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    RepRapFirmware 3.6.0-alpha.4+3 available for testing

    Scheduled Pinned Locked Moved
    Beta Firmware
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    • Adrian52undefined
      Adrian52 @dc42
      last edited by

      @dc42 When trying the new alpha4+3, I get "movement halted step timing error occurred (code 3) Please reset the controller"
      Got same error with two different files. Duet2wifi standalone on a linear delta
      M122 following error:

      m122
      === Diagnostics ===
      RepRapFirmware for Duet 2 WiFi/Ethernet version 3.6.0-alpha.4+3 (2024-08-28 10:03:28) running on Duet WiFi 1.0 or 1.01
      Board ID: 08DAM-999TL-MQ4SD-6J9FD-3SJ6J-K593W
      Used output buffers: 3 of 26 (24 max)
      === RTOS ===
      Static ram: 23360
      Dynamic ram: 66712 of which 12 recycled
      Never used RAM 16112, free system stack 112 words
      Tasks: NETWORK(2,nWait 6,13.1%,222) HEAT(3,nWait 5,0.1%,328) Move(4,invalid,4.8%,266) MAIN(1,running,82.0%,832) IDLE(0,ready,0.0%,29), total 100.0%
      Owned mutexes: WiFi(NETWORK)
      === Platform ===
      Last reset 00:38:48 ago, cause: power up
      Last software reset at 2024-08-24 14:15, reason: User, Gcodes spinning, available RAM 25120, slot 1
      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
      Error status: 0x00
      Aux0 errors 0,0,0
      MCU temperature: min 36.1, current 38.1, max 39.1
      Supply voltage: min 24.1, current 24.3, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
      Heap OK, handles allocated/used 99/2, heap memory allocated/used/recyclable 2048/60/0, gc cycles 0
      Events: 0 queued, 0 completed
      Date/time: 2024-08-28 21:43:15
      Slowest loop: 213.94ms; fastest: 0.13ms
      I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
      === Storage ===
      Free file entries: 9
      SD card 0 detected, interface speed: 20.0MBytes/sec
      SD card longest read time 10.1ms, write time 0.0ms, max retries 0
      === Move ===
      Segments created 495, maxWait 54217ms, bed comp in use: none, height map offset 0.000, hiccups added 7 (0.25ms), max steps late 0, ebfmin 0.00, ebfmax 0.00
      Pos req/act/dcf: 66607.00/66935/-0.71 68379.00/68333/0.81 68571.00/68351/0.46
      no step interrupt scheduled
      Driver 0: standstill, SG min 0
      Driver 1: standstill, SG min 0
      Driver 2: standstill, SG min 0
      Driver 3: standstill, SG min 0
      Driver 4: standstill, SG min 0
      Driver 5: 
      Driver 6: 
      Driver 7: 
      Driver 8: 
      Driver 9: 
      Driver 10: 
      Driver 11: 
      === DDARing 0 ===
      Scheduled moves 242824, completed 242785, LaErrors 0, Underruns [0, 0, 0]
      === Heat ===
      Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
      Heater 0 is on, I-accum = 0.3
      Heater 1 is on, I-accum = 0.4
      === GCodes ===
      Movement locks held by null
      HTTP is idle in state(s) 0
      Telnet is idle in state(s) 0
      File is idle in state(s) 3
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      Daemon is idle in state(s) 0
      Autopause is idle in state(s) 0
      Q0 segments left 17
      Code queue 0 is empty
      === Filament sensors ===
      check 6729139 clear 1019682
      Extruder 0: pos 4.41, brightness 27, shutter 117, errs: frame 0 parity 0 ovrun 0 pol 0 ovdue 0
      === Network ===
      Slowest loop: 21.17ms; fastest: 0.07ms
      Responder states: HTTP(0) HTTP(1) HTTP(1) FTP(0) Telnet(0)
      HTTP sessions: 1 of 8
      === WiFi ===
      Interface state: active
      Module is connected to access point 
      Failed messages: pending 0, notrdy 0, noresp 0
      Firmware version 2.1.0
      MAC address 5c:cf:7f:2c:24:6b
      Module reset reason: Turned on by main processor, Vcc 3.38, flash size 4194304, free heap 41984
      WiFi IP address 192.168.1.16
      Signal strength -46dBm, channel 4, mode 802.11n, reconnections 0
      Clock register 00002002
      Socket states: 5 0 3 3 0 0 0 0
      28/08/2024, 21:42:39 	Error: Movement halted because a step timing error occurred (code 3). Please reset the controller.
      28/08/2024, 21:08:45 	M32 "0:/gcodes/OrcaCube_225.gcode"
      File 0:/gcodes/OrcaCube_225.gcode selected for printing
      
      1 Reply Last reply Reply Quote 1
      • edspedundefined
        edsped
        last edited by

        I had the same issue....

        timing error.jpg

        gloomyandyundefined 1 Reply Last reply Reply Quote 0
        • gloomyandyundefined
          gloomyandy @edsped
          last edited by

          @edsped What sort of printer are you using? What controller board?

