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    home z bug fix

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    • Adamrobotundefined
      Adamrobot
      last edited by

      Hello everyone,

      I'm a complete beginner with Duet 3D, and I'm using the Duet2 WiFi version. After assembling everything, it all seemed to work well. However, I'm encountering an issue when homing the Z-axis. The print bed of the 3D printer moves down three times and then stops at a new position. If I run the home Z command multiple times, the print bed continues to lower until it starts making a noise, yet there are no error messages throughout this process.

      I really need help with this issue, so any advice or guidance would be greatly appreciated. If more information is needed to help diagnose the problem, please let me know and I'll provide it as soon as possible. Thank you all in advance!

      The home Z code:
      ; homez.g
      ; called to home the Z axis

      T-1 ;just in case there is a tool coupled, go try to drop it at the dock

      M98 P/macros/Coupler - Unlock ;Open Coupler

      G91 ; Relative mode
      G1 H2 Z5 F5000 ; Lower the bed
      G90 ; back to absolute positioning

      G1 X150 Y100 F50000 ; Position the endstop above the bed centre
      G4 P500
      G91 ; Relative mode

      G4 P500 ; wait 500msec
      G1 Z-300 H1 F1000 ; Move Z down until the switch triggers (first pass)

      G4 P500 ; wait 500msec
      G1 Z5 F5000 ; Lift Z

      G4 P500 ; wait 500msec
      G1 Z-300 H1 F300 ; Move Z down until the switch triggers (second pass)

      G4 P500 ; wait 500msec
      G1 Z5 F5000 ; Drop the Bed

      G90 ; Back to absolute positioning

      jay_s_ukundefined 1 Reply Last reply Reply Quote 0
      • jay_s_ukundefined
        jay_s_uk @Adamrobot
        last edited by

        @Adamrobot have you tested whether the endstop is actually working using M119?
        what type of printer is it? if its a toolchanger like the E3D one, the switch on the print head is usually treated as a probe and you should be using G30 rather than G1 H1

        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

        Adamrobotundefined 1 Reply Last reply Reply Quote 0
        • Adamrobotundefined
          Adamrobot @jay_s_uk
          last edited by

          @jay_s_uk
          hi jay its the output after using M119

          M119
          Endstops - X: not stopped, Y: not stopped, Z: at min stop, 😄 no endstop, Z probe: at min stop

          and yes its toolchanger, there is a sensor at the bottom of printhead

          jay_s_ukundefined droftartsundefined 2 Replies Last reply Reply Quote 0
          • jay_s_ukundefined
            jay_s_uk @Adamrobot
            last edited by

            @Adamrobot so from the looks of it you should probably be using G30.
            Can you post your config?

            Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

            Adamrobotundefined 1 Reply Last reply Reply Quote 0
            • Adamrobotundefined
              Adamrobot @jay_s_uk
              last edited by

              @jay_s_uk hi jay here's the config

              ; Configurat; Configuration file for Duet WiFi / Ethernet
              ; executed by the firmware on start-up

              ; General preferences
              M111 S0 ; Debugging off
              G21 ; Work in millimetres
              G90 ; Send absolute coordinates...
              M83 ; ...but relative extruder moves
              M555 P2 ; Set firmware compatibility to look like Marlin

              ; Network
              ; Read https://duet3d.dozuki.com/Wiki/Gcode#Section_M587_Add_WiFi_host_network_to_remembered_list_or_list_remembered_networks
              M550 P"ToolChanger" ; Set machine name
              M552 S1 ; Enable Networking
              M586 P0 S1 ; Enable HTTP
              M586 P1 S0 ; Disable FTP
              M586 P2 S0 ; Disable Telnet

              M667 S1 ; Select CoreXY mode

              ; Endstops
              M574 X1 Y1 S3 ; Set X / Y endstop stall detection
              M574 Z1 S2 ; Set Z endstop probe
              M558 P7 X0 Y0 Z2 H3 F360 I0 T20000 ; Set Z probe type to switch, the axes for which it is used and the dive height + speeds
              G31 P200 X0 Y0 Z0 ; Set Z probe trigger value, offset and trigger height
              M557 X10:290 Y20:180 S40 ; Define mesh grid

