30 ;G28 Z M402 ; retract probe (omit if using bltouch)
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@dc42
After a couple days without any resets, it happend again twice yesterday:power up + 00:00:03 [info] Event logging started at level debug power up + 00:00:03 [info] Running: Duet 3 Mini5plus WiFi: 3.5.0-beta.4 (2023-06-08 23:40:14) power up + 00:00:03 [debug] Done! power up + 00:00:03 [debug] RepRapFirmware for Duet 3 Mini 5+ is up and running. power up + 00:00:04 [warn] WiFi module started power up + 00:00:07 [warn] WiFi module is connected to access point RV32-IOT2G, IP address 192.168.10.50 power up + 00:00:09 [warn] HTTP client 192.168.10.100 login succeeded (session key 1366409378) 2023-06-16 01:23:20 [warn] Date and time set at power up + 00:00:09 power up + 00:00:03 [info] Event logging started at level debug power up + 00:00:03 [info] Running: Duet 3 Mini5plus WiFi: 3.5.0-beta.4 (2023-06-08 23:40:14) power up + 00:00:03 [debug] Done! power up + 00:00:03 [debug] RepRapFirmware for Duet 3 Mini 5+ is up and running. power up + 00:00:04 [warn] WiFi module started power up + 00:00:07 [warn] WiFi module is connected to access point RV32-IOT2G, IP address 192.168.10.50 power up + 00:00:08 [warn] HTTP client 192.168.10.100 login succeeded (session key 125510966) 2023-06-16 10:24:14 [warn] Date and time set at power up + 00:00:08
m122 === Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.5.0-beta.4 (2023-06-08 23:40:14) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: FAP55-Q967A-G65J0-401GL-0S02Z-RF9TL Used output buffers: 1 of 40 (30 max) === RTOS === Static ram: 102996 Dynamic ram: 124208 of which 16 recycled Never used RAM 11980, free system stack 180 words Tasks: NETWORK(2,nWait,126.9%,219) HEAT(3,nWait,0.5%,327) Move(4,nWait,0.1%,344) CanReceiv(6,nWait,1.1%,672) CanSender(5,nWait,0.0%,337) CanClock(7,delaying,0.2%,351) TMC(4,delaying,26.0%,108) MAIN(1,running,48.1%,704) IDLE(0,ready,8.9%,29) AIN(4,delaying,18.0%,266), total 229.7% Owned mutexes: === Platform === Last reset 26:40:40 ago, cause: software Last software reset at 2023-06-16 10:24, reason: HardFault invState, Gcodes spinning, available RAM 10580, slot 1 Software reset code 0x4063 HFSR 0x40000000 CFSR 0x00020000 ICSR 0x00000803 BFAR 0xe000ed38 SP 0x20011fa8 Task NETW Freestk 482 ok Stack: 000001ae 00000002 200014ec 00000000 2003335a 0009d43d 00000000 600f0000 00000000 00000000 00000000 00000000 20032174 00000800 20035e68 2002c558 20018670 2002c3f5 20018670 2001e920 0002fe6f 00000000 00000000 00000000 20012058 00000014 b5ddc1d1 Error status: 0x00 Aux0 errors 0,0,0 MCU revision 3, ADC conversions started 96040137, completed 96040137, timed out 0, errs 0 MCU temperature: min 35.1, current 36.3, max 39.4 Supply voltage: min 23.7, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 99/28, heap memory allocated/used/recyclable 2048/980/596, gc cycles 3588 Events: 0 queued, 0 completed Driver 0: standstill, SG min 2, read errors 0, write errors 1, ifcnt 33, reads 14596, writes 13, timeouts 0, DMA errors 0, CC errors 0 Driver 1: standstill, SG min 0, read errors 0, write errors 1, ifcnt 33, reads 14596, writes 13, timeouts 0, DMA errors 0, CC errors 0 Driver 2: standstill, SG min 2, read errors 0, write errors 1, ifcnt 147, reads 14596, writes 13, timeouts 0, DMA errors 0, CC errors 0 Driver 3: standstill, SG min 0, read errors 0, write errors 1, ifcnt 147, reads 14595, writes 13, timeouts 1, DMA errors 0, CC errors 0, failedOp 0x6c Driver 4: standstill, SG min 0, read errors 0, write errors 1, ifcnt 150, reads 14595, writes 13, timeouts 1, DMA errors 0, CC errors 0, failedOp 0x6a Driver 5: standstill, SG min 0, read errors 0, write errors 1, ifcnt 43, reads 14597, writes 10, timeouts 2, DMA errors 0, CC errors 0, failedOp 0x6a Driver 6: standstill, SG min 0, read errors 0, write errors 1, ifcnt 43, reads 14599, writes 10, timeouts 0, DMA errors 0, CC errors 0 Date/time: 2023-06-17 13:04:45 Cache data hit count 4294967295 Slowest loop: 22.78ms; fastest: 0.14ms === Storage === Free file entries: 18 