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    Z-axis / tramming issues with 3.6.0-alpha2+3

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    • edspedundefined
      edsped @edsped
      last edited by edsped

      @edsped Running a second tram immediately following the above resulted in my front left leadscrew ending ~4mm higher than the other two... FWIW, the front left side of my bed is also where my nozzle crashed due to that corner of the bed being too high. I should clarify, higher on my printer is actually - Z

      Edit:
      Powered down and back up and now get the following on G32...

      8/3/2024, 4:38:57 PM Error: Compensation or calibration cancelled due to probing errors
      8/3/2024, 4:38:52 PM Error: G30: Probe was not triggered during probing move

      1 Reply Last reply Reply Quote 0
      • DonStaufferundefined
        DonStauffer @edsped
        last edited by

        @edsped Interesting. I was only having one of the three go in the wrong direction.

        edspedundefined 1 Reply Last reply Reply Quote 0
        • edspedundefined
          edsped @DonStauffer
          last edited by

          @DonStauffer That's what mine was doing the first time. I reverted to 3.5.2 then back to 3.6 a2+3 and added the M400 as suggested by @dc42 and what I posted above are my results. This time knowing what I was looking for I was able to bail before anything bad happened.

          dc42undefined 1 Reply Last reply Reply Quote 0
          • dc42undefined
            dc42 administrators @edsped
            last edited by

            Currently, after performing probing a bed tramming move is executed with all Z motors moving simultaneously in different amounts and a mixture of directions. Would there be any problem if the Z motor moves were executed one at a time sequentially instead?

            Duet WiFi hardware designer and firmware engineer
            Please do not ask me for Duet support via PM or email, use the forum
            http://www.escher3d.com, https://miscsolutions.wordpress.com

            gloomyandyundefined Exerqtorundefined 2 Replies Last reply Reply Quote 0
            • gloomyandyundefined
              gloomyandy @dc42
              last edited by

              @dc42 Could this in some situations cause a nozzle strike? I'm thinking of a situation with a very highly tilted bed and homing/probing in the middle portion of the bed, you could in theory end up with the nozzle lower then one edge of the bed and if you then raise the (currently) lower edge first the bed would hit the nozzle? The same situation with a simultaneous move may not cause the strike? Probably not very likely though.

              Possible mitigating actions: Perform any negative (moving the bed away from the nozzle) moves first? Limit the distance each motor moves in one operation and cycle through the motors until the move is complete?

              dc42undefined 1 Reply Last reply Reply Quote 0
              • dc42undefined
                dc42 administrators @gloomyandy
                last edited by

                @gloomyandy said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                ould this in some situations cause a nozzle strike? I'm thinking of a situation with a very highly tilted bed and homing/probing in the middle portion of the bed, you could in theory end up with the nozzle lower then one edge of the bed and if you then raise the (currently) lower edge first the bed would hit the nozzle?

                If the probe had to make a deeper than normal move ton reach the lower edge, it will still rise to the dive height above the Z=0 reference afterwards. So I don't think this is a risk, provided that the maximum permitted correction is less than the dive height - which already needs to be the case if nozzle strikes are to be avoided.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

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                • Exerqtorundefined
                  Exerqtor @dc42
                  last edited by Exerqtor

                  @dc42 said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                  Currently, after performing probing a bed tramming move is executed with all Z motors moving simultaneously in different amounts and a mixture of directions. Would there be any problem if the Z motor moves were executed one at a time sequentially instead?

                  @gloomyandy said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                  @dc42 Could this in some situations cause a nozzle strike? I'm thinking of a situation with a very highly tilted bed and homing/probing in the middle portion of the bed, you could in theory end up with the nozzle lower then one edge of the bed and if you then raise the (currently) lower edge first the bed would hit the nozzle? The same situation with a simultaneous move may not cause the strike? Probably not very likely though.

                  Possible mitigating actions: Perform any negative (moving the bed away from the nozzle) moves first? Limit the distance each motor moves in one operation and cycle through the motors until the move is complete?

                  I don't know if this is possible, but is it possible to do it sequentially like you are proposing, but RRF "automatically" choose which axis/stepper to move 1st, 2nd, 3rd, etc. depending on the specified adjustmen that has to be made (taking my drive mapping as example)?

                  ; (While looking at the printer top down)
                  ;             0.0-----0.1
                  ;              |  0.2  |
                  ;              |-------|
                  ;              |0.3|0.4|
                  ;               ---+---
                  ;                Front
                  ;  Driver 0.1 & 0.2 is for the CoreXY motion, 0.2-0.4 is for the bed kinematics.
                  

                  Example 1:
                  Adjustments needed after probing:

                  • Driver 0.2 = -0.5mm
                  • Driver 0.3 = -0.2mm
                  • Driver 0.4 = +0.9mm

                  To avoid potential nozzle craches RRF will move the driver/axis that needs to adjust TOWARDS the nozzle last, and the driver/axis that needs to move the most AWAY from the nozzle first:

                  1. Lower driver 0.4 by 0.9mm.
                  2. Raise driver 0.3 by 0.2mm.
                  3. Raise driver 0.2 by 0.5mm.

                  This should both put the least mechanical strain on the bed (depending on how the bed is built ofc.), and it would provide maximal clearance to the nozzle.

