@Phaedrux
Well i switched 0.3 with 0.4. (extruder was 0.3 and now 0.4, one of the z motors is now on 0.3)
(can you double check old vs new if i did it correctly?)
So am i right to conclude there is something wrong with the steppenmotor of my E3D Hemera? @Phaedrux
2-6-2024, 10:16:12 Warning: Driver 0.4 warning: phase B may be disconnected
2-6-2024, 09:59:06 Leadscrew adjustments made: -0.003 0.011, points used 2, (mean, deviation) before (0.004, 0.005) after (0.000, 0.000)
2-6-2024, 09:58:55 Leadscrew adjustments made: 0.115 0.070, points used 2, (mean, deviation) before (0.093, 0.016) after (0.000, 0.000)
2-6-2024, 09:58:08 File 0:/gcodes/corner_brace_3m_bolts_PETG_44m55s.gcode selected for printing
New
; Drives
M569 P0.0 S0 ; physical drive 0.0 goes backwards
M569 P0.1 S0 ; physical drive 0.1 goes backwards
M569 P0.2 S0 ; physical drive 0.2 goes backwards (Z Axis Left)
M569 P0.3 S0 ; physical drive 0.4 goes backwards (Z Axis Right)
M569 P0.4 S0 ; physical drive 0.3
M584 X0.0 Y0.1 Z0.2:0.3 E0.4 ; set drive mapping
M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
M92 X80.00 Y80.00 Z800.00 E394.26 ; set steps per mm
M566 X1200.00 Y1200.00 Z60.00 E3000.00 ; set maximum instantaneous speed changes (mm/min)(was X900.00 Y900.00 Z60.00(600) E120.00)
M203 X5000.00 Y5000.00 Z180.00 E5000.00 ; set maximum speeds (mm/min)(was X6000.00 Y6000.00 Z180.00 E1200.00)
M201 X1500.00 Y1500.00 Z20.00 E5000.00 ; set accelerations (mm/s^2)(was X500.00 Y500.00 Z20.00(80) E500.00)
M906 X800 Y800 Z800 E800 I30 ; set motor currents (mA) and motor idle factor in per cent(was X800 Y800 Z800 E800 I30)
M84 S30 ; Set idle timeout
Old
; Drives
M569 P0.0 S0 ; physical drive 0.0 goes backwards
M569 P0.1 S0 ; physical drive 0.1 goes backwards
M569 P0.2 S0 ; physical drive 0.2 goes backwards (Z Axis Left)
M569 P0.3 S0 ; physical drive 0.3 goes backwards
M569 P0.4 S0 ; physical drive 0.4 goes backwards (Z Axis Right)
M584 X0.0 Y0.1 Z0.2:0.4 E0.3 ; set drive mapping
M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
M92 X80.00 Y80.00 Z800.00 E394.26 ; set steps per mm
M566 X1200.00 Y1200.00 Z60.00 E3000.00 ; set maximum instantaneous speed changes (mm/min)(was X900.00 Y900.00 Z60.00(600) E120.00)
M203 X5000.00 Y5000.00 Z180.00 E5000.00 ; set maximum speeds (mm/min)(was X6000.00 Y6000.00 Z180.00 E1200.00)
M201 X1500.00 Y1500.00 Z20.00 E5000.00 ; set accelerations (mm/s^2)(was X500.00 Y500.00 Z20.00(80) E500.00)
M906 X800 Y800 Z800 E800 I30 ; set motor currents (mA) and motor idle factor in per cent(was X800 Y800 Z800 E800 I30)
M84 S30 ; Set idle timeout
extra information:
2-6-2024, 21:10:48 Finished printing file 0:/gcodes/blank_carriage_PETG_5h26m.gcode, print time was 6h 14m
2-6-2024, 20:51:29 Warning: Driver 0.4 warning: phase A may be disconnected, phase B may be disconnected
2-6-2024, 20:20:03 Warning: Driver 0.4 warning: phase A may be disconnected
2-6-2024, 19:48:10 Warning: Driver 0.4 warning: phase B may be disconnected
2-6-2024, 19:46:37 Warning: Driver 0.4 warning: phase B may be disconnected
2-6-2024, 19:44:45 Warning: Driver 0.4 warning: phase A may be disconnected
