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    Z-axis / tramming issues with 3.6.0-alpha2+3

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    • DonStaufferundefined
      DonStauffer @gloomyandy
      last edited by

      @gloomyandy I could, but hasn't Exerqtor already confirmed that? I think I saw a post where he said he reverted and the problem went away. This didn't happen on 3.5.2 ~2 or 3 weeks ago when I leveled the bed hundreds of times.

      I understand about alpha. I was stuck because I couldn't print but I found a way for now that works OK. It's a pain though.

      What I have done is set my bed.g for one iteration and used the S-1 parameter for the last G30, so it only prints the adjustments that are needed. Then I've been manually adjusting the various Z motors according to that. Then I re-home and G32 again. It took me a couple hours, but the bed is level and the printer is printing now. So it's clearly the G30 S3 that's wrongly adjusting the motors some of the time.

      gloomyandyundefined 1 Reply Last reply Reply Quote 0
      • gloomyandyundefined
        gloomyandy @DonStauffer
        last edited by gloomyandy

        @DonStauffer The more data points we can gather the faster we will be able to identify and hopefully fix the problems. From reading the reports it seems that @Exerqtor was able to tram his bed several times using 3.6 without any issues before then running into problems. I'm not sure how many times it worked after reverting to 3.5 but clearly for Exerqtor it is not a simple case of 3.5 works and 3.6 does not.

        @all it might be useful to understand what direction the stepper that has problems is trying to move in (and perhaps what direction it moved in last), so for instance does the error only occur with a stepper that is trying to move up (or down) and did it last move in the same or a different direction.

        @DonStauffer when you manually adjust the steppers to level the bed what commands are you actually using and do they work correctly?

        Exerqtorundefined DonStaufferundefined 3 Replies Last reply Reply Quote 0
        • Exerqtorundefined
          Exerqtor @gloomyandy
          last edited by Exerqtor

          @gloomyandy Yeah it worked 2-3 times (at least) on 3.6 for me before acting up all off a sudden. On 3.5 it's running stable without issues (and it has been since release).

          I'll smack together a simplified bed.g, verify it working stabily with 3.5 by doing 20-30 back too back G32's. Then upgrade too 3.6, enable debug logging and do the same there, and report back here with how it went.

          gloomyandyundefined 1 Reply Last reply Reply Quote 0
          • gloomyandyundefined
            gloomyandy @Exerqtor
            last edited by

            @Exerqtor If you can please make a note of the stepper that has a problem and the direction that it has been asked to move in.

            Exerqtorundefined 1 Reply Last reply Reply Quote 0
            • edspedundefined
              edsped
              last edited by

              Add another to the list of those with tramming issues. Just trashed my build sheet. I've never had an issue with the printer before so I'm pretty sure it's related to the 3.6 A... Reverted back to 3.5.2 and am re printing now. There's definitely a difference in tramming between the two...

              Tramming with 3.6... This is the print that trashed the sheet...
              Screenshot 2024-08-03 100058.jpg

              Tramming with 3.5.2 After crash...
              Screenshot 2024-08-03 101207.jpg

              Damage...
              IMG_3852.JPG IMG_3853.JPG

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              • Exerqtorundefined
                Exerqtor @gloomyandy
                last edited by Exerqtor

                @gloomyandy said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                @Exerqtor If you can please make a note of the stepper that has a problem and the direction that it has been asked to move in.

                I'm 99.9% sure the what happened in my case (when it was fucking up the adjustments in the coarse tramming pass) is that the "front right" axis (0.4 in my case) went up rather than down. But I might be able to verify this when I get time to run the macro I make for debug later.

                @edsped said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                Add another to the list of those with tramming issues. Just trashed my build sheet. I've never had an issue with the printer before so I'm pretty sure it's related to the 3.6 A... Reverted back to 3.5.2 and am re printing now. There's definitely a difference in tramming between the two...

                Ouch that sucks! Hope your hotend/nozzle didn't take any damage 😢


                As a baseline reference this is my standard set off tramming macros (if I forgot to add a sub-macro let me know and I'll supply that as well.

                bed.g
                bed_probe_points

                The homing macro's haven't been acting up so I didn't bother adding those.