              ; Drive direction
              M569 P0 S0 ; Drive 0 X
              M569 P1 S0 ; Drive 1 Y
              M569 P2 S1 ; Drive 2 Z
              M569 P3 S0 ; Drive 3 E0
              M569 P4 S0 ; Drive 4 E1
              M569 P5 S1 ; Drive 5 E2
              M569 P6 S1 ; Drive 6 E3
              M569 P7 S0 ; Drive 7 COUPLER
              M569 P8 S0 ; Drive 8 UNUSED
              M569 P9 S0 ; Drive 9 UNUSED

              M584 X0 Y1 Z2 C7 E3:4:5:6 ; Apply custom drive mapping
              M208 X-35:328.5 Y-49:243 Z0:300 C0:260 S0 ; Set axis maxima & minima
              M350 C8 I0 ; Configure microstepping without interpolation
              M350 X16 Y16 Z16 E16:16:16:16 I1 ; Configure microstepping with interpolation
              M92 X100 Y100 Z1600 C100 E834:834:834:834 ; Set steps per mm
              M566 X400 Y400 Z8 C2 E2:2:2:2 ; Set maximum instantaneous speed changes (mm/min)
              M203 X35000 Y35000 Z1200 C5000 E5000:5000:5000:5000 ; Set maximum speeds (mm/min)
              M201 X6000 Y6000 Z400 C400 E2500:2500:2500:2500 ; Set accelerations (mm/s^2)
              M906 X1800 Y1800 Z1330 C400 I30 ; Idle motion motors to 30%
              M906 E1000:1000:1000:1000 I10 ; Idle extruder motors to 10%

              ;Stall Detection
              M915 C S5 F0 H200 ; Coupler

              ;Stall Detection
              M915 X Y S5 F0 H400 ; X / Y Axes

              ; Heaters
              M305 P0 T100000 B4725 C7.06e-8 ; Set thermistor
              M143 H0 S225 ; Set temperature limit for heater 0 to 225C

              M305 S"T0" P1 T100000 B4725 C7.06e-8 ; Set thermistor
              M143 H1 S300 ; Set temperature limit for heater 1 to 300C

              M305 S"T1" P2 T100000 B4725 C7.06e-8 ; Set thermistor
              M143 H2 S300 ; Set temperature limit for heater 2 to 300C

              M305 S"T2" P3 T100000 B4725 C7.06e-8 ;Set thermistor
              M143 H3 S300 ; Set temperature limit for heater 3 to 300C

              M305 S"T3" P4 T100000 B4725 C7.06e-8 ; Set thermistor
              M143 H4 S300 ; Set temperature limit for heater 4 to 300C

              ; Tools
              M563 P0 S"T0" D0 H1 F2 ; Define tool 0
              G10 P0 X0 Y0 Z0 ; Reset tool 0 axis offsets
              G10 P0 R0 S0 ; Reset initial tool 0 active and standby temperatures to 0C

              M563 P1 S"T1" D1 H2 F4 ; Define tool 1
              G10 P1 X0 Y0 Z0 ; Reset tool 1 axis offsets
              G10 P1 R0 S0 ; Reset initial tool 1 active and standby temperatures to 0C

              M563 P2 S"T2" D2 H3 F6 ; Define tool 2
              G10 P2 X0 Y0 Z0 ; Reset tool 2 axis offsets
              G10 P2 R0 S0 ; Reset initial tool 2 active and standby temperatures to 0C

              M563 P3 S"T3" D3 H4 F8 ; Define tool 3
              G10 P3 X0 Y0 Z0 ; Reset tool 3 axis offsets
              G10 P3 R0 S0 ; Reset initial tool 3 active and standby temperatures to 0C

              ; Fans
              M106 P0 S0 ; UNUSED
              M106 P1 S255 H1 T70 ; T0 HE
              M106 P2 S0 ; T0 PCF
              M106 P3 S255 H2 T70 ; T1 HE
              M106 P4 S0 ; T1 PCF
              M106 P5 S255 H3 T70 ; T2 HE
              M106 P6 S0 ; T2 PCF
              M106 P7 S255 H4 T70 ; T3 HE
              M106 P8 S0 ; T3 PCF

