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RepRapFirmware 3.6.0-alpha.2 for Duet main boards available

Scheduled Pinned Locked Moved
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  • undefined
    balajiramani @dc42
    last edited by balajiramani 14 Aug 2024, 13:25

    @dc42 Here is a video that shows the crash - https://forum.duet3d.com/assets/uploads/files/1721977512327-pxl_20240726_065615215-2.mp4. The motion from from one probe point to the other is more of a 'U' shaped travel, instead of a straight line.

    Let me know if you need any other information.

    Here is bed.g file.

    M561 ; clear any bed transform, otherwise homing may be at the wrong height
    M290 R0 S0 ; Remove any baby stepping
    ; bed.g file for RepRapFirmware, generated by Escher3D calculator
    ; 16 points, 4 factors, probing radius: 150, probe offset (0, 0)
    ; If the printer hasn't been homed, home it
    if !move.axes[0].homed || !move.axes[1].homed || !move.axes[2].homed
    G28
    ; Probe the bed and do auto calibration
    G1 X0 Y0 Z10 F10000 ; go to just above the first probe point
    while true
    if iterations = 5
    abort "Too many auto calibration attempts"
    G30 P0 X0.00 Y150.00 Z-99999 H0
    if result != 0
    continue
    G30 P1 X96.42 Y114.91 Z-99999 H0
    if result != 0
    continue
    G30 P2 X147.72 Y26.05 Z-99999 H0
    if result != 0
    continue
    G30 P3 X129.90 Y-75.00 Z-99999 H0
    if result != 0
    continue
    G30 P4 X51.30 Y-140.95 Z-99999 H0
    if result != 0
    continue
    G30 P5 X-51.30 Y-140.95 Z-99999 H0
    if result != 0
    continue
    G30 P6 X-129.90 Y-75.00 Z-99999 H0
    if result != 0
    continue
    G30 P7 X-147.72 Y26.05 Z-99999 H0
    if result != 0
    continue
    G30 P8 X-96.42 Y114.91 Z-99999 H0
    if result != 0
    continue
    G30 P9 X0.00 Y75.00 Z-99999 H0
    if result != 0
    continue
    G30 P10 X64.95 Y37.50 Z-99999 H0
    if result != 0
    continue
    G30 P11 X64.95 Y-37.50 Z-99999 H0
    if result != 0
    continue
    G30 P12 X0.00 Y-75.00 Z-99999 H0
    if result != 0
    continue
    G30 P13 X-64.95 Y-37.50 Z-99999 H0
    if result != 0
    continue
    G30 P14 X-64.95 Y37.50 Z-99999 H0
    if result != 0
    continue
    G30 P15 X0 Y0 Z-99999 S6
    if result != 0
    continue
    if move.calibration.initial.deviation <= 0.03
    break
    echo "Repeating calibration because deviation is too high (" ^ move.calibration.initial.deviation ^ "mm)"
    ; end loop
    echo "Auto calibration successful, deviation", move.calibration.final.deviation ^ "mm"
    undefined 1 Reply Last reply 14 Aug 2024, 13:28 Reply Quote 0
    • undefined
      dc42 administrators @balajiramani
      last edited by 14 Aug 2024, 13:28

      @balajiramani it sounds to me that segmentation is not working on those moves. If you send M669 without parameters, what does it report?

      Duet WiFi hardware designer and firmware engineer
      Please do not ask me for Duet support via PM or email, use the forum
      http://www.escher3d.com, https://miscsolutions.wordpress.com

      undefined 1 Reply Last reply 14 Aug 2024, 14:12 Reply Quote 0
      • undefined
        balajiramani @dc42
        last edited by 14 Aug 2024, 14:12

        @dc42 Here is what I see:

        M669
        Kinematics is Linear delta, 100 segments/sec, min. segment length 0.20mm
        undefined 1 Reply Last reply 14 Aug 2024, 16:06 Reply Quote 0
        • undefined
          Exerqtor @balajiramani
          last edited by Exerqtor 14 Aug 2024, 16:06

          @dc42 Just had time to TRY a print with the alpha.4 binaries you uploaded the other day (on both the D3 Mini & the 1LC), and the bed leveling seems to be working.

          BUT now the extruder won't extrude (or retract for that matter), either through G-code or if I to use the "extrude buttons" in DWC & PD.

          When I canceled the print on PD i got these error messages:

          CAN response timeout: board 121, req type 6044, RID 220.
          Error: at column 2: G10: hA
          CAN response timeout: board 121, req type 6029, RID 222
          CAN response timeout: board 121, req type 6044, RID 223

          Which is new behaviour from alpha.2+3.