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 4.5ms, write time 4.2ms, max retries 0 === Move === DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, height map offset 0.000, ebfmin 0.00, ebfmax 0.00 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 1 is on, I-accum = 0.0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 S1 " in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000803 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === CAN === Messages queued 864369, received 1920872, lost 0, boc 0 Longest wait 3ms for reply type 6053, peak Tx sync delay 277, free buffers 18 (min 17), ts 480201/480200/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 22.24ms; fastest: 0.00ms Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) HTTP sessions: 1 of 8 = WiFi = Interface state: active Module is connected to access point Failed messages: pending 0, notready 0, noresp 0 Firmware version 2.1beta4 MAC address bc:ff:4d:e6:b1:62 Module reset reason: Power up, Vcc 3.38, flash size 2097152, free heap 42972 WiFi IP address 192.168.10.50 Signal strength -50dBm, channel 1, mode 802.11n, reconnections 0 Clock register 00002001 Socket states: 0 0 0 0 0 0 0 0
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@Exerqtor that's interesting, it's not the same crash as before but it is the same task (NETW) and probably the same area of code.
If your machine is not being used, please can you do a couple of things to increase the load on it, in the hope that this will make the problem occur more frequently. In particular, try these:
- In the DWC Machine Specific config, reduce the polling interval e.g. to 100ms
- Reduce the lengths of G4 delay commands that you have in daemon.g.
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@dc42
Guess that's somewhat positive and it would help narrow down the search a little? wishfull thinkingOk I've set the "Communication update invervals" to 100ms now (if that's the one you were refering to).
What do you suggest changing the daemon.g delay to? It's currently 1second, so reduce it to 300ms or something maybe? -
@Exerqtor I suggest you try 100ms. If that makes the response to console commands such as M122 excessively slow, increase it.
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@dc42
Ok, then both have been set to 100ms. Now it's just to wait for a crash i guess -
@dc42
Don't look like the added stress we were able to muster up with those changes did much, only had one crash since they were changed:power up + 00:00:03 [info] Event logging started at level debug power up + 00:00:03 [info] Running: Duet 3 Mini5plus WiFi: 3.5.0-beta.4 (2023-06-08 23:40:14) power up + 00:00:03 [debug] Done! power up + 00:00:03 [debug] RepRapFirmware for Duet 3 Mini 5+ is up and running. power up + 00:00:04 [warn] WiFi module started power up + 00:00:07 [warn] WiFi module is connected to access point RV32-IOT2G, IP address 192.168.10.50 power up + 00:00:08 [warn] HTTP client 192.168.10.100 login succeeded (session key 775616360) 2023-06-18 04:59:53 [warn] Date and time set at power up + 00:00:08
M122 === Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.5.0-beta.4 (2023-06-08 23:40:14) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: FAP55-Q967A-G65J0-401GL-0S02Z-RF9TL Used output buffers: 1 of 40 (38 max) === RTOS === Static ram: 102996 Dynamic ram: 125612 of which 12 recycled Never used RAM 10580, free system stack 180 words Tasks: NETWORK(1,ready,84.6%,219) HEAT(3,nWait,0.1%,327) Move(4,nWait,0.0%,344) CanReceiv(6,nWait,0.2%,672) CanSender(5,nWait,0.0%,337) CanClock(7,delaying,0.0%,351) TMC(4,nWait,4.9%,108) MAIN(1,running,150.3%,704) IDLE(0,ready,13.1%,29) AIN(4,delaying,3.4%,266), total 256.8% Owned mutexes: === Platform === Last reset 04:11:46 ago, cause: software Last software reset at 2023-06-18 04:59, reason: HardFault invState, Gcodes spinning, available RAM 9444, slot 2 Software reset code 0x4063 HFSR 0x40000000 CFSR 0x00020000 ICSR 0x00000803 BFAR 0xe000ed38 SP 0x20011fa8 Task NETW Freestk 482 ok Stack: 000001af 00000002 200014ec 00000000 2003335b 0009d43d 00000000 