              M593 F50 ; cancel ringing at 50Hz (https://forum.e3d-online.com/threads/accelerometer-and-resonance-measurements-of-the-motion-system.3445/)
              ;M376 H15 ; bed compensation taper

              ;tool offsets
              ; !ESTIMATED! offsets for:
              ; V6-tool: X-9 Y39 Z-5
              ; Volcano-tool: X-9 Y39 Z-13.5
              ; Hemera-tool: X20 Y43.5 Z-6

              G10 P0 X-9 Y39 Z-5 ; T0
              G10 P1 X-9 Y39 Z-5 ; T1
              G10 P2 X-9 Y39 Z-5 ; T2
              G10 P3 X-9 Y39 Z-5 ; T3

              ;deselect tools
              T-1

              ;M572 D0 S0.2 ; pressure advance T0
              ;M572 D1 S0.2 ; pressure advance T1
              ;M572 D2 S0.2 ; pressure advance T2
              ;M572 D3 S0.2 ; pressure advance T3

              M501; load config-override.g

              jay_s_ukundefined 1 Reply Last reply Reply Quote 0
              • jay_s_ukundefined
                jay_s_uk @Adamrobot
                last edited by

                @Adamrobot so yes, your switch on your printhead it setup as a probe so you should be using G30.
                I would also suggest you look into upgrading from RRF2 to RRF3

                Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                1 Reply Last reply Reply Quote 0
                • droftartsundefined
                  droftarts administrators @Adamrobot
                  last edited by

                  @Adamrobot said in home z bug fix:

                  When you did the M119 and got this back:
                  Z: at min stop, C: no endstop, Z probe: at min stop

                  Was the endstop/probe touching the bed, or were you triggering it? If not, then you need to invert this in M558 in config.g, ie change I0 to I1:

                  M558 P7 X0 Y0 Z2 H3 F360 I1 T20000 ; Set Z probe type to switch, the axes for which it is used and the dive height + speeds
                  

                  Ian

                  Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                  Adamrobotundefined 1 Reply Last reply Reply Quote 0
                  • Adamrobotundefined
                    Adamrobot @droftarts
                    last edited by Adamrobot

                    @droftarts @jay_s_uk
                    Hello jay and mr administrator,

                    After implementing your suggestions, part of the home Z function succeeded. However, I need to manually move the printhead above the Print bed position before I run home Z. When I use the home Z command directly after homeX and Y, although the dashboard shows the Printhead's position as 150 and 100, it is actually still in the bottom left corner. In this position, the print bed cannot reach the probe Z sensor.

                    now im using RRF3

                    the home Z code:

                    ; homez.g
                    ; called to home the Z axis
                    
                    M98 P"/macros/Coupler - Unlock"	; Open Coupler
                    
                    G91 							; Relative mode
                    G1 H2 Z5 F5000					; Lower the bed
                    G90								; back to absolute positioning
                    
                    G1 X150 Y100 F50000				; Position the endstop above the bed centre
                    
                    M558 F1000
                    G30
                    M558 F300
                    G30
                    
                    
                    jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                    • jay_s_ukundefined
                      jay_s_uk @Adamrobot
                      last edited by

                      @Adamrobot maybe F50000 is just too fast. Try something slower. Maybe take a 0 off

                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                      Adamrobotundefined 1 Reply Last reply Reply Quote 0
                      • Adamrobotundefined
                        Adamrobot @jay_s_uk
                        last edited by Adamrobot

                        @jay_s_uk @droftarts
                        Great it works!

                        and a followed question: When I attempt to heat the nozzle, it shows that the M568 command is no longer needed. I referred to other posts on forums, and they suggest the issue might be a mismatch but I believe I have installed the latest firmware version for the Duet 2 WiFi/Ethernet. Could there be another reason for this issue? or anywhere wrong?