          AND the hotend heater (connected to the 1LC) won't turn off. Both DWC & PD show active/standby heat to be 0, but the heater is still at working temp (255c).
          If i manually try to input 0 in active on DWC and push enter i get this error:

          M568 P0 S0
          Error: at column 2: M568: P

          The only way I've found to actually make it turn off/adjust the temp down is to power toggle or restart the printer.

          undefined undefined 2 Replies Last reply 14 Aug 2024, 16:13 Reply Quote 0
          • undefined
            gloomyandy @Exerqtor
            last edited by 14 Aug 2024, 16:13

            @Exerqtor What version of the firmware do you have installed on the 1LC?

            1 Reply Last reply Reply Quote 0
            • undefined
              Exerqtor @Exerqtor
              last edited by Exerqtor 14 Aug 2024, 16:17

              @gloomyandy said in RepRapFirmware 3.6.0-alpha.2 for Duet main boards available:

              @Exerqtor What version of the firmware do you have installed on the 1LC?

              @Exerqtor said in RepRapFirmware 3.6.0-alpha.2 for Duet main boards available:

              @dc42 Just had time to TRY a print with the alpha.4 binaries you uploaded the other day (on both the D3 Mini & the 1LC), and the bed leveling seems to be working.

              To be more specific:

              M122 B121
              Diagnostics for board 121:
              Duet TOOL1LC rev 1.1 or later firmware version 3.6.0-alpha.4 (2024-08-13 12:30:07)
              Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25)

              I just tested if the extrusion works while idle, which it does. I'm about to start a new test print (same job g-code as earlier) and see what happens.

              Here is a couple M122's from BEFORE starting the print:

              M122
              === Diagnostics ===
              RepRapFirmware for Duet 3 Mini 5+ version 3.6.0-alpha.4 (2024-08-13 15:11:57) running on Duet 3 Mini5plus WiFi (standalone mode)
              Board ID: XNHXF-HR6KL-K65J0-409N2-K9W1Z-RV2MZ
              Used output buffers: 16 of 40 (37 max)
              === RTOS ===
              Static ram: 92296
              Dynamic ram: 94544 of which 0 recycled
              Never used RAM 50316, free system stack 142 words
              Tasks: NETWORK(2,nWait 7,16.7%,211) HEAT(3,nWait 6,0.0%,350) Move(4,nWait 6,0.0%,247) TMC(4,nWait 6,0.9%,65) CanReceiv(6,nWait 1,0.1%,792) CanSender(5,nWait 7,0.0%,336) CanClock(7,delaying,0.0%,339) MAIN(1,running,80.5%,665) IDLE(0,ready,1.1%,29) AIN(4,delaying,0.8%,259), total 100.0%
              Owned mutexes: WiFi(NETWORK)
              === Platform ===
              Last reset 00:17:06 ago, cause: software
              Last software reset at 2024-08-14 18:13, reason: User, Gcodes spinning, available RAM 52872, slot 2
              Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
              Error status: 0x00
              Aux0 errors 0,1,0
              MCU temperature: min 41.0, current 44.0, max 46.0
              Supply voltage: min 2.8, current 24.2, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
              Heap OK, handles allocated/used 99/34, heap memory allocated/used/recyclable 2048/696/252, gc cycles 232
              Events: 0 queued, 0 completed
              Date/time: 2024-08-14 18:30:13
              Slowest loop: 49.66ms; fastest: 0.11ms
              === Storage ===
              Free file entries: 18
              SD card 0 detected, interface speed: 22.5MBytes/sec
              SD card longest read time 8.0ms, write time 9.5ms, max retries 0
              === Move ===
              Segments created 33, maxWait 232923ms, bed comp in use: none, height map offset 0.000, hiccups added 0 (0.00ms), max steps late 0, ebfmin 0.00, ebfmax 0.00, mcet 0.012
              Pos req/act/dcf: 10.00/10/0.00 -27991.00/-27991/0.00 4000.00/4000/0.00
              no step interrupt scheduled
              Driver 0: standstill, SG min 0, read errors 0, write errors 0, ifcnt 38, reads 53987, writes 38, timeouts 0, DMA errors 0, CC errors 0
              Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 38, reads 53987, writes 38, timeouts 0, DMA errors 0, CC errors 0
              Driver 2: standstill, SG min 0, read errors 0, write errors 0, ifcnt 24, reads 54001, writes 24, timeouts 0, DMA errors 0, CC errors 0
              Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 23, reads 54001, writes 23, timeouts 0, DMA errors 0, CC errors 0
              Driver 4: standstill, SG min 0, read errors 0, write errors 0, ifcnt 23, reads 54002, writes 23, timeouts 0, DMA errors 0, CC errors 0
              Driver 5: not present
              Driver 6: not present
              === DDARing 0 ===
              Scheduled moves 63, completed 63, LaErrors 0, Underruns [0, 0, 0]
              === DDARing 1 ===
              Scheduled moves 0, completed 0, LaErrors 0, Underruns [0, 0, 0]
              === Heat ===
              Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
              Heater 0 is on, I-accum = 0.5
              Heater 1 is on, I-accum = 0.0
              === GCodes ===
              Movement locks held by null, null
              HTTP is idle in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon is doing "G4 P250" in state(s) 0 0, running macro
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              File2 is idle in state(s) 0
              Queue2 is idle in state(s) 0
              Q0 segments left 0, axes/extruders owned 0x0000803
              Code queue 0 is empty