                I'll upload the simplified/debug bed.g once I get time to write it!

                edspedundefined 1 Reply Last reply Reply Quote 0
                • edspedundefined
                  edsped @Exerqtor
                  last edited by

                  @Exerqtor

                  Nozzle, gammamaster, appears to be okay, No first layer or offset issues so I'm guessing the rapido is okay but I wouldn't be surprised if the heatbreak isn't a little tweaked. I've got thousands of toolchanges and the same with print starts and this is the first time, other than the initial commissioning of the printer that I had something like this happen. I'm definitely bummed but knew what I was getting into when I loaded an alpha firmware. Coarse tramming was definitely not as good on 3.6 as it is on 3.5.2 as can be seen in my screenshots.

                  1 Reply Last reply Reply Quote 0
                  • edspedundefined
                    edsped
                    last edited by

                    My bed.g is pretty basic but am posting just i case it helps..
                    bed.g

                    DonStaufferundefined 1 Reply Last reply Reply Quote 0
                    • DonStaufferundefined
                      DonStauffer @gloomyandy
                      last edited by

                      @gloomyandy

                      ;-------------------------------------------------------------------------------
                      ;	MoveZStepper Macro
                      ;-------------------------------------------------------------------------------
                      ;	Moves one Z stepper independently, for manual, coarse tramming. Creates
                      ;	(or reuses) an A axis for the purpose, then hides it when done.
                      ;
                      ;	Parameters:
                      ;		N	Stepper number (default: 7)
                      ;		Z	Distance. which may be negative to move up (default: 1)
                      ;		S	Speed (default: 150)
                      ;-------------------------------------------------------------------------------
                      ;	Don Stauffer					July, 2024
                      ;-------------------------------------------------------------------------------
                      ;if global.DebugLevel >= 1200
                      ;	var This = "MoveZStepper"
                      ;	set var.This = var.This^(exists(param.N) ? " N"^param.N : "")
                      ;	set var.This = var.This^(exists(param.Z) ? " Z"^param.Z : "")
                      ;	set var.This = var.This^(exists(param.S) ? " S"^param.S : "")
                      ;	echo var.This
                      ;-------------------------------------------------------------------------------
                      ;	Parameters
                      ;-------------------------------------------------------------------------------
                      var StepperNum = (exists(param.N) ? param.N : 7)
                      var Distance = (exists(param.Z) ? param.Z : 1)
                      var Speed = (exists(param.S) ? param.S : 150)
                      ;-------------------------------------------------------------------------------
                      ;	Echo back what will be done
                      ;-------------------------------------------------------------------------------
                      echo "Moving Z stepper", var.StepperNum, "by", var.Distance
                      ;-------------------------------------------------------------------------------
                      ;	Create A axis if necessary; make it visible if it already exists
                      ;-------------------------------------------------------------------------------
                      var DoesAAxisExist = false
                      
                      while iterations < #move.axes
                      	if move.axes[iterations].letter != "A"
                      		continue
                      	set var.DoesAAxisExist = true
                      	break
                      
                      if var.DoesAAxisExist
                      	M584 P4
                      M584 A{var.StepperNum}
                      ;-------------------------------------------------------------------------------
                      ;	Configuration adapted from config.g. Not sure if everything is needed here
                      ;-------------------------------------------------------------------------------
                      M669 K1			    ;	CoreXY mode
                      M350 A16 I1		    ;	16x microstepping for axes & extruder, w/interpolation
                      M574 A1 S2			;	Set Endstop configuration (P"pin_name"); S2 = Z probe
                      M906 A1500 I60		;	Set motor currents (mA)
                      M203 A{var.Speed}	;	Maximum speeds (mm/min)
                      
                      M566 A12			;	Jerk
                      M201 A90			;	Max acceleration
                      
                      M208 A635			;	Set axis maxima & high homing switch positions
                      M208 A-0.5 S1		;	Set axis minima & low homing switch positions
                      
                      M92 A3200			;	Steps/mm
                      ;-------------------------------------------------------------------------------
                      ;	Move the Z stepper as the "A axis"
                      ;-------------------------------------------------------------------------------
                      G91
                      G1 A{var.Distance} H2
                      ;-------------------------------------------------------------------------------
                      ;	Reset everything back to the same as config.g
                      ;-------------------------------------------------------------------------------
                      M584 X0 Y1 Z5:6:7	;	Map Z to drivers 5, 6, 7.
                      