          1 Reply Last reply Reply Quote 0
          • curieosundefined
            curieos
            last edited by curieos

            It appears I too had this issue. I completed the exact same print twice on alpha 4. I didn't have my computer on to catch the error in the log, but my print was halted and it did not respond to a pause. As the log says, Duet 3 Mini 5+ wifi, and I have a Fly RRF 36 toolboard (on 3.5.2). This is on a Micron (miniaturized Voron 2.4).

            M122
            === Diagnostics ===
            RepRapFirmware for Duet 3 Mini 5+ version 3.6.0-alpha.4+3 (2024-08-28 10:03:49) running on Duet 3 Mini5plus WiFi (standalone mode)
            Board ID: 3SKZN-BQ6KL-K65J0-409NS-K1X1Z-ZFT7Y
            Used output buffers: 3 of 40 (23 max)
            === RTOS ===
            Static ram: 92328
            Dynamic ram: 98920 of which 0 recycled
            Never used RAM 37916, free system stack 128 words
            Tasks: NETWORK(2,nWait 7,13.5%,179) HEAT(3,nWait 6,0.0%,325) Move(4,invalid,0.2%,247) TMC(4,nWait 6,1.6%,65) CanReceiv(6,nWait 1,0.1%,771) CanSender(5,nWait 7,0.0%,327) CanClock(7,delaying,0.0%,348) MAIN(1,running,83.7%,665) IDLE(0,ready,0.0%,29) AIN(4,delaying,0.8%,255), total 100.0%
            Owned mutexes:
            === Platform ===
            Last reset 19:27:32 ago, cause: software
            Last software reset at 2024-08-27 14:00, reason: User, Gcodes spinning, available RAM 6052, slot 2
            Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00487000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
            Error status: 0x00
            MCU temperature: min 38.7, current 40.4, max 43.2
            Supply voltage: min 23.6, current 23.9, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
            Heap OK, handles allocated/used 99/10, heap memory allocated/used/recyclable 2048/832/624, gc cycles 0
            Events: 1 queued, 1 completed
            Date/time: 2024-08-29 08:58:29
            Slowest loop: 226.13ms; fastest: 0.12ms
            === Storage ===
            Free file entries: 19
            SD card 0 detected, interface speed: 22.5MBytes/sec
            SD card longest read time 7.8ms, write time 0.0ms, max retries 0
            === Move ===
            Segments created 366, maxWait 152501ms, bed comp in use: mesh, height map offset 0.000, hiccups added 0 (0.00/0.00ms), max steps late 1, ebfmin 0.00, ebfmax 0.00
            Pos req/act/dcf: 23270.00/23909/-0.08 -1963.00/-2663/0.85 86222.00/86221/-0.00
            no step interrupt scheduled
            Driver 0: standstill, SG min 0, read errors 0, write errors 1, ifcnt 109, reads 11371, writes 19, timeouts 0, DMA errors 0, CC errors 0
            Driver 1: standstill, SG min 0, read errors 0, write errors 1, ifcnt 109, reads 11371, writes 19, timeouts 0, DMA errors 0, CC errors 0
            Driver 2: standstill, SG min 0, read errors 0, write errors 1, ifcnt 112, reads 11369, writes 20, timeouts 0, DMA errors 0, CC errors 0
            Driver 3: standstill, SG min 0, read errors 0, write errors 1, ifcnt 112, reads 11369, writes 20, timeouts 0, DMA errors 0, CC errors 0
            Driver 4: standstill, SG min 0, read errors 0, write errors 1, ifcnt 112, reads 11370, writes 20, timeouts 0, DMA errors 0, CC errors 0
            Driver 5: standstill, SG min 0, read errors 0, write errors 1, ifcnt 112, reads 11370, writes 20, timeouts 0, DMA errors 0, CC errors 0
            Driver 6: standstill, SG min 0, read errors 0, write errors 1, ifcnt 54, reads 11379, writes 10, timeouts 0, DMA errors 0, CC errors 0
            === DDARing 0 ===
            Scheduled moves 267477, completed 267437, LaErrors 0, Underruns [0, 0, 0]
            === DDARing 1 ===
            Scheduled moves 0, completed 0, LaErrors 0, Underruns [0, 0, 0]
            === Heat ===
            Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
            Heater 0 is on, I-accum = 0.2
            Heater 1 is on, I-accum = 0.0
            === GCodes ===
            Movement locks held by null, null
            HTTP is idle in state(s) 0
            Telnet is idle in state(s) 0
            File is doing "G1 X53.835 Y60.773 E.0219" in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            SBC is idle in state(s) 0
            Daemon is idle in state(s) 0
            Aux2 is idle in state(s) 0
            Autopause is idle in state(s) 0
            File2 is idle in state(s) 0
            Queue2 is idle in state(s) 0
            Q0 segments left 1, axes/extruders owned 0x0000807
            Code queue 0 is empty
            Q1 segments left 0, axes/extruders owned 0x0000000
            Code queue 1 is empty
            === CAN ===
            Messages queued 886806, received 1401380, lost 0, ignored 0, errs 1, boc 0
            Longest wait 2ms for reply type 6039, peak Tx sync delay 282, free buffers 26 (min 25), ts 350263/350262/0
            Tx timeouts 0,0,0,0,0,0
            === Network ===
            Slowest loop: 18.02ms; fastest: 0.00ms
            Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
            HTTP sessions: 1 of 8
            === WiFi ===
            Interface state: active
            Module is connected to access point 
            Failed messages: pending 0, notrdy 0, noresp 0
            Firmware version 2.1.0
            MAC address e8:68:e7:e1:4d:a8
            Module reset reason: Power up, Vcc 3.36, flash size 2097152, free heap 42012
            WiFi IP address 192.168.1.2
            Signal strength -48dBm, channel 11, mode 802.11n, reconnections 0
            Clock register 00002001
            Socket states: 3 0 0 0 0 0 0 0
            

            Edit: I'd also like to report that there wasn't an improvement in pressure advance behavior. Should I be running a 3.6 alpha on my toolboard too?