                        M122
                        === Diagnostics ===
                        RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2.2 running on Duet WiFi 1.02 or later + DueX5
                        Board ID: 0JD0M-9X6JA-JUNSN-6JTD2-3SD6T-KBRRV
                        Used output buffers: 3 of 24 (24 max)
                        === RTOS ===
                        Static ram: 23460
                        Dynamic ram: 76280 of which 60 recycled
                        Never used RAM 12280, free system stack 115 words
                        Tasks: NETWORK(ready,169) HEAT(blocked,308) DUEX(blocked,31) MAIN(running,449) IDLE(ready,20)
                        Owned mutexes: WiFi(NETWORK)
                        === Platform ===
                        Last reset 00:07:44 ago, cause: power up
                        Last software reset at 2024-01-16 13:48, reason: User, GCodes spinning, available RAM 12280, slot 0
                        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                        Error status: 0x00
                        Aux0 errors 0,0,0
                        MCU temperature: min 29.7, current 37.5, max 37.5
                        Supply voltage: min 11.9, current 12.0, max 12.3, under voltage events: 0, over voltage events: 0, power good: yes
                        Driver 0: position 13750, standstill, SG min/max 0/1023
                        Driver 1: position -16250, standstill, SG min/max 0/1023
                        Driver 2: position 12800, standstill, SG min/max 0/1023
                        Driver 3: position 3641, standstill, SG min/max not available
                        Driver 4: position 0, standstill, SG min/max not available
                        Driver 5: position 0, standstill, SG min/max not available
                        Driver 6: position 0, standstill, SG min/max not available
                        Driver 7: position 0, standstill, SG min/max 0/79
                        Driver 8: position 0, standstill, SG min/max not available
                        Driver 9: position 0, standstill, SG min/max not available
                        Driver 10: position 0
                        Driver 11: position 0
                        Date/time: 2024-01-16 14:37:37
                        Cache data hit count 566541634
                        Slowest loop: 9.99ms; fastest: 0.18ms
                        I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                        === Storage ===
                        Free file entries: 10
                        SD card 0 detected, interface speed: 20.0MBytes/sec
                        SD card longest read time 4.0ms, write time 0.0ms, max retries 0
                        === Move ===
                        DMs created 83, maxWait 179513ms, bed compensation in use: none, comp offset 0.000
                        === MainDDARing ===
                        Scheduled moves 26, completed moves 26, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                        === AuxDDARing ===
                        Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                        === Heat ===
                        Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                        Heater 1 is on, I-accum = 0.0
                        === GCodes ===
                        Segments left: 0
                        Movement lock held by null
                        HTTP is idle in state(s) 0
                        Telnet is idle in state(s) 0
                        File is idle in state(s) 0
                        USB is idle in state(s) 0
                        Aux is idle in state(s) 0
                        Trigger is idle in state(s) 0
                        Queue is idle in state(s) 0
                        LCD is idle in state(s) 0
                        Daemon is idle in state(s) 0
                        Autopause is idle in state(s) 0
                        Code queue is empty.
                        === Network ===
                        Slowest loop: 24.56ms; fastest: 0.00ms
                        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                        HTTP sessions: 1 of 8
                        - WiFi -
                        Network state is active
                        WiFi module is connected to access point 
                        Failed messages: pending 0, notready 0, noresp 0
                        WiFi firmware version 1.26
                        WiFi MAC address 48:3f:da:a6:84:05
                        WiFi Vcc 3.40, reset reason Power up
                        WiFi flash size 2097152, free heap 24400
                        WiFi IP address 10.10.0.163
                        WiFi signal strength -71dBm, mode 802.11n, reconnections 0, sleep mode modem
                        Clock register 00002002
                        Socket states: 0 2 0 0 0 0 0 0
                        === DueX ===
                        Read count 1, 0.13 reads/min
                        
                        droftartsundefined 1 Reply Last reply Reply Quote 0
                        • droftartsundefined
                          droftarts administrators @Adamrobot
                          last edited by

                          @Adamrobot said in home z bug fix:

                          RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2.2

                          M568 is supported from RRF 3.3. An older version of the command was supported up to RRF 1.18.