                      M669 K1			    ;	CoreXY mode
                      M350 Z16 I1		    ;	16x microstepping for axes & extruder, w/interpolation
                      M574 Z1 S2			;	Set Endstop configuration (P"pin_name"); S2 = Z probe
                      M906 Z1500 I60		;	Set motor currents (mA)M203 Z600
                      M203 Z600			;	Maximum speeds (mm/min)
                      
                      M566 Z12			;	Jerk
                      M201 Z90			;	Max acceleration
                      
                      M208 Z635			;   set axis maxima & high homing switch positions
                      M208 Z-0.5 S1		;   set axis minima & low homing switch positions
                      
                      M92 Z3200			;   Steps/mm
                      ;-------------------------------------------------------------------------------
                      ;	Hide A-axis by setting number of visible axes back to 3
                      ;-------------------------------------------------------------------------------
                      M584 P3
                      ;-------------------------------------------------------------------------------
                      ;if global.DebugLevel >= 1200
                      ;	echo "Leaving MoveZStepper"
                      ;-------------------------------------------------------------------------------
                      
                      1 Reply Last reply Reply Quote 0
                      • DonStaufferundefined
                        DonStauffer @gloomyandy
                        last edited by

                        @gloomyandy If you tell me the procedure I'll revert and then test it.

                        It's possible that the direction problem is that when a negative adjustment is needed, it does a positive adjustment. That does happen. I don't know if it happens the other way around, but I have seen this.

                        dc42undefined 1 Reply Last reply Reply Quote 0
                        • dc42undefined
                          dc42 administrators @DonStauffer
                          last edited by dc42

                          @DonStauffer @Exerqtor @edsped thanks for reporting this. I'm sorry for any damage caused.

                          I don't have a system with multiple Z motors that I can test on, but I think I know what is causing this. It's to do with getting the motor direction wrong when switching between normal Z moves and leadscrew adjustment moves. Please can you identify for me which of the following is happening:

                          1. When the first bed tramming move is executed, some of the motors move in the wrong direction.
                          2. Immediately after the first bed tramming move is executed, when executing a normal Z move (which could be part of a new G32 probing sequence), some of the the Z motors move in the wrong direction.
                          3. Both of the above.

                          If the main problem is #2 then a workaround for now might be to insert M400 after the G32 call, to ensure motion stops before another Z move is executed.

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                          Exerqtorundefined DonStaufferundefined 3 Replies Last reply Reply Quote 0
                          • Exerqtorundefined
                            Exerqtor @dc42
                            last edited by Exerqtor

                            @dc42 said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                            @DonStauffer @Exerqtor @edsped thanks for reporting this. I'm sorry for any damage caused.

                            It's part of the course with testing pre-release stuff imo! Win some loose some 😅

                            I don't have a system with multiple Z motors that I can test on, but I think I know what is causing this. It's to do with getting the motor direction wrong when switching between normal Z moves and leadscrew adjustment moves. Please can you identify for me which of the following is happening:

                            1. When the first bed tramming move is executed, some of the motors move in the wrong direction.
                            2. Immediately after the first bed tramming move is executed, when executing a normal Z move (which could be part of a new G32 probing sequence), some of the the Z motors move in the wrong direction.
                            3. Both of the above.

                            If the main problem is #2 then a workaround for now might be to insert M400 after the G32 call, to ensure motion stops before another Z move is executed.

                            Well, when I think back the first time it happened for me was during the Z homing routine before tramming start. I think it was between one of the "tolerance" moves when doing G30. Did the first move, went to lower the bed to specified dive height, but rather than switching over the two front axis to rise up again to "engage" the second probe once dive height was reached they contiuned on a downwards motion.