              Q1 segments left 0, axes/extruders owned 0x0000000
              Code queue 1 is empty
              === Filament sensors ===
              check 0 clear 0
              Extruder 0 sensor: no filament
              === CAN ===
              Messages queued 9333, received 21187, lost 0, ignored 0, errs 1318, boc 0
              Longest wait 6ms for reply type 6024, peak Tx sync delay 10502, free buffers 26 (min 25), ts 5135/5133/0
              Tx timeouts 0,0,1,0,0,0 last cancelled message type 30 dest 127
              === Network ===
              Slowest loop: 19.26ms; fastest: 0.00ms
              Responder states: MQTT(0) HTTP(2) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
              HTTP sessions: 1 of 8
              === WiFi ===
              Interface state: active
              Module is connected to access point
              Failed messages: pending 0, notrdy 0, noresp 0
              Firmware version 2.1.0
              MAC address c4:5b:be:ce:91:93
              Module reset reason: Power up, Vcc 3.38, flash size 2097152, free heap 39620
              WiFi IP address 192.168.30.50
              Signal strength -48dBm, channel 6, mode 802.11n, reconnections 0
              Clock register 00002001
              Socket states: 0 0 0 0 0 0 0 0
              M122 B121
              Diagnostics for board 121:
              Duet TOOL1LC rev 1.1 or later firmware version 3.6.0-alpha.4 (2024-08-13 12:30:07)
              Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25)
              All averaging filters OK
              Never used RAM 7956, free system stack 92 words
              Tasks: Move(3,nWait 7,0.0%,100) TMC(2,delaying,3.6%,52) HEAT(2,nWait 6,0.4%,98) CanAsync(5,nWait 4,0.0%,54) CanRecv(3,nWait 1,0.0%,70) CanClock(5,nWait 1,0.0%,58) ACCEL(3,nWait 6,0.0%,52) MAIN(1,running,91.0%,318) IDLE(0,ready,0.0%,26) AIN(2,delaying,5.0%,112), total 100.0%
              Owned mutexes:
              Last reset 00:17:09 ago, cause: power up
              Last software reset at 2024-03-12 16:55, reason: StackOverflow, available RAM 2968, slot 0
              Software reset code 0x0100 ICSR 0x0042600e SP 0x20007f34 Task Move Freestk 3342 ok
              Stack: 20004a80 20004ab4 0001cf33 20004c98 20004938 00000000 0001c011 20003320 fffffffd a5a5a5a5 00000000 20007f8c 00000000 20007f8c 0001cc97 00000000 200017c4 20001748 0001c4d7 20001748 200017c4 00000032 454c4449 00022700 0001ac77 200018e0 200018e0
              Driver 0: pos 34130, 568.8 steps/mm, standstill, SG min 0, read errors 0, write errors 0, ifcnt 14, reads 37260, writes 3, timeouts 0, DMA errors 0, CC errors 0
              Moves scheduled 4, hiccups 0 (0.00ms), segs 3, step errors 0 (types 0x0), maxLate 0 maxPrep 96, ebfmin 0.00 max 0.00
              Peak sync jitter -2/9, peak Rx sync delay 222, resyncs 0/0, no timer interrupt scheduled, next step interrupt due in 3857541807 ticks, disabled
              VIN voltage: min 23.8, current 24.7, max 25.2
              MCU temperature: min 60.4C, current 64.1C, max 65.5C
              Last sensors broadcast 0x00000012 found 2 165 ticks ago, 0 ordering errs, loop time 0
              CAN messages queued 15059, send timeouts 0, received 6624, lost 0, ignored 0, errs 0, boc 0, free buffers 18, min 18, error reg 0
              dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 294, adv 37049/37148
              Accelerometer: LIS3DH, status: 00
              I2C bus errors 0, naks 0, contentions 0, other errors 0
              === Filament sensors ===
              Interrupt 5726621 to 0us, poll 5 to 1268us
              Driver 0: ok

              EDIT:

              I've got no idea what was going on earlier, because now it extrudes like it should 😶
              I'm letting the test print finish to see what's going to happen.