            She/Her
            I work at a local 3D printing shop.
            Printers: Micron+ w/Duet 3 Mini, in-progress adaptation of the Jubilee REL onto an E3D MS, Prusa i3 MK3S.

            1 Reply Last reply Reply Quote 0
            • balajiramaniundefined
              balajiramani @dc42
              last edited by

              @dc42 I just tried this version on the linear delta and the bed calibration bug still exists.

              @Adrian52, since you have a linear delta, are you able to run a bed calibration?

              Thanks,
              Balaji

              Adrian52undefined 1 Reply Last reply Reply Quote 0
              • Adrian52undefined
                Adrian52 @balajiramani
                last edited by

                @balajiramani I run delta calibration using the smart effector probe without any obvious problem, with residual error usually under 0.02. I normally don't need to use mesh compensation.

                Exerqtorundefined balajiramaniundefined 2 Replies Last reply Reply Quote 0
                • Exerqtorundefined
                  Exerqtor @Adrian52
                  last edited by

                  Just the the update earlier this evening and started a test print, and now I'm experiencing the same step timing issue as mentioned above.

                  D3 Mini with 1LC in standalone mode.

                  There printer is currently halted with this error message:

                  30.8.2024, 18:29:54	Error: Movement halted because a step timing error occurred (code 3). Please reset the controller.
                  30.8.2024, 17:55:27	ABS filament loaded
                  ABS filament loaded & config applied
                  30.8.2024, 17:54:49	16 points probed, min error -0.030, max error 0.016, mean -0.012, deviation 0.013
                  Height map saved to file 0:/sys/heightmap.csv
                  Height map saved to file 0:/sys/adaptive_heightmap.csv
                  30.8.2024, 17:54:18	Default grid: X10.0:340.0, Y10.0:340.0, Number of points: X12 Y12, 144 points
                  Adaptive grid: X120.833:229.167, Y120.833:229.136, Number of points: X4 Y4, 16 points
                  30.8.2024, 17:53:57	M32 "0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode"
                  File 0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode selected for printing
                  

                  This is the M122 outputs:

                  30.8.2024, 20:23:58	M122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 Mini 5+ version 3.6.0-alpha.4+3 (2024-08-28 10:03:49) running on Duet 3 Mini5plus WiFi (standalone mode)
                  Board ID: XNHXF-HR6KL-K65J0-409N2-K9W1Z-RV2MZ
                  Used output buffers: 11 of 40 (37 max)
                  === RTOS ===
                  Static ram: 92328
                  Dynamic ram: 95720 of which 0 recycled
                  Never used RAM 45628, free system stack 126 words
                  Tasks: NETWORK(1,ready,19.3%,179) HEAT(3,nWait 6,0.0%,325) Move(4,invalid,0.0%,247) TMC(4,nWait 6,0.9%,65) CanReceiv(6,nWait 1,0.1%,794) CanSender(5,nWait 7,0.0%,327) CanClock(7,delaying,0.0%,339) MAIN(1,running,77.6%,627) IDLE(0,ready,1.4%,29) AIN(4,delaying,0.8%,259), total 100.0%
                  Owned mutexes:
                  === Platform ===
                  Last reset 02:41:46 ago, cause: software
                  Last software reset at 2024-08-30 17:42, reason: User, Gcodes spinning, available RAM 52612, slot 0
                  Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                  Error status: 0x00
                  Aux0 errors 0,0,0
                  MCU temperature: min 45.7, current 46.0, max 46.0
                  Supply voltage: min 23.9, current 24.1, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
                  Heap OK, handles allocated/used 99/34, heap memory allocated/used/recyclable 2048/916/440, gc cycles 2170
                  Events: 0 queued, 0 completed
                  Date/time: 2024-08-30 20:23:53
                  Slowest loop: 46.99ms; fastest: 0.13ms
                  === Storage ===
                  Free file entries: 17
                  SD card 0 detected, interface speed: 22.5MBytes/sec
                  SD card longest read time 5.7ms, write time 7.2ms, max retries 0
                  === Move ===
                  Segments created 178, maxWait 0ms, bed comp in use: mesh, height map offset 0.000, hiccups added 0 (0.00/39.68ms), max steps late 0, ebfmin 0.00, ebfmax 0.00
                  Pos req/act/dcf: -3086.00/-3086/0.45 -23971.00/-23971/0.43 33160.00/33160/-0.00
                  no step interrupt scheduled
                  Driver 0: standstill, SG min 8, read errors 0, write errors 0, ifcnt 47, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
                  Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 47, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
                  Driver 2: standstill, SG min 2, read errors 0, write errors 0, ifcnt 22, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
                  Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
                  Driver 4: standstill, SG min 2, read errors 0, write errors 0, ifcnt 23, reads 1350, writes 0, timeouts 0, DMA errors 0, CC errors 0
                  Driver 5: not present
                  Driver 6: not present
                  === DDARing 0 ===
                  Scheduled moves 66586, completed 66560, LaErrors 0, Underruns [0, 0, 0]
                  === DDARing 1 ===
                  Scheduled moves 0, completed 0, LaErrors 0, Underruns [0, 0, 0]
                  === Heat ===
                  Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                  Heater 0 is on, I-accum = 0.4
                  Heater 1 is on, I-accum = 0.0
                  === GCodes ===
                  Movement locks held by null, null
                  HTTP is idle in state(s) 0
                  Telnet is idle in state(s) 0
                  File is doing "G1 X192.529 Y130.297 E.90485" in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon is doing "G4 P250" in state(s) 0 0, running macro
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  File2 is idle in state(s) 0
                  Queue2 is idle in state(s) 0
                  Q0 segments left 1, axes/extruders owned 0x0000807
                  Code queue 0 is empty
                  Q1 segments left 0, axes/extruders owned 0x0000000
                  Code queue 1 is empty
                  === Filament sensors ===
                  check 0 clear 0
                  Extruder 0 sensor: no filament
                  === CAN ===
                  Messages queued 247, received 600, lost 0, ignored 0, errs 0, boc 0
                  Longest wait 6ms for reply type 6024, peak Tx sync delay 132, free buffers 26 (min 25), ts 128/128/0
                  Tx timeouts 0,0,0,0,0,0
                  === Network ===
                  Slowest loop: 20.21ms; fastest: 0.07ms
                  Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
                  HTTP sessions: 1 of 8
                  === WiFi ===
                  Interface state: active
                  Module is connected to access point 
                  Failed messages: pending 0, notrdy 0, noresp 0
                  Firmware version 2.1.0
                  MAC address c4:5b:be:ce:91:93
                  Module reset reason: Power up, Vcc 3.37, flash size 2097152, free heap 43044
                  WiFi IP address 192.168.30.50
                  Signal strength -50dBm, channel 1, mode 802.11n, reconnections 0
                  Clock register 00002001
                  Socket states: 0 0 0 0 0 0 0 0
                  30.8.2024, 20:23:54	M122 B121
                  Diagnostics for board 121:
                  Duet TOOL1LC rev 1.1 or later firmware version 3.6.0-alpha.4+3 (2024-08-28 11:24:12)
                  Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25)
                  All averaging filters OK
                  Never used RAM 6672, free system stack 79 words
                  Tasks: Move(3,nWait 7,0.0%,84) TMC(2,delaying,3.6%,52) HEAT(2,nWait 6,0.4%,88) CanAsync(5,nWait 4,0.0%,48) CanRecv(3,nWait 1,0.0%,70) CanClock(5,nWait 1,0.0%,58) ACCEL(3,nWait 6,0.0%,52) MAIN(1,running,91.0%,318) IDLE(0,ready,0.0%,26) AIN(2,delaying,5.0%,112), total 100.0%
                  Owned mutexes:
                  Last reset 02:41:43 ago, cause: power up
                  Last software reset at 2024-03-12 16:55, reason: StackOverflow, available RAM 2968, slot 0
                  Software reset code 0x0100 ICSR 0x0042600e SP 0x20007f34 Task Move Freestk 3342 ok
                  Stack: 20004a80 20004ab4 0001cf33 20004c98 20004938 00000000 0001c011 20003320 fffffffd a5a5a5a5 00000000 20007f8c 00000000 20007f8c 0001cc97 00000000 200017c4 20001748 0001c4d7 20001748 200017c4 00000032 454c4449 00022700 0001ac77 200018e0 200018e0
                  Moves scheduled 65223, hiccups 0 (39.68/39.68ms), segs 58, step errors 0 (types 0x0), maxLate 0 maxPrep 0, ebfmin 0.00 max 0.00
                  Peak sync jitter -1/8, peak Rx sync delay 199, resyncs 0/0, no timer interrupt scheduled, next step interrupt due in 3459548387 ticks, disabled
                  VIN voltage: min 24.5, current 24.5, max 24.6
                  MCU temperature: min 41.1C, current 75.3C, max 75.5C
                  Driver 0: pos 2824553, 568.8 steps/mm, standstill, SG min 2, read errors 0, write errors 0, ifcnt 12, reads 9061, writes 0, timeouts 0, DMA errors 0, CC errors 0
                  Last sensors broadcast 0x00000012 found 2 164 ticks ago, 0 ordering errs, loop time 0
                  CAN messages queued 405, send timeouts 0, received 171, lost 0, ignored 0, errs 0, boc 0, free buffers 18, min 18, error reg 0
                  dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
                  Accelerometer: LIS3DH, status: 00
                  I2C bus errors 0, naks 0, contentions 0, other errors 0
                  === Filament sensors ===
                  Interrupt 5726621 to 0us, poll 9 to 925us
                  Driver 0: ok
                  
                  dc42undefined 1 Reply Last reply Reply Quote 0
                  • dc42undefined
                    dc42 administrators @Exerqtor
                    last edited by dc42

                    Thanks everyone, looks like we are getting a lot more step error code 3 than before with this build.