                            The other times it happened it seemd to apply the axis adjustements wronlgy (in 1 or all axis) when it was done with the G30 moves for tramming.

                            If that made sense?

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                            • DonStaufferundefined
                              DonStauffer @dc42
                              last edited by

                              @dc42 I have not had bed tramming without one of the motors going the wrong direction since installing alpha 2. I will have to test for #2. I don't think I've seen it but I wasn't looking for it.

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                              • DonStaufferundefined
                                DonStauffer @edsped
                                last edited by DonStauffer

                                @edsped Here's my bed.g, and the DefineBed macro you have to run to create the global Bed variable it uses for the data points:

                                ;-------------------------------------------------------------------------------
                                ;	bed.g
                                ;-------------------------------------------------------------------------------
                                ;	Bed leveling macro.
                                ;-------------------------------------------------------------------------------
                                ;	Don Stauffer									July, 2024
                                ;-------------------------------------------------------------------------------
                                ;   Subscript Constants
                                ;-------------------------------------------------------------------------------
                                var LEV = 1
                                ;-------------------------------------------------------------------------------
                                ;   Other Constants
                                ;-------------------------------------------------------------------------------
                                var ITERATION_COUNT_MAX = 15
                                var ERR_ALLOWED = 0.005
                                ;-------------------------------------------------------------------------------
                                ;	Clear any existing bed transform and move up
                                ;-------------------------------------------------------------------------------
                                M561
                                G1 H2 Z5
                                ;-------------------------------------------------------------------------------
                                ;	Start NeoPixel progress meters
                                ;-------------------------------------------------------------------------------
                                ;M98 P"0:/macros/Lights/NeoPixel/Progress/BedLeveling/StartProgressMeters" E{var.ERR_ALLOWED}
                                ;-------------------------------------------------------------------------------
                                ;	Iteratively attempt to level the bed
                                ;-------------------------------------------------------------------------------
                                var Raw = null
                                var Abs = null
                                var Sign = null
                                var x = null
                                var y = null
                                var z = null
                                
                                var Err = pow(2, 31)		;	"infinity"
                                
                                while iterations < var.ITERATION_COUNT_MAX && var.Err > var.ERR_ALLOWED
                                	;---------------------------------------------------------------------------
                                	;   Retrieve and probe the points
                                	;---------------------------------------------------------------------------
                                	while iterations < #(global.Bed[var.LEV])
                                		;-----------------------------------------------------------------------
                                		;   Decode probe point coordinates
                                		;-----------------------------------------------------------------------
                                		set var.Raw = mod(global.Bed[var.LEV][iterations], pow(2, 15))
                                		set var.Abs = mod(var.Raw, pow(2, 14))
                                		set var.Sign = floor((var.Raw - var.Abs) / pow(2, 14) + 0.5)
                                		set var.x = var.Abs * (1 - var.Sign * 2)
                                
                                		set var.Raw = floor((global.Bed[var.LEV][iterations]-var.Raw)/pow(2, 15)+ 0.5)
                                		set var.Abs = mod(var.Raw, pow(2, 14))
                                		set var.Sign = floor((var.Raw - var.Abs) / pow(2, 14) + 0.5)
                                		set var.y = var.Abs * (1 - var.Sign * 2)
                                		;-----------------------------------------------------------------------
                                		;	Moving this way updates move.axes[i].userPosition faster
                                		;	(Important for NeoPixel progress meter for index)
                                		;-----------------------------------------------------------------------
                                		set var.z =sensors.probes[0].diveHeights[0]-sensors.probes[0].offsets[2]
                                		;-----------------------------------------------------------------------
                                		;	Probe the point
                                		;-----------------------------------------------------------------------
                                		if iterations ==  #(global.Bed[var.LEV]) - 1
                                			G30 P{iterations} X{var.x} Y{var.y} Z-99999 S3
                                			;G30 P{iterations} X{var.x} Y{var.y} Z-99999 S{#(global.Bed[var.LEV])}
                                		else
                                			G30 P{iterations} X{var.x} Y{var.y} Z-99999
                                	;---------------------------------------------------------------------------
                                	;	Calculate the error sum
                                	;---------------------------------------------------------------------------
                                	set var.Err = abs(move.calibration.initial.mean)
                                	set var.Err = var.Err + move.calibration.initial.deviation
                                
