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    Pressure Advance killing extruder motor

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    • deckingmanundefined
      deckingman @gnydick
      last edited by

      @gnydick What are your steps per mm with that 40:1 gearing at the 8x micro stepping you are using? Also, what value do you have PA set to?

      Ian
      https://somei3deas.wordpress.com/
      https://www.youtube.com/@deckingman

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      • Vetiundefined
        Veti
        last edited by

        whats your value for pressure advance?

        with a ratio of 40:1 your extruder prob cant move fast enough for a E jerk of 600 try going down on that.

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        • Edgars Batnaundefined
          Edgars Batna
          last edited by Edgars Batna

          If you use too low microstepping the motors can also start skipping steps, but, yeah, 40:1... I'd say 10:1 is the practical limit or you need to switch to 48V or higher.

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          • garisundefined
            garis
            last edited by

            I have a zesty nimble. They have 30:1 gearing. I have done extensive testing with PETG, and jerk seems best in the range 50 - 70 ( or around M205 0.8 to 1.2)

            Acceleration of 350 to 420.

            Works fine with M350 E16

            I am using a 0.6 nozzle. 0.4 may require a lower jerk and acceleration than a 0.6.

            Pressure Advance around 0.02 +/- Retraction 0.7

            Edgars Batnaundefined gnydickundefined 2 Replies Last reply Reply Quote 0
            • Edgars Batnaundefined
              Edgars Batna @garis
              last edited by Edgars Batna

              @garis The firmware jerk actually increases when you enable PA in the current implementation. It is computed as

              pa_jerk = jerk / pa_time

              so, in your case the firmware attempts to wiggle the motor 50 times faster than you've set it. At 8 microsteps (assuming TMC 2660) without interpolation you get loads of resonance fast. Plus at 40:1 it's a stretch to get it spinning as fast as 30mm/s with all the wiggling going on.

              Have you checked if the EMF is too high on https://reprapfirmware.org/ ?

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              • Alexander Mundyundefined
                Alexander Mundy
                last edited by Alexander Mundy

                I have Nimbles which use 30:1 and solved the jerk problem by using these 3.6 low inertia disc magnet steppers:

                https://www.portescap.com/products/disc-magnet-motors/p430-disc-magnet-high-speed-step-motor

                They are extremely expensive new but I lucked into a sweet deal on used ones which didn't break the bank.

                Here is an 80mm/s retraction test that shows how fast that stepper can change direction:

                https://youtu.be/sBAlXLfjx78

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                • garisundefined
                  garis
                  last edited by

                  Perhaps I haven't used a sufficiently high magnifying glass to understand what defects I should be observing or tolerating. My printing experience is limited and just now I am reprinting a few parts to upgrade the originals I printed for my Hypercube now that it is working.

                  As I understand it during the jerk phase the driver is asking the stepper to accelerate as fast as possible limited by the the motor current, up to the jerk setting leading to resonance in the more controlled velocity ramp during the acceleration phase. For the XY motors this is of concern but for the extruder I could imagine some/much of this resonance would be absorbed by the plastic, and perhaps some under extrusion if steps were missed. For a stepper with 2,600 steps that is likely to be of minor concern???

                  I am using a pancake stepper with lower inertia and it seems to work fine. (My original stepper was a recycled cheap one that did not move - it just growled at me - clearly the EMF was way too high on that one.)

                  The general print quality with PA of 0.02 was better than no PA. Using retraction speeds of 30 mm/s seems to be the sweet spot. The other variable is the print jerk with
                  the extruder being the slave but with the extruder able to limit the print speed - I am using XY jerk of 1,200 but higher values up to 2,000 + also seem to mechanically work ok, although print quality may be another matter.

                  I also don't know how far to go down this burrow given it seems to work ok and others don't seem have a problem - another limiting factor is the rotational flexibility of the nimble cable with the high performance magnetic motors just mentioned - curious about them.

                  Edgars Batnaundefined 1 Reply Last reply Reply Quote 0
                  • Alexander Mundyundefined
                    Alexander Mundy
                    last edited by

                    I don't have any data on the rotational flex of the Nimble cable. What I do know is that with the recommended Nema 14 and or the recommended Nema 17 pancake I could only increase extruder jerk to 60 and coupled with pressure advance made for really slow prints. With the disc steppers I can go to "normal" jerk and acceleration settings. Out of town so I can't see what they are right now.