              1 Reply Last reply Reply Quote 0
              • undefined
                DonStauffer @dc42
                last edited by DonStauffer 16 Aug 2024, 01:47

                @dc42 I didn't try it and I reverted to alpha 2. It's called from the last few lines in config.g so I didn't think it would be different.

                I reinstalled alpha 4 and yes, the error occurs on the M260 lines when the macro is invoked from the console using M98.

                undefined 1 Reply Last reply 16 Aug 2024, 06:55 Reply Quote 0
                • undefined
                  dc42 administrators @DonStauffer
                  last edited by 16 Aug 2024, 06:55

                  @DonStauffer my apologies, I accidentally disabled M260 in that build. I will reinstate it in the next build. Meanwhile, M260.0 should do what you want in alpha 4.

                  Duet WiFi hardware designer and firmware engineer
                  Please do not ask me for Duet support via PM or email, use the forum
                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                  undefined 2 Replies Last reply 18 Aug 2024, 15:58 Reply Quote 0
                  • undefined
                    edsped
                    last edited by 16 Aug 2024, 11:23

                    Am I the only one having connection interrupted errors with the most recent build? I'm hard wired into a Ubiquiti network if that matters.

                    Bed leveling is working as intended.

                    Controller MB6HC using built in wired network.
                    Jubilee toolchanger with (4) RRF-36's running the tools.