                          RRF 3.2.2 is not the latest version. RRF 3.4.6 is the current release; download the large zip file "Duet2and3Firmware-3.4.6.zip", without unzipping it, from https://github.com/Duet3D/RepRapFirmware/releases/tag/3.4.6
                          In DWC, click System > Upload System Files and upload the ZIP file to the Duet. This should update the firmware, DWC and probably the WiFi firmware.

                          Ian

                          Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                          Adamrobotundefined 1 Reply Last reply Reply Quote 0
                          • Adamrobotundefined
                            Adamrobot @droftarts
                            last edited by

                            @droftarts

                            Hello Mr Administrator,

                            I upload the newest RRF version, but I still can't head the printhead:(

                            temperature rising too slowly: expected 2.32°C/sec measured 0.63°C/sec

                            M122
                            === Diagnostics ===
                            RepRapFirmware for Duet 2 WiFi/Ethernet version 3.4.6 (2023-07-21 14:08:28) running on Duet WiFi 1.02 or later + DueX5v0.11
                            Board ID: 0JD0M-9X6JA-JUNSN-6JTD2-3SD6T-KBRRV
                            Used output buffers: 1 of 26 (19 max)
                            === RTOS ===
                            Static ram: 23896
                            Dynamic ram: 78284 of which 0 recycled
                            Never used RAM 9564, free system stack 118 words
                            Tasks: NETWORK(notifyWait,15.5%,242) HEAT(notifyWait,0.0%,295) Move(notifyWait,0.0%,282) DUEX(notifyWait,0.0%,24) MAIN(running,84.3%,436) IDLE(ready,0.2%,30), total 100.0%
                            Owned mutexes: WiFi(NETWORK)
                            === Platform ===
                            Last reset 00:10:47 ago, cause: power up
                            Last software reset at 2024-01-16 15:56, reason: User, GCodes spinning, available RAM 9264, slot 1
                            Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                            Error status: 0x00
                            Aux0 errors 0,0,0
                            Step timer max interval 0
                            MCU temperature: min 33.8, current 38.5, max 39.7
                            Supply voltage: min 11.8, current 12.0, max 12.3, under voltage events: 0, over voltage events: 0, power good: yes
                            Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                            Events: 1 queued, 1 completed
                            Driver 0: standstill, SG min 0
                            Driver 1: standstill, SG min 0
                            Driver 2: standstill, SG min 0
                            Driver 3: standstill, SG min n/a
                            Driver 4: standstill, SG min n/a
                            Driver 5: standstill, SG min n/a
                            Driver 6: standstill, SG min n/a
                            Driver 7: standstill, SG min 0
                            Driver 8: standstill, SG min n/a
                            Driver 9: standstill, SG min n/a
                            Driver 10: 
                            Driver 11: 
                            Date/time: 2024-01-16 16:11:41
                            Cache data hit count 4294967295
                            Slowest loop: 19.66ms; fastest: 0.19ms
                            I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                            === Storage ===
                            Free file entries: 10
                            SD card 0 detected, interface speed: 20.0MBytes/sec
                            SD card longest read time 8.9ms, write time 2.1ms, max retries 0
                            === Move ===
                            DMs created 83, segments created 14, maxWait 56617ms, bed compensation in use: none, comp offset 0.000
                            === MainDDARing ===
                            Scheduled moves 145, completed 145, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 93], CDDA state -1
                            === AuxDDARing ===
                            Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                            === Heat ===
                            Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                            === GCodes ===
                            Segments left: 0
                            Movement lock held by null
                            HTTP is idle in state(s) 0
                            Telnet is idle in state(s) 0
                            File is idle in state(s) 0
                            USB is idle in state(s) 0
                            Aux is idle in state(s) 0
                            Trigger is idle in state(s) 0
                            Queue is idle in state(s) 0
                            LCD is idle in state(s) 0
                            Daemon is idle in state(s) 0
                            Autopause is idle in state(s) 0
                            Code queue is empty
                            === DueX ===
                            Read count 1, 0.09 reads/min
                            === Network ===
                            Slowest loop: 22.38ms; fastest: 0.00ms
                            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
                            HTTP sessions: 1 of 8
                            = WiFi =
                            Interface state: active
                            Module is connected to access point 
                            Failed messages: pending 0, notready 0, noresp 0
                            WiFi firmware version 1.27
                            WiFi MAC address 48:3f:da:a6:84:05
                            WiFi Vcc 3.40, reset reason Power up
                            WiFi flash size 2097152, free heap 25136
                            WiFi IP address 10.10.0.163
                            WiFi signal strength -49dBm, mode 802.11n, reconnections 0, sleep mode modem
                            Clock register 00002002
                            Socket states: 0 0 0 0 0 0 0 0
                            