600f0000 00000000 00000000 00000000 00000000 2003217c 00000800 20035e70 2002c558 20018670 2002c3f5 20018670 2001e920 0002fe6f 00000000 00000000 00000000 20012058 00000014 ffffffff Error status: 0x00 Aux0 errors 0,0,0 MCU revision 3, ADC conversions started 15106363, completed 15106363, timed out 0, errs 0 MCU temperature: min 35.1, current 35.5, max 41.8 Supply voltage: min 23.7, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 99/32, heap memory allocated/used/recyclable 2048/1372/948, gc cycles 4666 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, read errors 0, write errors 1, ifcnt 63, reads 62550, writes 13, timeouts 0, DMA errors 0, CC errors 0 Driver 1: standstill, SG min 2, read errors 0, write errors 1, ifcnt 63, reads 62549, writes 13, timeouts 0, DMA errors 0, CC errors 0 Driver 2: standstill, SG min 2, read errors 0, write errors 1, ifcnt 166, reads 62549, writes 13, timeouts 0, DMA errors 0, CC errors 0 Driver 3: standstill, SG min 0, read errors 0, write errors 1, ifcnt 165, reads 62549, writes 13, timeouts 0, DMA errors 0, CC errors 0 Driver 4: standstill, SG min 0, read errors 0, write errors 1, ifcnt 168, reads 62550, writes 13, timeouts 0, DMA errors 0, CC errors 0 Driver 5: standstill, SG min 0, read errors 0, write errors 1, ifcnt 54, reads 62553, writes 10, timeouts 0, DMA errors 0, CC errors 0 Driver 6: standstill, SG min 0, read errors 0, write errors 1, ifcnt 54, reads 62552, writes 10, timeouts 0, DMA errors 0, CC errors 0 Date/time: 2023-06-18 09:11:30 Cache data hit count 4294967295 Slowest loop: 37.72ms; fastest: 0.14ms === Storage === Free file entries: 18 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 7.0ms, write time 5.6ms, max retries 0 === Move === DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, height map offset 0.000, ebfmin 0.00, ebfmax 0.00 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 1 is on, I-accum = 0.0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 P100 " in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000803 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === CAN === Messages queued 135965, received 302172, lost 0, boc 0 Longest wait 3ms for reply type 6053, peak Tx sync delay 306, free buffers 18 (min 17), ts 75532/75531/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 22.11ms; fastest: 0.00ms Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) HTTP sessions: 1 of 8 = WiFi = Interface state: active Module is connected to access point Failed messages: pending 0, notready 0, noresp 0 Firmware version 2.1beta4 MAC address bc:ff:4d:e6:b1:62 Module reset reason: Power up, Vcc 3.38, flash size 2097152, free heap 42960 WiFi IP address 192.168.10.50 Signal strength -55dBm, channel 1, mode 802.11n, reconnections 0 Clock register 00002001 Socket states: 0 0 0 0 0 0 0 0
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@dc42 Have you had any more time or luck with this David?
Mine havent had any news crashes sunday, and been sitting idle since then since it quite frankly ain't stable enough to be used for any duration of time
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@Exerqtor unfortunately I haven't been able to reproduce it.
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@dc42
Haven't had any more crashes here either, though the printer has just been sitting idle since last time it happened. -
@Exerqtor I'm wondering whether it could possibly be a hardware issue, because I haven't been able to reproduce it and nobody else has reported it. Which country are you in and which Duet3D reseller do you use?
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@dc42
Might be the case, this perticular board ain't a original duet3 board but a Fysetc "Big Dipper" (killed the processor on my Duet 2 so I needed a subsitute board ASAP, and couldn't justify cashing out for a original duet 3 mini & addon board to the mrs🤦♂️
).It haven't had a single crash since the last one i reportet two weeks ago though. Even with the extra load we added.
Just started a 2.3hr print on it now to see if it wil act up again.