                    M12 after a few "Connection Interrupted" errors

                    m122
                    === Diagnostics ===
                    RepRapFirmware for Duet 3 MB6HC version 3.6.0-alpha.4 (2024-08-13 15:11:47) running on Duet 3 MB6HC v1.02 or 1.02a (standalone mode)
                    Board ID: 08DJM-9P63L-DJ3T8-6J1F2-3SS6J-KA6VB
                    Used output buffers: 1 of 40 (38 max)
                    === RTOS ===
                    Static ram: 133840
                    Dynamic ram: 128256 of which 128 recycled
                    Never used RAM 57328, free system stack 103 words
                    Tasks: NETWORK(1,ready,35.9%,182) ETHERNET(5,nWait 7,0.1%,311) HEAT(3,nWait 6,0.0%,323) Move(4,nWait 6,0.3%,209) TMC(4,nWait 6,8.5%,53) CanReceiv(6,nWait 1,0.1%,767) CanSender(5,nWait 7,0.0%,327) CanClock(7,delaying,0.0%,348) MAIN(1,running,55.0%,103) IDLE(0,ready,0.0%,29), total 100.0%
                    Owned mutexes:
                    === Platform ===
                    Last reset 00:39:59 ago, cause: power up
                    Last software reset at 2024-08-02 12:23, reason: User, Gcodes spinning, available RAM 62628, slot 1
                    Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a000 BFAR 0x00000000 SP 0x00000000 Task MAIN Freestk 0 n/a
                    Error status: 0x00
                    Aux0 errors 0,0,0
                    MCU temperature: min 10.7, current 31.1, max 31.4
                    Supply voltage: min 24.0, current 24.1, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
                    12V rail voltage: min 12.0, current 12.2, max 12.5, under voltage events: 0
                    Heap OK, handles allocated/used 99/4, heap memory allocated/used/recyclable 2048/312/264, gc cycles 0
                    Events: 0 queued, 0 completed
                    Date/time: 2024-08-16 07:22:24
                    Slowest loop: 224.31ms; fastest: 0.05ms
                    === Storage ===
                    Free file entries: 19
                    SD card 0 detected, interface speed: 25.0MBytes/sec
                    SD card longest read time 3.0ms, write time 4.8ms, max retries 0
                    === Move ===
                    Segments created 381, maxWait 819860ms, bed comp in use: mesh, height map offset 0.000, hiccups added 0 (0.00ms), max steps late 1, ebfmin 0.00, ebfmax 0.00, mcet 0.087
                    Pos req/act/dcf: 58485.00/66365/-0.04 15858.00/15858/0.04 1934.00/1938/-0.97 0.00/0/0.00
                    next step interrupt due in 1 ticks, disabled
                    Driver 0: ok, SG min 0, mspos 327, reads 49227, writes 26 timeouts 0
                    Driver 1: standstill, SG min 0, mspos 276, reads 49227, writes 26 timeouts 0
                    Driver 2: standstill, SG min 0, mspos 352, reads 49231, writes 22 timeouts 0
                    Driver 3: ok, SG min 0, mspos 1007, reads 49228, writes 26 timeouts 0
                    Driver 4: ok, SG min 0, mspos 255, reads 49228, writes 26 timeouts 0
                    Driver 5: ok, SG min 0, mspos 271, reads 49228, writes 26 timeouts 0
                    === DDARing 0 ===
                    Scheduled moves 18403, completed 18344, LaErrors 0, Underruns [0, 0, 0]
                    === DDARing 1 ===
                    Scheduled moves 0, completed 0, LaErrors 0, Underruns [0, 0, 0]
                    === Heat ===
                    Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                    Heater 0 is on, I-accum = 0.2
                    Heater 1 is on, I-accum = 0.0
                    === GCodes ===
                    Movement locks held by null, null
                    HTTP is idle in state(s) 0
                    Telnet is idle in state(s) 0
                    File is idle in state(s) 3
                    USB is idle in state(s) 0
                    Aux is idle in state(s) 0
                    Trigger is idle in state(s) 0
                    Queue is idle in state(s) 0
                    LCD is idle in state(s) 0
                    SBC is idle in state(s) 0
                    Daemon is idle in state(s) 0
                    Aux2 is idle in state(s) 0
                    Autopause is idle in state(s) 0
                    File2 is idle in state(s) 0
                    Queue2 is idle in state(s) 0
                    Q0 segments left 11, axes/extruders owned 0x80000007
                    Code queue 0 is empty
                    Q1 segments left 0, axes/extruders owned 0x0000000
                    Code queue 1 is empty
                    === CAN ===
                    Messages queued 39620, received 192185, lost 0, ignored 0, errs 791, boc 0
                    Longest wait 2ms for reply type 6031, peak Tx sync delay 61333, free buffers 50 (min 49), ts 11997/11996/0
                    Tx timeouts 0,0,0,0,0,0
                    === Network ===
                    Slowest loop: 193.94ms; fastest: 0.03ms
                    Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
                    HTTP sessions: 2 of 8
                    = Ethernet =
                    Interface state: active
                    Error counts: 0 0 0 1 0 0
                    Socket states: 5 2 2 2 2 0 0 0
                    === WiFi ===
                    Interface state: disabled
                    Module is disabled
                    Failed messages: pending 0, notrdy 0, noresp 0
                    Socket states: 0 0 0 0 0 0 0 0
                    === Multicast handler ===
                    Responder is inactive, messages received 0, responses 0
                    undefined 1 Reply Last reply 16 Aug 2024, 12:52 Reply Quote 0
                    • undefined
                      edsped @edsped
                      last edited by 16 Aug 2024, 12:52

                      @edsped said in RepRapFirmware 3.6.0-alpha.2 for Duet main boards available:

                      Tasks: NETWORK(1,ready,35.9%,182) ETHERNET(5,nWait 7,0.1%,311) HEAT(3,nWait 6,0.0%,323) Move(4,nWait 6,0.3%,209) TMC(4,nWait 6,8.5%,53) CanReceiv(6,nWait 1,0.1%,767) CanSender(5,nWait 7,0.0%,327) CanClock(7,delaying,0.0%,348) MAIN(1,running,55.0%,103) IDLE(0,ready,0.0%,29), total 100.0%

                      Not sure what's going on, I reverted back to 3.5.2 and the dropped connection persists.. All works well using the paneldue but the web interface is all but unusable and sometimes I'm unable to reconnect for several minutes. Not sure what got hosed but something is surely borked.

                      undefined 1 Reply Last reply 16 Aug 2024, 13:51 Reply Quote 0
                      • undefined
                        dc42 administrators @edsped
                        last edited by dc42 16 Aug 2024, 13:51

                        @edsped I see connection errors too. Do your connections errors go away if you put the PanelDue on the Setup page so that it stops polling the 6HC?