                            droftartsundefined 1 Reply Last reply Reply Quote 0
                            • droftartsundefined
                              droftarts administrators @Adamrobot
                              last edited by droftarts

                              @Adamrobot Please post your config.g. Have you tuned your heaters? See https://docs.duet3d.com/en/How_to_guides/Commissioning#h-6-check-heater-functionality and the section after.

                              Ian

                              Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                              Adamrobotundefined 1 Reply Last reply Reply Quote 0
                              • Adamrobotundefined
                                Adamrobot @droftarts
                                last edited by

                                @droftarts Hello Mr administrator,

                                I tried to tune my heater, but it was always unsuccessful. The error displayed is: Auto tune cancelled because target temperature was not reached.

                                My config:

                                ; Configuration file for Duet WiFi / Ethernet running RRF3 on E3D Tool Changer
                                ; executed by the firmware on start-up
                                
                                ; General preferences
                                M111 S0 						; Debugging off
                                G21 							; Work in millimetres
                                G90 							; Send absolute coordinates...
                                M83 							; ...but relative extruder moves
                                M555 P2 						; Set firmware compatibility to look like Marlin
                                M667 S1 						; Select CoreXY mode	
                                
                                ; Network
                                M550 P"ToolChanger" 			; Set machine name
                                ;M587 S"ssid" P"password"		; WiFi Settings
                                ;M552 S1 P"ssid"				; Enable WiFi Networking
                                M552 S1							; Enable Networking
                                M586 P0 S1 						; Enable HTTP
                                M586 P1 S0 						; Disable FTP
                                M586 P2 S0 						; Disable Telnet
                                
                                ; Drive direction
                                M569 P0 S0 						; Drive 0 X
                                M569 P1 S0 						; Drive 1 Y
                                M569 P2 S1 						; Drive 2 Z
                                M569 P3 S0 						; Drive 3 E0
                                M569 P4 S0 						; Drive 4 E1
                                M569 P5 S1 						; Drive 5 E2
                                M569 P6 S1 						; Drive 6 E3
                                M569 P7 S0 						; Drive 7 COUPLER
                                M569 P8 S0 						; Drive 8 UNUSED
                                M569 P9 S0 						; Drive 9 UNUSED
                                
                                M584 X0 Y1 Z2 C7 E3:4:5:6 								; Apply custom drive mapping
                                M208 X-35:328.5 Y-49:243 Z0:300 C-45:360	 				; Set axis maxima & minima
                                M92 X100 Y100 Z1600 C91.022 E834:834:834:834				; Set steps per mm assuming x16 microstepping
                                M350 E16:16:16:16 I1 									; Configure microstepping with interpolation
                                M350 C16 I10											; Configure microstepping without interpolation
                                M350 X16 Y16 Z16 I1										; Configure microstepping with interpolation
                                M566 X400 Y400 Z8 C2 E2:2:2:2							; Set maximum instantaneous speed changes (mm/min)
                                M203 X35000 Y35000 Z1200 C5000 E5000:5000:5000:5000	; Set maximum speeds (mm/min)
                                M201 X6000 Y6000 Z400 C500 E2500:2500:2500:2500			; Set accelerations (mm/s^2)
                                M906 X1800 Y1800 Z1330 I30   						; Idle motion motors to 30%
                                M906 E1000:1000:1000:1000 C500 I10     						; Idle extruder motors to 10%
                                