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                    • gnydickundefined
                      gnydick @garis
                      last edited by

                      This post is deleted!
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                      • ayudteeundefined
                        ayudtee
                        last edited by

                        I can't explain the mystery as to why PA is causing this problem, very strange that everything works when it is turned off. PA is such a good feature, its worth trying to get it to work. I am recommending that you consider increasing your extruder motor current. 400mA seems low to me, as I am running 800mA on my Ormerod 2 and 700mA on my Delta.

                        deckingmanundefined 1 Reply Last reply Reply Quote 0
                        • deckingmanundefined
                          deckingman @ayudtee
                          last edited by

                          @ayudtee The motor current is what the stepper motor can tolerate and a good rule of thumb is to 85% of the rated maximum. So increasing the current to 800mA would not be a good idea if the Op's motors are rated at (say) 500 mA.

                          Ian
                          https://somei3deas.wordpress.com/
                          https://www.youtube.com/@deckingman

                          gnydickundefined 1 Reply Last reply Reply Quote 0
                          • gnydickundefined
                            gnydick @deckingman
                            last edited by

                            @deckingman they're definitely rated for more. I think the logic is, at 40:1 gearing, anything much more than 400-500mA doesn't work well. I've tried it, it's not happy.

                            deckingmanundefined 1 Reply Last reply Reply Quote 0
                            • deckingmanundefined
                              deckingman @gnydick
                              last edited by

                              @gnydick said in Pressure Advance killing extruder motor:

                              @deckingman they're definitely rated for more. I think the logic is, at 40:1 gearing, anything much more than 400-500mA doesn't work well. I've tried it, it's not happy.

                              Fair enough - there is nothing in this thread to state what the rated current of your motors are so I had to revet to using a crystal ball.

                              Referring back to my earlier post of 30th March @ 05:51, I might have some ideas but you haven't answered the questions I asked.

                              Ian
                              https://somei3deas.wordpress.com/
                              https://www.youtube.com/@deckingman

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                              • Alexander Mundyundefined
                                Alexander Mundy
                                last edited by Alexander Mundy

                                It was explained to me this way. At such high steps per time frame required with high gear ratio the current doesn't have much time to decay and so higher current exasperates the situation. With 3.6 degree steppers I run normal current levels but couldn't with 1.8 degree steppers.

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                                • dc42undefined
                                  dc42 administrators
                                  last edited by

                                  With such a high gearing ratio, you don't need much torque but you do need low inertia and high speed. So I suggest choosing a motor with low inductance, modest torque, and a high ratio of holding torque to rotor inertia. Run it close to its rated current (e.g. 85%).

                                  Duet WiFi hardware designer and firmware engineer
                                  Please do not ask me for Duet support via PM or email, use the forum
                                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                                  gnydickundefined garisundefined 2 Replies Last reply Reply Quote 0
                                  • Edgars Batnaundefined
                                    Edgars Batna @garis
                                    last edited by

                                    @garis said in Pressure Advance killing extruder motor:

                                    Perhaps I haven't used a sufficiently high magnifying glass to understand what defects I should be observing or tolerating. My printing experience is limited and just now I am reprinting a few parts to upgrade the originals I printed for my Hypercube now that it is working.

                                    You need to use a magnifying crystal ball, preferably with Christmas decorations within the ball.

                                    For the XY motors this is of concern but for the extruder I could imagine some/much of this resonance would be absorbed by the plastic, and perhaps some under extrusion if steps were missed. For a stepper with 2,600 steps that is likely to be of minor concern???

                                    At 40:1 there's basically no resistance whatsoever on the motor end to absorb anything, so there is just the rotor.

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                                    • gnydickundefined
                                      gnydick @dc42
                                      last edited by gnydick

                                      @dc42 thanks. Can you give an example of what qualifies as those suggestions? low inductance, modest, torque, high ratio of holding torque to rotor inertia?

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                                      • garisundefined
                                        garis @dc42
                                        last edited by

                                        @dc42 My pancake has more than enough torque @ 30:1. What is the reason to use high current?

                                        dc42undefined 1 Reply Last reply Reply Quote 0
                                        • dc42undefined
                                          dc42 administrators @garis
                                          last edited by

                                          @garis said in Pressure Advance killing extruder motor:

                                          @dc42 My pancake has more than enough torque @ 30:1. What is the reason to use high current?

                                          The reason to use a motor current close to the rated maximum is to provide enough torque to overcome the inertia of the rotor, because high gearing means you need high acceleration.

                                          Duet WiFi hardware designer and firmware engineer
                                          Please do not ask me for Duet support via PM or email, use the forum
                                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                                          1 Reply Last reply Reply Quote 0
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