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        undefined 3 Replies Last reply 16 Aug 2024, 14:05 Reply Quote 0
                        • undefined
                          edsped @dc42
                          last edited by 16 Aug 2024, 14:05

                          @dc42 I'm working through it now. Some of my issues appear to be related to running the Jubilee on an IOT network... I've had ongoing connection issues with the paneldue and leave it disconnected unless I have issues with the web interface. I'll follow up once I get my network in order and run a few tests.

                          1 Reply Last reply Reply Quote 0
                          • undefined
                            edsped @dc42
                            last edited by 16 Aug 2024, 14:54

                            @dc42 Still getting connection errors. Paneldue is disconnected FWIW.

                            1 Reply Last reply Reply Quote 0
                            • undefined
                              edsped @dc42
                              last edited by 17 Aug 2024, 00:55

                              @dc42 Did a fair amount of reworking of my network and I'm 45 minutes into a print without a disconnect... I believe my issue was more networking than the alpha firmware. Next try, running DWC and the Paneldue together.

                              1 Reply Last reply Reply Quote 0
                              • undefined
                                DonStauffer @dc42
                                last edited by 18 Aug 2024, 15:58

                                @dc42 Thanks for the information.

                                1 Reply Last reply Reply Quote 0
                                • undefined
                                  balajiramani
                                  last edited by 18 Aug 2024, 16:36

                                  Hi am seeing a new error today. A few minutes into a print, the printer stopped with the following error:

                                  Error: Movement halted because a step timing error occurred (code 3). Please reset the controller.

                                  Here is the output of M122 after that:

                                  8/18/2024, 5:05:27 PM M122
                                  === Diagnostics ===
                                  RepRapFirmware for Duet 2 WiFi/Ethernet version 3.6.0-alpha.4 (2024-08-13 15:11:39) running on Duet WiFi 1.0 or 1.01
                                  Board ID: 08DAM-999TL-MQ4SD-6JTDL-3SS6N-968BX
                                  Used output buffers: 12 of 26 (21 max)
                                  === RTOS ===
                                  Static ram: 23368
                                  Dynamic ram: 66976 of which 12 recycled
                                  Never used RAM 16440, free system stack 112 words
                                  Tasks: NETWORK(2,nWait 6,15.9%,195) HEAT(3,nWait 5,0.1%,328) Move(4,invalid,1.1%,272) MAIN(1,running,82.9%,744) IDLE(0,ready,0.0%,29), total 100.0%
                                  Owned mutexes: WiFi(NETWORK)
                                  === Platform ===
                                  Last reset 01:00:54 ago, cause: power up
                                  Last software reset at 2024-08-09 19:04, reason: User, Gcodes spinning, available RAM 13844, slot 2
                                  Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                                  Error status: 0x00
                                  Aux0 errors 0,0,0
                                  MCU temperature: min 38.2, current 46.3, max 49.1
                                  Supply voltage: min 23.5, current 24.2, max 24.6, under voltage events: 0, over voltage events: 0, power good: yes
                                  Heap OK, handles allocated/used 99/3, heap memory allocated/used/recyclable 2048/1184/1096, gc cycles 1
                                  Events: 0 queued, 0 completed
                                  Date/time: 2024-08-18 17:05:26
                                  Slowest loop: 226.73ms; fastest: 0.13ms
                                  I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                                  === Storage ===
                                  Free file entries: 8
                                  SD card 0 detected, interface speed: 20.0MBytes/sec
                                  SD card longest read time 6.2ms, write time 4.3ms, max retries 0
                                  === Move ===
                                  Segments created 470, maxWait 2498505ms, bed comp in use: none, height map offset 0.000, hiccups added 1 (0.03ms), max steps late 0, ebfmin 0.00, ebfmax 0.00, mcet 0.085
                                  Pos req/act/dcf: 68507.00/68479/0.99 65547.00/65566/-0.81 65391.00/65409/-0.99
                                  no step interrupt scheduled
                                  Driver 0: standstill, SG min 0
                                  Driver 1: standstill, SG min 0
                                  Driver 2: standstill, SG min 0
                                  Driver 3: standstill, SG min 0
                                  Driver 4: standstill, SG min n/a
                                  Driver 5:
                                  Driver 6:
                                  Driver 7:
                                  Driver 8:
                                  Driver 9:
                                  Driver 10:
                                  Driver 11:
                                  === DDARing 0 ===
                                  Scheduled moves 69133, completed 69131, LaErrors 0, Underruns [0, 0, 0]
                                  === Heat ===
                                  Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                                  Heater 0 is on, I-accum = 0.0
                                  Heater 1 is on, I-accum = 0.2
                                  === GCodes ===
                                  Movement locks held by null
                                  HTTP is idle in state(s) 0
                                  Telnet is idle in state(s) 0
                                  File is doing "G1 X-13.401 Y-8.549" in state(s) 0
                                  USB is idle in state(s) 0
                                  Aux is idle in state(s) 0
                                  Trigger is idle in state(s) 0
                                  Queue is idle in state(s) 0
                                  LCD is idle in state(s) 0
                                  Daemon is idle in state(s) 0
                                  Autopause is idle in state(s) 0
                                  Q0 segments left 1
                                  Code queue 0 is empty
                                  === Network ===
                                  Slowest loop: 208.96ms; fastest: 0.00ms
                                  Responder states: HTTP(4) HTTP(0) HTTP(0) FTP(0) Telnet(0)
                                  HTTP sessions: 1 of 8
                                  === WiFi ===
                                  Interface state: active
                                  Module is connected to access point
                                  Failed messages: pending 0, notrdy 0, noresp 0
                                  Firmware version 2.1.0
                                  MAC address 5c:cf:7f:2c:25:00
                                  Module reset reason: Turned on by main processor, Vcc 3.40, flash size 4194304, free heap 40988
                                  WiFi IP address 192.168.1.61
                                  Signal strength -36dBm, channel 6, mode 802.11n, reconnections 0
                                  Clock register 00002002
                                  Socket states: 0 0 0 0 0 0 0 0
                                  undefined 1 Reply Last reply 18 Aug 2024, 16:46 Reply Quote 0
                                  • undefined
                                    dc42 administrators @balajiramani
                                    last edited by 18 Aug 2024, 16:46