                                ; Endstops
                                M574 X1 Y1 S3 					; Set X / Y endstop stall detection
                                M574 C0 Z0  						; No C Z endstop
                                
                                ; Z probe
                                M558 P8 C"zstop" H3 F360 I0 T20000 	; Set Z probe type to switch, the axes for which it is used and the dive height + speeds
                                G31 P200 X0 Y0 Z0	 				; Set Z probe trigger value, offset and trigger height
                                M557 X10:290 Y20:180 S40 			; Define mesh grid
                                
                                ;Stall Detection
                                M915 X Y S3 F0 H400 R4700				; X / Y Axes
                                
                                ; Heaters
                                M308 S0 P"bedtemp" Y"thermistor" A"Bed" T100000 B4138 C0 		; Set thermistor 
                                M950 H0 C"bedheat" T0											; Bed heater
                                M143 H0 S225 													; Set temperature limit for heater 0 to 225C
                                M140 H0															; Bed heater is heater 0
                                
                                M308 S1 P"e0temp" Y"thermistor" A"T0" T100000 B4725 C7.06e-8 	; Set thermistor
                                M950 H1 C"e0heat" T1											; Extruder 0 heater
                                M143 H1 S305 													; Set temperature limit for heater 1 to 300C
                                
                                M308 S2 P"e1temp" Y"thermistor" A"T1" T100000 B4725 C7.06e-8 	; Set thermistor
                                M950 H2 C"e1heat" T2											; Extruder 0 heater
                                M143 H2 S305 													; Set temperature limit for heater 2 to 300C
                                
                                M308 S3 P"e2temp" Y"thermistor" A"T2" T100000 B4725 C7.06e-8 	; Set thermistor
                                M950 H3 C"duex.e2heat" T3										; Extruder 0 heater
                                M143 H3 S305 													; Set temperature limit for heater 3 to 300C
                                
                                M308 S4 P"e3temp" Y"thermistor" A"T3" T100000 B4725 C7.06e-8 	; Set thermistor
                                M950 H4 C"duex.e3heat" T4										; Extruder 0 heater
                                M143 H4 S305 													; Set temperature limit for heater 4 to 300C
                                
                                
                                ; Tools
                                M563 P0 S"T0" D0 H1 F2 					; Define tool 0
                                G10 P0 X0 Y0 Z0 						; Reset tool 0 axis offsets
                                G10 P0 R0 S0 							; Reset initial tool 0 active and standby temperatures to 0C
                                
                                M563 P1 S"T1" D1 H2 F4 					; Define tool 1
                                G10 P1 X0 Y0 Z0 						; Reset tool 1 axis offsets
                                G10 P1 R0 S0 							; Reset initial tool 1 active and standby temperatures to 0C
                                
                                M563 P2 S"T2" D2 H3 F6 					; Define tool 2
                                G10 P2 X0 Y0 Z0 						; Reset tool 2 axis offsets
                                G10 P2 R0 S0 							; Reset initial tool 2 active and standby temperatures to 0C
                                
                                M563 P3 S"T3" D3 H4 F8 					; Define tool 3
                                G10 P3 X0 Y0 Z0 						; Reset tool 3 axis offsets
                                G10 P3 R0 S0 							; Reset initial tool 3 active and standby temperatures to 0C
                                
                                ; Fans
                                M950 F1 C"fan1"
                                M950 F2 C"fan2"
                                M950 F3 C"duex.fan3"
                                M950 F4 C"duex.fan4"
                                M950 F5 C"duex.fan5"
                                M950 F6 C"duex.fan6"
                                M950 F7 C"duex.fan7"
                                M950 F8 C"duex.fan8"
                                
                                M106 P1 S255 H1 T70				; T0 HE
                                M106 P2 S0						; T0 PCF
                                M106 P3 S255 H2 T70 			; T1 HE
                                M106 P4 S0						; T1 PCF 
                                M106 P5 S255 H3 T70 			; T2 HE 
                                M106 P6 S0 						; T2 PCF
                                M106 P7 S255 H4 T70				; T3 HE
                                M106 P8 S0						; T3 PCF
                                