                  Example 2:
                  Adjustments needed after probing:

                  • Driver 0.2 = +3.7mm
                  • Driver 0.3 = -0.3mm
                  • Driver 0.4 = +1.1mm

                  Adjustment order:

                  1. Lower driver 0.2 by 3.7mm.
                  2. Lower driver 0.4 by 1.1mm.
                  3. Raise driver 0.3 by 0.3mm.
                  dc42undefined gloomyandyundefined 2 Replies Last reply Reply Quote 1
                  • dc42undefined
                    dc42 administrators @Exerqtor
                    last edited by

                    @Exerqtor that's a good idea.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    1 Reply Last reply Reply Quote 1
                    • gloomyandyundefined
                      gloomyandy @Exerqtor
                      last edited by

                      @Exerqtor said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                      To avoid potential nozzle craches RRF will move the axis the driver/axis that needs to adjust TOWARDS the nozzle last, and the driver/axis that needs to move the most AWAY from the nozzle first:

                      Yes that's what I was suggesting with:

                      @gloomyandy said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                      Possible mitigating actions: Perform any negative (moving the bed away from the nozzle) moves first

                      Exerqtorundefined 1 Reply Last reply Reply Quote 1
                      • Exerqtorundefined
                        Exerqtor @gloomyandy
                        last edited by

                        @dc42 Got any builds I/we could test incorporating this commit?

                        dc42undefined 1 Reply Last reply Reply Quote 0
                        • dc42undefined
                          dc42 administrators @Exerqtor
                          last edited by

                          @Exerqtor yes, is this for D3 Mini or another board?

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                          Exerqtorundefined 1 Reply Last reply Reply Quote 0
                          • Exerqtorundefined
                            Exerqtor @dc42
                            last edited by

                            @dc42 said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                            @Exerqtor yes, is this for D3 Mini or another board?

                            Yes in my case it's for a D3 mini at least ☺️

                            dc42undefined 1 Reply Last reply Reply Quote 0
                            • dc42undefined
                              dc42 administrators @Exerqtor
                              last edited by dc42

                              I've put new RRF builds at https://www.dropbox.com/scl/fo/yc7mnauicu5vqw6yegeq7/AKnV4j8k1MCADG4VE4EIG6Y?rlkey=skjxh23i9c953yvxm2tb8qr36&dl=0. Some notes:

                              • The issue with bed tramming might be fixed. I don't have a suitable machine to test it on.
                              • Scanning Z probes are fixed (they didn't work in previous 3.6.0 alpha releases)
                              • Also included are 3.6.0 alpha versions of some expansion board firmware (not EXP1HCL or M23CL). You can revert to 3.5.2 versions if you have any issues with them.

                              See https://github.com/Duet3D/RepRapFirmware/wiki/Changelog-RRF-3.x-Beta#reprapfirmware-360-beta1-in-preparation for more details.

                              Duet WiFi hardware designer and firmware engineer
                              Please do not ask me for Duet support via PM or email, use the forum
                              http://www.escher3d.com, https://miscsolutions.wordpress.com

                              edspedundefined o_lampeundefined 3 Replies Last reply Reply Quote 3
                              • edspedundefined
                                edsped @dc42
                                last edited by

                                @dc42 Still seeing accumulation on one of the leadscrews so I'm hesitant to test...
                                812faa74-af2f-4803-8dd3-a9aee5c65cff-image.png

                                dc42undefined 1 Reply Last reply Reply Quote 0
                                • edspedundefined
                                  edsped @dc42
                                  last edited by

                                  @dc42 Same iterations on 3.5.2
                                  874007a2-054d-4595-8065-335a6bd4d14f-image.png

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                                  • o_lampeundefined
                                    o_lampe @dc42
                                    last edited by

                                    @dc42 said in Z-axis / tramming issues with 3.6.0-alpha2+3:

                                    The issue with bed tramming might be fixed. I don't have a suitable machine to test it on.

                                    IIRC, the problem was also seen on a Delta printer...that's why I hesitate to test 3.6.a+

                                    dc42undefined 1 Reply Last reply Reply Quote 0
                                    • dc42undefined
                                      dc42 administrators @o_lampe
                                      last edited by

                                      @o_lampe no this issue does not affect deltas.

                                      Duet WiFi hardware designer and firmware engineer
                                      Please do not ask me for Duet support via PM or email, use the forum
                                      http://www.escher3d.com, https://miscsolutions.wordpress.com

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                                      • dc42undefined
                                        dc42 administrators @edsped
                                        last edited by

                                        @edsped thanks, looks like it's adjusting the 3rd leadscrew the wrong way on the second and subsequent iterations.

                                        Duet WiFi hardware designer and firmware engineer
                                        Please do not ask me for Duet support via PM or email, use the forum
                                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                                        dc42undefined 1 Reply Last reply Reply Quote 1
                                        • dc42undefined
                                          dc42 administrators @dc42
                                          last edited by

                                          I have now reproduced and fixed this issue. I've prepared a new alpha release which I hope to make available tomorrow after some internal testing.

                                          Duet WiFi hardware designer and firmware engineer
                                          Please do not ask me for Duet support via PM or email, use the forum
                                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                                          Exerqtorundefined edspedundefined 2 Replies Last reply Reply Quote 2
                                          • Exerqtorundefined
                                            Exerqtor @dc42
                                            last edited by

                                            @dc42 Sweet, i just saw the commits and was about to ask for a build, but i'll wait til you've done the internal one 😃

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