                    We've found a few other issues too:

                    • After a homing move there was sometimes a short pause before movement resumes. This is now fixed in the 3.6-dev source code. It may affect probing moves too.
                    • When an endstop switch is triggered during a homing move and the drivers concerned are on an expansion board, it's normal for the expansion board motor(s) to overshoot very slightly and then move back to the correct position. However, in this release the overshoot is often somewhat greater than it is in RRF 3.5.3-rc1, resulting in a noticeable jolt. This occurs with main board firmware 3.6.0-alpha.4+3 even if the expansion board is running firmware 3.5.3-rc.1.
                    • When EXP1HCL boards running 3.6.0-alpha.4+3 firmware are used in open loop mode, the start and end of the moves are jerky. Closed loop and assisted open loop modes work properly. This probably affects M23CL motors too.

                    I won't be able to fix these issues for a while because of other commitments.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    1 Reply Last reply Reply Quote 2
                    • gloomyandyundefined
                      gloomyandy
                      last edited by

                      Folks if anyone has a print that generates a "Movement halted error" after a short time (so relatively early in the print) can you please post the gcode file and the config.g file for the printer. That way we can try and reproduce the issue.

                      @Exerqtor did your error occur on the first print after a printer restart or had you already printed a previous file? I ask because your m122 is showing a hiccup delay, but no hiccups (maybe you have run m122 more than once after the failure). If this was the second print that failed can you test to see if the same print fails as the first print after the printer is restarted?

                      Exerqtorundefined 1 Reply Last reply Reply Quote 0
                      • balajiramaniundefined
                        balajiramani @Adrian52
                        last edited by

                        @Adrian52 I haven't been able to run a successful delta calibration with the 3.6.0 firmware. This was not an issue in 3.5.2. The head crashes into the bed. The movement is not straight from one probe point to the other and it more of a 'U' shaped move. Can you post your bed.g, so that I can compare it with what I have?

                        Thanks,
                        Balaji

                        dc42undefined Adrian52undefined 2 Replies Last reply Reply Quote 0
                        • dc42undefined
                          dc42 administrators @balajiramani
                          last edited by dc42

                          @balajiramani a U shaped move suggests that the auto-generated travel move is not being segmented. Please run M669 without parameters, to check that segmentation hasn't been disabled. Also please send M115 to verify that you really are running the latest alpha firmware.

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                          balajiramaniundefined 1 Reply Last reply Reply Quote 0
                          • balajiramaniundefined
                            balajiramani @dc42
                            last edited by

                            @dc42 Here are the output of the commands:

                            8/31/2024, 1:20:52 PM	M115
                            FIRMWARE_NAME: RepRapFirmware for Duet 2 WiFi/Ethernet FIRMWARE_VERSION: 3.6.0-alpha.4+3 ELECTRONICS: Duet WiFi 1.0 or 1.01 FIRMWARE_DATE: 2024-08-28 10:03:28
                            8/31/2024, 1:20:40 PM	M669
                            Kinematics is Linear delta, 100 segments/sec, min. segment length 0.20mm
                            
                            dc42undefined 2 Replies Last reply Reply Quote 0
                            • dc42undefined
                              dc42 administrators @balajiramani
                              last edited by dc42

                              Those of you with the code 3 errors, how long was the print running? I think I've just found a bug that could cause a code 3 error if a print was running about 47 minutes after the Duet 3 was booted up (about 38 minutes for Duet 2).

                              Duet WiFi hardware designer and firmware engineer
                              Please do not ask me for Duet support via PM or email, use the forum
                              http://www.escher3d.com, https://miscsolutions.wordpress.com

                              tasundefined Adrian52undefined curieosundefined 3 Replies Last reply Reply Quote 0
                              • dc42undefined
                                dc42 administrators @balajiramani
                                last edited by

                                @balajiramani thanks. Are you sure that the delta radius and rod length are set to approximately the correct value before calibration? I don't think anyone else has reported issues with delta calibration running recent 3.6.0 alpha versions, and calibration works perfectly on my own delta. So I am wondering whether the reason for the U-shaped moves is that either the rod length or delta radius is set incorrectly. Possibly there is an error in your M665 or M666 command and RRF 3.6 responds differently to that error. So please run M665 and M666 without parameters and check that the reported values are as expected.

                                Duet WiFi hardware designer and firmware engineer
                                Please do not ask me for Duet support via PM or email, use the forum
                                http://www.escher3d.com, https://miscsolutions.wordpress.com

                                balajiramaniundefined 1 Reply Last reply Reply Quote 0
                                • tasundefined
                                  tas @dc42
                                  last edited by

                                  @dc42 Duet 2 Wifi on an Ender 5 plus stopped with the code 3 error. Your 38 minute mark sounds about right but I don't have an exact time when it stopped.

                                  I installed 3.5.3 rc1 and ran the same gcode without issues.