                                	if global.DebugLevel > 1000
                                		echo "Error="^var.Err,"Mean="^move.calibration.initial.mean,"Dev="^move.calibration.initial.deviation
                                
                                if var.Err > var.ERR_ALLOWED
                                	echo "Leveling didn't converge;",var.ITERATION_COUNT_MAX,"tries. Error="^var.Err
                                else
                                	echo "Leveling converged. Error="^var.Err
                                ;-------------------------------------------------------------------------------
                                ;	Move to center (necessary for NeoPixel progress meters to detect done)
                                ;-------------------------------------------------------------------------------
                                G53 G1 X150 Y150 F9000
                                ;-------------------------------------------------------------------------------
                                ;	Wait for NeoPixel progress mweter processes to end themselves
                                ;-------------------------------------------------------------------------------
                                ;M98 P"0:/macros/Lights/NeoPixel/Progress/WaitForEnd"
                                
                                ;-------------------------------------------------------------------------------
                                ;	DefineBed Macro
                                ;-------------------------------------------------------------------------------
                                ;   Initializes global.Bed.
                                ;   global.Bed[var.LEV] contains the 3 probe points for bed leveling, encoded
                                ;   as bitmaps to save memory.
                                ;
                                ;   This is intended to be called from config.g.
                                ;
                                ;   The X and Y coordinates of each point are compressed into a single integer
                                ;   for memory conservation. The decoding routine is at the bottom of this file.
                                ;-------------------------------------------------------------------------------
                                ;	Don Stauffer					            July, 2024
                                ;-------------------------------------------------------------------------------
                                ;if global.DebugLevel >= 1200
                                ;	echo "DefineBed"
                                ;-------------------------------------------------------------------------------
                                ;	Subscript Constants
                                ;-------------------------------------------------------------------------------
                                var HTR = 0
                                var OM = 0
                                ;var STATE = 1
                                
                                var LEV = 1
                                ;-------------------------------------------------------------------------------
                                ;   Create global.Bed if necessary
                                ;-------------------------------------------------------------------------------
                                if !exists(global.Bed)
                                    global Bed = vector(2, null)
                                    set global.Bed[var.HTR] = vector(2, null)
                                    set global.Bed[var.LEV] = vector(3, null)
                                ;-------------------------------------------------------------------------------
                                ;   Define probe points for bed leveling; bitmap encode to save memory
                                ;-------------------------------------------------------------------------------
                                var x = {10, 10, 265}
                                var y = {12, 228, 100}
                                
                                while iterations < 3
                                    ;---------------------------------------------------------------------------
                                    ;   Encode x and y coordinates into a single integer
                                    ;---------------------------------------------------------------------------
                                    var xEnc = abs(var.x[iterations]) + (var.x[iterations] < 0 ? pow(2, 14) : 0)
                                
                                    var yEnc = abs(var.y[iterations]) * pow(2, 15)
                                    set var.yEnc = var.yEnc + (var.y[iterations] < 0 ? pow(2, 29) : 0)
                                
                                    set global.Bed[var.LEV][iterations] = var.xEnc + var.yEnc
                                ;-------------------------------------------------------------------------------
                                ;   Set up bed heater information
                                ;-------------------------------------------------------------------------------
                                while iterations < #heat.bedHeaters
                                    if heat.bedHeaters[iterations] != -1
                                        set global.Bed[var.HTR][var.OM] = iterations
                                        break
                                ;-------------------------------------------------------------------------------
                                ;if global.DebugLevel >= 1200
                                ;	echo "Leaving DefineBed"
                                ;-------------------------------------------------------------------------------
                                M99
                                ;-------------------------------------------------------------------------------
                                ;   To decode bitmap-encoded probe points:
                                ;-------------------------------------------------------------------------------
                                while iterations < 3
                                