                                    @balajiramani please share the GCode file that provoked that message and your config.g file.

                                    Duet WiFi hardware designer and firmware engineer
                                    Please do not ask me for Duet support via PM or email, use the forum
                                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                                    undefined 1 Reply Last reply 19 Aug 2024, 12:27 Reply Quote 0
                                    • undefined
                                      balajiramani @dc42
                                      last edited by 19 Aug 2024, 12:27

                                      @dc42 Here is the gcode - Uno_CNC_Back_0.2mm_PLA_BigDelta_28m.gcode

                                      Here is config.g

                                      ; Setup some global variables
                                      global power_fail_retract = 2 ; Retract 2mm when power fails
                                      ; Communication and general
                                      M550 P"BigDelta" ; Machine name and Netbios name (can be anything you like)
                                      M551 Preprap ; Machine password (used for FTP)
                                      M552 S1 ; Enable WiFi. Disabled for setup and testing. Enable once set up on your network.
                                      ; Enable telnet
                                      M586 S1 P2
                                      ; Debugging
                                      M111 S0 ; Debug off
                                      M929 P"eventlog.txt" S1 ; Start logging to file eventlog.txt
                                      M555 P2 ; Set output to look like Marlin
                                      G21 ; Work in millimetres
                                      G90 ; Send absolute coordinates...
                                      M83 ; ...but relative extruder moves
                                      ; Axis and motor configuration
                                      M569 P0 S0 ; Drive 0 goes backwards
                                      M569 P1 S0 ; Drive 1 goes backwards
                                      M569 P2 S0 ; Drive 2 goes backwards
                                      M569 P3 S0 ; Drive 3 goes backwards
                                      ; Assign extruder drive
                                      M584 E3
                                      ; Set homing switch config
                                      M574 X2 S1 P"!xstop" ; Set homing switch configuration on S1 = high-end, active-low
                                      M574 Y2 S1 P"!ystop" ; Set homing switch configuration on S1 = high-end, active-low
                                      M574 Z2 S1 P"!zstop" ; Set homing switch configuration on S1 = high-end, active-low
                                      ; Set it as a linear delta
                                      M669 K3
                                      ; Setup paneldue 5i
                                      M575 P1 S1 B57600
                                      M665 R215.062 L395.317:395.475:395.433 B160 H374.050 ; set delta radius, diagonal rod length, printable radius and homed height
                                      M666 X0 Y0 Z0 ; put your endstop adjustments here, or let auto calibration find them
                                      M350 X16 Y16 Z16 E16 I1 ; Set 16x microstepping with interpolation
                                      M92 X200 Y200 Z200 ; Set axis steps/mm
                                      M906 X1400 Y1400 Z1400 E1400 I60 ; Set motor currents (mA) and increase idle current to 60%
                                      M84 S60 ; Set idle timeout
                                      M201 X12000 Y12000 Z2000 E10000 ; Accelerations (mm/s^2)
                                      M203 X30000 Y30000 Z5000 E3600 ; Maximum speeds (mm/min)
                                      ;M566 X900 Y900 Z300 E1200 P1 ; Maximum instant speed changes mm/minute
                                      ;M566 X300 Y300 Z300 E450 P1 ; Maximum instant speed changes mm/minute
                                      M566 X600 Y600 Z300 E900 P1 ; Maximum instant speed changes mm/minute
                                      M204 P9000 T9000 ; Set acceleration for print and travel moves
                                      ; Configure Input shaping
                                      M593 P"zvdd" F45
                                      ; Thermistors
                                      M308 S0 P"bed_temp" Y"thermistor" T100000 B3950 R4700 H30 L0 ; Put your own H and/or L values here to set the bed thermistor ADC correction
                                      M308 S1 P"e0_temp" Y"thermistor" T100000 B3950 R4700 H30 L0 ; 100K NTC
                                      ;M308 S1 P"e0_temp" Y"thermistor" T100000 B4658 C6.5338987554e-08 ; 104-NT Aliexpress thermistor
                                      M950 H0 C"bed_heat" T0 ; Set up H0 as the bed heater using T0 as the sensor
                                      M950 H1 C"e0_heat" T1 ; Set up H1 as the extruder heater using T1 as the sensor
                                      M140 H0 ; Map H0 as the bed heater
                                      ; Set temperature excursion warnings
                                      M570 H0 P20
                                      M570 H1 P20
                                      M308 S3 Y"mcu-temp" A"MCU" ; configure sensor 3 as thermistor on pin e1temp for left stepper
                                      M308 S4 Y"drivers" A"Drivers" ; configure sensor 4 as temperature warning and overheat flags on the TMC2660 on Duet
                                      M912 P0 S-3.5 ; Calibrate MCU temp
                                      ; Fan definitions
                                      M950 F0 C"fan0"
                                      M950 F1 C"fan1"
                                      M950 F2 C"fan2"
                                      ; Thermostatic fan on 1 for cooling the hotend
                                      M106 P1 T50 H1
                                      ; Thermostatic fan on 2 for cooling the board
                                      M106 P2 H3:4 L.3 X1 B0.3 T35:70 ; set fan 2 value
                                      ; Tool definitions
                                      M563 P0 D0 H1 ; Define tool 0
                                      G10 P0 S0 R0 ; Set tool 0 operating and standby temperatures
                                      ;M92 E1392 ; Based on https://www.thingiverse.com/thing:1359717; 2023/01/06
                                      M92 E1077.1646 ; This is the new value for the hobb-goblin extruder. 03/07/2023
                                      ;M92 E319.2005 ; Set extruder steps per mm. This is for the MK8 gear
                                      ; Z probe and compensation definition
                                      M558 P8 C"^!zprobe.in" R0.4 H4 F1200 T6000 A5 S0.01 ; Z probe is a piezo sensor
                                      G31 X0 Y0 Z-0.08 P100 ; Set the zprobe height and threshold
                                      M557 R150 S20 ; Probe within a radius of 150mm and mesh spacing of 20
                                      M376 H5 ; Taper off bed compensation after 5mm
                                      ; Configure power failure and resume
                                      M911 S21.0 R23.0 P"G91 M83 G1 Z3 E{-global.power_fail_retract} F1000" ; Relative movement and extrusion. Move head up and retract 2mm filament.
                                      M208 S1 Z-0.5 ; set minimum Z
                                      T0 ; select first hot end
                                      M501 ; Load any config overrides
                                      undefined 1 Reply Last reply 28 Aug 2024, 12:50 Reply Quote 0
                                      • undefined
                                        DonStauffer @dc42
                                        last edited by DonStauffer 21 Aug 2024, 15:29

                                        This post is deleted!
                                        1 Reply Last reply Reply Quote 0
                                        • curieosundefined
                                          curieos
                                          last edited by 27 Aug 2024, 15:40

                                          Does alpha 4 still work with toolboards running 3.5.2? I'd like to give this a try, but the toolboard on my Micron is a Fly RRF 36 and it doesn't look like team gloomy is releasing 3.6 alpha builds.

                                          She/Her
                                          I work at a local 3D printing shop.
                                          Printers: Micron+ w/Duet 3 Mini, in-progress adaptation of the Jubilee REL onto an E3D MS, Prusa i3 MK3S.

                                          Notepadundefined undefined 2 Replies Last reply 27 Aug 2024, 16:24 Reply Quote 0
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