                                  1 Reply Last reply Reply Quote 0
                                  • Exerqtorundefined
                                    Exerqtor @gloomyandy
                                    last edited by Exerqtor

                                    @gloomyandy said in RepRapFirmware 3.6.0-alpha.4+3 available for testing:

                                    Folks if anyone has a print that generates a "Movement halted error" after a short time (so relatively early in the print) can you please post the gcode file and the config.g file for the printer. That way we can try and reproduce the issue.

                                    For me it happened roughly 35min into the print.

                                    @Exerqtor did your error occur on the first print after a printer restart or had you already printed a previous file? I ask because your m122 is showing a hiccup delay, but no hiccups (maybe you have run m122 more than once after the failure). If this was the second print that failed can you test to see if the same print fails as the first print after the printer is restarted?

                                    Yeah it was the first print after the update! And you're right, it was the second M122 output. Here is the first output (including the print startinfo, error message etc:

                                    30.8.2024, 20:23:36	M122 B121
                                    Diagnostics for board 121:
                                    Duet TOOL1LC rev 1.1 or later firmware version 3.6.0-alpha.4+3 (2024-08-28 11:24:12)
                                    Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25)
                                    All averaging filters OK
                                    Never used RAM 6672, free system stack 79 words
                                    Tasks: Move(3,nWait 7,0.3%,84) TMC(2,nWait 6,3.6%,52) HEAT(2,nWait 6,0.4%,88) CanAsync(5,nWait 4,0.0%,48) CanRecv(3,nWait 1,0.1%,70) CanClock(5,nWait 1,0.0%,58) ACCEL(3,nWait 6,0.0%,52) MAIN(1,running,90.5%,318) IDLE(0,ready,0.0%,26) AIN(2,delaying,5.0%,112), total 100.0%
                                    Owned mutexes:
                                    Last reset 02:41:25 ago, cause: power up
                                    Last software reset at 2024-03-12 16:55, reason: StackOverflow, available RAM 2968, slot 0
                                    Software reset code 0x0100 ICSR 0x0042600e SP 0x20007f34 Task Move Freestk 3342 ok
                                    Stack: 20004a80 20004ab4 0001cf33 20004c98 20004938 00000000 0001c011 20003320 fffffffd a5a5a5a5 00000000 20007f8c 00000000 20007f8c 0001cc97 00000000 200017c4 20001748 0001c4d7 20001748 200017c4 00000032 454c4449 00022700 0001ac77 200018e0 200018e0
                                    Moves scheduled 65223, hiccups 782 (39.68/39.68ms), segs 58, step errors 2 (types 0x8), maxLate 0 maxPrep 1303, ebfmin 0.00 max 0.00
                                    Peak sync jitter -4/10, peak Rx sync delay 255, resyncs 0/0, no timer interrupt scheduled, next step interrupt due in 3473139117 ticks, disabled
                                    VIN voltage: min 23.7, current 24.5, max 25.0
                                    MCU temperature: min 41.1C, current 75.4C, max 75.5C
                                    Driver 0: pos 2824553, 568.8 steps/mm, standstill, SG min 0, read errors 1, write errors 0, ifcnt 12, reads 44905, writes 12, timeouts 3, DMA errors 0, CC errors 0, failedOp 0x6f
                                    Last sensors broadcast 0x00000012 found 2 43 ticks ago, 0 ordering errs, loop time 0
                                    CAN messages queued 200813, send timeouts 0, received 154587, lost 0, ignored 0, errs 0, boc 0, free buffers 18, min 17, error reg 0
                                    dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 825, adv 35393/74627
                                    Accelerometer: LIS3DH, status: 00
                                    I2C bus errors 0, naks 3, contentions 0, other errors 0
                                    === Filament sensors ===
                                    Interrupt 5726621 to 0us, poll 4 to 2225us
                                    Driver 0: ok
                                    