                                    var P = global.Bed[var.LEV][iterations]
                                
                                    var xRaw = mod(var.P, pow(2, 15))
                                    var yRaw = floor((var.P - var.xRaw) / pow(2, 15) + 0.5)
                                
                                    var xAbs = mod(var.xRaw, pow(2, 14))
                                    var yAbs = mod(var.yRaw, pow(2, 14))
                                
                                    var xSign = floor((var.xRaw - var.xAbs) / pow(2, 14) + 0.5)
                                    var ySign = floor((var.yRaw - var.yAbs) / pow(2, 14) + 0.5)
                                
                                    var xDec = var.xAbs * (1 - var.xSign * 2)
                                    var yDec = var.yAbs * (1 - var.ySign * 2)
                                
                                    echo "("^var.xDec^",", var.yDec^")"
                                
                                
                                Exerqtorundefined 1 Reply Last reply Reply Quote 0
                                • Exerqtorundefined
                                  Exerqtor @DonStauffer
                                  last edited by Exerqtor

                                  Just slapped together a stripped down bed.g, hopefully i get time to test it either today or tomorrow.

                                  bed.g

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                                  • DonStaufferundefined
                                    DonStauffer @dc42
                                    last edited by

                                    @dc42 Here are my testing results.

                                    In bed.g, I inserted immediately after my first G30:

                                    		G1 Z25 F75
                                    		M99
                                    

                                    Then I homed and did a G32. Nothing that happened was unexpected. The motors all ran in the correct direction. So the only issue I can confirm is that the adjustment when the G30 with the S parameter executes goes in the wrong direction for one of the motors - and not always the same one. Initially it was #7. Then when I did my "manual" tramming with bed.g doing S-1 to report the correct adjustments, it was #6. I did that manual tramming over and over, making very conservative adjustments, and throughout several hours it remained #6. But it absolutely was a different motor than the problem started on. And there's no doubt it isn't just a simple reversal - it's conditional, only apparently happening on the G30 S adjustments.

                                    So, my answer is "neither #1 nor #2".

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                                    • edspedundefined
                                      edsped
                                      last edited by

                                      Switched back to 3.6 alpha 2 +3 and for me at least it looks like it's applying the the leadscrew adjustments in the wrong direction. If you look at my screenshot the offsets pretty much double on each iteration. Note, for the initial print adjustments were similar to what I got on 3.5.2 but G32 after the print gave the wonky adjustments.

                                      Screenshot 2024-08-03 162037.jpg

                                      Disregard the bed.g warnings I inadvertently hit save when exiting out of the editor.

                                      edspedundefined DonStaufferundefined 2 Replies Last reply Reply Quote 0
                                      • edspedundefined
                                        edsped @edsped
                                        last edited by edsped

                                        @edsped Running a second tram immediately following the above resulted in my front left leadscrew ending ~4mm higher than the other two... FWIW, the front left side of my bed is also where my nozzle crashed due to that corner of the bed being too high. I should clarify, higher on my printer is actually - Z

                                        Edit:
                                        Powered down and back up and now get the following on G32...

                                        8/3/2024, 4:38:57 PM Error: Compensation or calibration cancelled due to probing errors
                                        8/3/2024, 4:38:52 PM Error: G30: Probe was not triggered during probing move

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                                        • DonStaufferundefined
                                          DonStauffer @edsped
                                          last edited by

                                          @edsped Interesting. I was only having one of the three go in the wrong direction.

                                          edspedundefined 1 Reply Last reply Reply Quote 0
                                          • edspedundefined
                                            edsped @DonStauffer
                                            last edited by

                                            @DonStauffer That's what mine was doing the first time. I reverted to 3.5.2 then back to 3.6 a2+3 and added the M400 as suggested by @dc42 and what I posted above are my results. This time knowing what I was looking for I was able to bail before anything bad happened.

                                            dc42undefined 1 Reply Last reply Reply Quote 0
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