                                M593 F42.2						; cancel ringing at 42.2Hz (https://forum.e3d-online.com/threads/accelerometer-and-resonance-measurements-of-the-motion-system.3445/)
                                ;M376 H15						; bed compensation taper
                                
                                ;tool offsets
                                ; !ESTIMATED! offsets for:
                                ; V6-tool: X-9 Y39 Z-5
                                ; Volcano-tool: X-9 Y39 Z-13.5
                                ; Hemera-tool: X20 Y43.5 Z-6
                                
                                G10 P0 X-9 Y39 Z-5					; T0
                                G10 P1 X-9 Y39 Z-5					; T1
                                G10 P2 X-9 Y39 Z-5					; T2
                                G10 P3 X-9 Y39 Z-5					; T3
                                
                                ;M572 D0 S0.2 						; pressure advance T0
                                ;M572 D1 S0.2 						; pressure advance T1
                                ;M572 D2 S0.2 						; pressure advance T2
                                ;M572 D3 S0.2 						; pressure advance T3
                                
                                M575 P1 S1 B57600				; Enable LCD
                                G29 S2							    ; disable mesh
                                T-1								      ; deselect tools
                                
                                M501                    ; load config-override.g
                                
                                
                                

                                and the PID parameter:

                                M307 H4
                                Heater 4: heating rate 2.430, cooling rate 0.560, dead time 30.00, max PWM 1.00, mode PID, calibrated at 0.0V
                                Predicted max temperature rise 296°C
                                PID parameters: heating P2.4 I0.032 D51.4, steady P2.4 I0.045 D51.4
                                Heater 4: heating rate 2.430, cooling rate 0.560, dead time 30.00, max PWM 1.00, mode PID, calibrated at 0.0V
                                Predicted max temperature rise 296°C
                                PID parameters: heating P2.4 I0.032 D51.4, steady P2.4 I0.045 D51.4
                                
                                droftartsundefined 1 Reply Last reply Reply Quote 0
                                • droftartsundefined
                                  droftarts administrators @Adamrobot
                                  last edited by

                                  @Adamrobot Is it just heater 4 that can't tune, or is it a problem for all heaters? What command are you sending to tune the heater? What does the graph look like when you tune that heater, and is it different from the other heaters if their tuning succeeds?

                                  Ian

                                  Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                  Adamrobotundefined 1 Reply Last reply Reply Quote 0
                                  • Adamrobotundefined
                                    Adamrobot @droftarts
                                    last edited by

                                    @droftarts I attempted to tune heater1 and heater4, the Command is M303 T0(T3) S200, and the result was the same, both heaters can only reach a maximum of around 150 degrees, and the heating will stop and in Console shows tune canceled.

                                    the temperature is as follows
                                    截屏2024-01-19 15.34.49.png

                                    droftartsundefined 1 Reply Last reply Reply Quote 0
                                    • droftartsundefined
                                      droftarts administrators @Adamrobot
                                      last edited by

                                      @Adamrobot From your M122 report, you are running this machine on 12V. Are your heaters 12V? I think they are 24V heaters, which will not get to temperature on 12V.

                                      Ian

                                      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                      Adamrobotundefined 1 Reply Last reply Reply Quote 0
                                      • Adamrobotundefined
                                        Adamrobot @droftarts
                                        last edited by

                                        @droftarts
                                        Hello mr administrator,

                                        If it's an issue of insufficient voltage, can I adjust the voltage of the heater on DWC? Or do I need to replace it with a higher power supply module?

                                        DIY-O-Sphereundefined 1 Reply Last reply Reply Quote 0
                                        • DIY-O-Sphereundefined
                                          DIY-O-Sphere @Adamrobot
                                          last edited by

                                          @Adamrobot
                                          This has nothing to do with a problem in the power supply unit.
                                          You have to check whether the heating cartridge is made for 12V or 24V.
                                          Either check the marking on the sleeve or measure the internal resistance.
                                          In general 24v supply voltage would be an advantage. However, you then also have to replace the heating bed and maybe the fans.

                                          (UTC+1)

                                          1 Reply Last reply Reply Quote 0
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