                                    30.8.2024, 20:23:32	M122
                                    === Diagnostics ===
                                    RepRapFirmware for Duet 3 Mini 5+ version 3.6.0-alpha.4+3 (2024-08-28 10:03:49) running on Duet 3 Mini5plus WiFi (standalone mode)
                                    Board ID: XNHXF-HR6KL-K65J0-409N2-K9W1Z-RV2MZ
                                    Used output buffers: 4 of 40 (37 max)
                                    === RTOS ===
                                    Static ram: 92328
                                    Dynamic ram: 95720 of which 0 recycled
                                    Never used RAM 45628, free system stack 126 words
                                    Tasks: NETWORK(1,ready,18.9%,179) HEAT(3,nWait 6,0.0%,325) Move(4,invalid,0.3%,247) TMC(4,nWait 6,0.9%,65) CanReceiv(6,nWait 1,0.1%,794) CanSender(5,nWait 7,0.0%,327) CanClock(7,delaying,0.0%,339) MAIN(1,running,77.7%,627) IDLE(0,ready,1.2%,29) AIN(4,delaying,0.8%,259), total 100.0%
                                    Owned mutexes: WiFi(NETWORK)
                                    === Platform ===
                                    Last reset 02:41:20 ago, cause: software
                                    Last software reset at 2024-08-30 17:42, reason: User, Gcodes spinning, available RAM 52612, slot 0
                                    Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                                    Error status: 0x00
                                    Aux0 errors 0,1,0
                                    MCU temperature: min 35.7, current 46.0, max 46.6
                                    Supply voltage: min 2.7, current 23.9, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
                                    Heap OK, handles allocated/used 99/34, heap memory allocated/used/recyclable 2048/1396/920, gc cycles 2164
                                    Events: 0 queued, 0 completed
                                    Date/time: 2024-08-30 20:23:27
                                    Slowest loop: 223.44ms; fastest: 0.10ms
                                    === Storage ===
                                    Free file entries: 17
                                    SD card 0 detected, interface speed: 22.5MBytes/sec
                                    SD card longest read time 10.2ms, write time 69.6ms, max retries 0
                                    === Move ===
                                    Segments created 178, maxWait 603453ms, bed comp in use: mesh, height map offset 0.000, hiccups added 0 (0.00/39.68ms), max steps late 0, ebfmin 0.00, ebfmax 0.00
                                    Pos req/act/dcf: -2663.00/-3086/0.45 -23548.00/-23971/0.43 33160.00/33160/-0.00
                                    no step interrupt scheduled
                                    Driver 0: standstill, SG min 0, read errors 0, write errors 0, ifcnt 47, reads 50443, writes 47, timeouts 0, DMA errors 0, CC errors 0
                                    Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 47, reads 50443, writes 47, timeouts 0, DMA errors 0, CC errors 0
                                    Driver 2: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 50467, writes 22, timeouts 0, DMA errors 0, CC errors 0
                                    Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 50467, writes 22, timeouts 0, DMA errors 0, CC errors 0
                                    Driver 4: standstill, SG min 0, read errors 0, write errors 0, ifcnt 23, reads 50467, writes 23, timeouts 0, DMA errors 0, CC errors 0
                                    Driver 5: not present
                                    Driver 6: not present
                                    === DDARing 0 ===
                                    Scheduled moves 66586, completed 66560, LaErrors 217, Underruns [0, 0, 0]
                                    === DDARing 1 ===
                                    Scheduled moves 0, completed 0, LaErrors 0, Underruns [0, 0, 0]
                                    === Heat ===
                                    Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                                    Heater 0 is on, I-accum = 0.4
                                    Heater 1 is on, I-accum = 0.0
                                    === GCodes ===
                                    Movement locks held by null, null
                                    HTTP is idle in state(s) 0
                                    Telnet is idle in state(s) 0
                                    File is doing "G1 X192.529 Y130.297 E.90485" in state(s) 0
                                    USB is idle in state(s) 0
                                    Aux is idle in state(s) 0
                                    Trigger is idle in state(s) 0
                                    Queue is idle in state(s) 0
                                    LCD is idle in state(s) 0
                                    SBC is idle in state(s) 0
                                    Daemon is doing "G4 P250" in state(s) 0 0, running macro
                                    Aux2 is idle in state(s) 0
                                    Autopause is idle in state(s) 0
                                    File2 is idle in state(s) 0
                                    Queue2 is idle in state(s) 0
                                    Q0 segments left 1, axes/extruders owned 0x0000807
                                    Code queue 0 is empty
                                    Q1 segments left 0, axes/extruders owned 0x0000000
                                    Code queue 1 is empty
                                    === Filament sensors ===
                                    check 0 clear 0
                                    Extruder 0 sensor: no filament
                                    === CAN ===
                                    Messages queued 154539, received 200688, lost 0, ignored 0, errs 1318, boc 0
                                    Longest wait 7ms for reply type 6029, peak Tx sync delay 10782, free buffers 26 (min 24), ts 48405/48403/0
                                    Tx timeouts 0,0,1,0,0,0 last cancelled message type 30 dest 127
                                    === Network ===
                                    Slowest loop: 210.77ms; fastest: 0.00ms
                                    Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
                                    HTTP sessions: 1 of 8
                                    === WiFi ===
                                    Interface state: active
                                    Module is connected to access point 
                                    Failed messages: pending 0, notrdy 0, noresp 0
                                    Firmware version 2.1.0
                                    MAC address c4:5b:be:ce:91:93
                                    Module reset reason: Power up, Vcc 3.38, flash size 2097152, free heap 43020
                                    WiFi IP address 192.168.30.50
                                    Signal strength -50dBm, channel 1, mode 802.11n, reconnections 0
                                    Clock register 00002001
                                    Socket states: 0 0 0 0 0 0 0 0
                                    
                                    30.8.2024, 18:29:54	Error: Movement halted because a step timing error occurred (code 3). Please reset the controller.
                                    
                                    30.8.2024, 17:55:27	ABS filament loaded
                                    ABS filament loaded & config applied
                                    30.8.2024, 17:54:49	16 points probed, min error -0.030, max error 0.016, mean -0.012, deviation 0.013
                                    Height map saved to file 0:/sys/heightmap.csv
                                    Height map saved to file 0:/sys/adaptive_heightmap.csv
                                    30.8.2024, 17:54:18	Default grid: X10.0:340.0, Y10.0:340.0, Number of points: X12 Y12, 144 points
                                    Adaptive grid: X120.833:229.167, Y120.833:229.136, Number of points: X4 Y4, 16 points
                                    30.8.2024, 17:53:57	M32 "0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode"
                                    File 0:/gcodes/ringing_text_test_0.2mm_ABS_0.4n_48m59s.gcode selected for printing
                                    
                                    dc42undefined 1 Reply Last reply Reply Quote 0
                                    • dc42undefined
                                      dc42 administrators @Exerqtor
                                      last edited by

                                      @Exerqtor @tas thanks. I will release 3.6.-alpha.5 after doing a couple of test prints.

                                      Duet WiFi hardware designer and firmware engineer
                                      Please do not ask me for Duet support via PM or email, use the forum
                                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                                      Exerqtorundefined 1 Reply Last reply Reply Quote 0
                                      • Exerqtorundefined
                                        Exerqtor @dc42
                                        last edited by

                                        @dc42 Awesome, i will install it and try the same testprint right away 😃

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                                        • balajiramaniundefined
                                          balajiramani @dc42
                                          last edited by

                                          @dc42 The delta calibration procedure works fine with 3.5.2. With 3.6.0-alpha*, I run into the issue. I checked the values of M665 and M666 in both 3.5.2 and 3.6.0-alpha and they are the same values.

                                          Here is what I see with 3.5.2:

                                          8/31/2024, 5:09:41 PM	M666
                                                                  Endstop adjustments X-1.26 Y-1.03 Z2.30, tilt X0.00% Y0.00%
                                          8/31/2024, 5:09:38 PM	M665
                                                                  Diagonals 395.647:395.647:395.647, delta radius 214.803, homed height 359.884, bed radius 160.0, X -0.068°, Y -0.015°, Z 0.000°
                                          
                                          

                                          Here is what I see with 3.6.0-alpha.4+3

                                          8/31/2024, 5:58:57 PM	M666
                                                                  Endstop adjustments X-1.26 Y-1.03 Z2.30, tilt X0.00% Y0.00%
                                          8/31/2024, 5:58:56 PM	M665
                                                                  Diagonals 395.647:395.647:395.647, delta radius 214.803, homed height 359.884, bed radius 160.0, X -0.068°, Y -0.015°, Z 0.000°
                                          
                                          o_lampeundefined 1 Reply Last reply Reply Quote 0
                                          • Adrian52undefined
                                            Adrian52 @balajiramani
                                            last edited by

                                            @balajiramani Hi - sorry for the delay
                                            here is my bed.g. I have a 250mm dia round bed

                                            ; Auto calibration routine for large delta printer
                                            M561                    ; clear any bed transform
                                            
                                            ; If the printer hasn't been homed, home it
                                            ;if !move.axes[0].homed || !move.axes[1].homed || !move.axes[2].homed
                                              G28
                                            
                                            ; Probe the bed and do auto calibration
                                            G1 X-70 Y-60 Z10 F6000        ; go to just above the first probe point
                                            while true
                                              if iterations = 5
                                                abort "too many auto calibration attempts"
                                              G30 P0 X-70 Y-60 Z-99999
                                              if result != 0
                                                continue
                                              G30 P1 X-85 Y0 Z-99999
                                              if result != 0
                                                continue
                                              G30 P2 X-50 Y75 Z-99999
                                              if result != 0
                                                continue
                                              G30 P3 X0 Y85 Z-99999
                                              if result != 0
                                                continue
                                              G30 P4 X50 Y75 Z-99999
                                              if result != 0
                                                continue
                                              G30 P5 X85 Y0 Z-99999
                                              if result != 0
                                                continue
                                              G30 P6 X75 Y-50 Z-99999
                                              if result != 0
                                                continue
                                              G30 P7 X0 Y-85 Z-99999
                                              if result != 0
                                                continue
                                              G30 P8 X-40 Y-40 Z-99999
                                              if result != 0
                                                continue
                                              G30 P9 X-50 Y0 Z-99999
                                              if result != 0
                                                continue
                                              G30 P10 X-40 Y40 Z-99999
                                              if result != 0
                                                continue
                                              G30 P11 X0 Y50 Z-99999
                                              if result != 0
                                                continue
                                              G30 P12 X40 Y40.00 Z-99999
                                              if result != 0
                                                continue
                                              G30 P13 X50 Y0 Z-99999
                                              if result != 0
                                                continue
                                              G30 P14 X40 Y-40 Z-99999
                                              if result != 0
                                                continue
                                              G30 P15 X-4 Y-2 Z-99999
                                              if result != 0
                                                continue
                                              G30 P16 X4 Y-2 Z-99999
                                              if result != 0
                                                continue
                                              G30 P17 X0 Y4 Z-99999 S6
                                              if result != 0
                                                continue
                                             
                                              if move.calibration.final.deviation <= 0.03
                                                break
                                              echo "Repeating calibration because deviation is too high (" ^ move.calibration.final.deviation ^ "mm)"
                                            ; end loop
                                            echo "Auto calibration successful, deviation", move.calibration.final.deviation ^ "mm"
                                            G1 X0 Y0 Z150 F5000                ; get the head out of the way
                                            M500
                                            G28
                                            
                                            balajiramaniundefined 1 Reply Last reply Reply Quote 0
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