2-6-2024, 19:38:50 Warning: Driver 0.4 warning: phase A may be disconnected
2-6-2024, 19:29:59 m122
=== Diagnostics ===
RepRapFirmware for Duet 3 Mini 5+ version 3.5.1 (2024-04-19 14:41:25) running on Duet 3 Mini5plus Ethernet (standalone mode)
Board ID: 5QZRJ-6F6M2-G65J0-409FD-3Q81Z-72HAQ
Used output buffers: 8 of 40 (40 max)
=== RTOS ===
Static ram: 103232
Dynamic ram: 116100 of which 12 recycled
Never used RAM 18112, free system stack 122 words
Tasks: NETWORK(1,ready,76.0%,180) ETHERNET(5,nWait 7,0.2%,567) HEAT(3,nWait 1,0.2%,326) Move(4,nWait 6,6.2%,237) CanReceiv(6,nWait 1,0.0%,940) CanSender(5,nWait 7,0.0%,336) CanClock(7,delaying,0.0%,334) TMC(4,nWait 6,2.6%,68) MAIN(1,running,12.2%,665) IDLE(0,ready,0.0%,30) AIN(4,delaying,2.7%,260), total 100.0%
Owned mutexes:
=== Platform ===
Last reset 04:39:09 ago, cause: power up
Last software reset at 2024-06-02 10:55, reason: User, Gcodes spinning, available RAM 18184, slot 1
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00487000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
Error status: 0x04
Aux0 errors 0,1,0
MCU revision 0, ADC conversions started 16749063, completed 16749063, timed out 0, errs 0
MCU temperature: min 24.8, current 47.6, max 47.9
Supply voltage: min 23.6, current 23.9, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
Heap OK, handles allocated/used 99/3, heap memory allocated/used/recyclable 2048/176/56, gc cycles 0
Events: 14 queued, 14 completed
Driver 0: ok, SG min 0, read errors 0, write errors 0, ifcnt 14, reads 29302, writes 14, timeouts 0, DMA errors 0, CC errors 0
Driver 1: ok, SG min 0, read errors 0, write errors 0, ifcnt 14, reads 29301, writes 14, timeouts 0, DMA errors 0, CC errors 0
Driver 2: ok, SG min 0, read errors 0, write errors 0, ifcnt 14, reads 29301, writes 14, timeouts 0, DMA errors 0, CC errors 0
Driver 3: ok, SG min 0, read errors 0, write errors 0, ifcnt 14, reads 29301, writes 14, timeouts 0, DMA errors 0, CC errors 0
Driver 4: ok, SG min 0, read errors 0, write errors 0, ifcnt 12, reads 29304, writes 12, timeouts 0, DMA errors 0, CC errors 0
Driver 5: not present
Driver 6: not present
Date/time: 2024-06-02 15:47:29
Cache data hit count 4294967295
Slowest loop: 225.69ms; fastest: 0.13ms
=== Storage ===
Free file entries: 19
SD card 0 detected, interface speed: 22.5MBytes/sec
SD card longest read time 4.9ms, write time 79.8ms, max retries 0
=== Move ===
DMs created 83, segments created 46, maxWait 339966ms, bed compensation in use: mesh, height map offset 0.000, max steps late 1, min interval 0, bad calcs 0, ebfmin 0.00, ebfmax 1.00
next step interrupt due in 174 ticks, enabled
Moves shaped first try 36396, on retry 2560, too short 106922, wrong shape 35365, maybepossible 5431
=== DDARing 0 ===
Scheduled moves 194886, completed 194876, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state 3
=== DDARing 1 ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
Heater 0 is on, I-accum = 0.4
Heater 1 is on, I-accum = 0.5
=== GCodes ===
Movement locks held by null, null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is doing "G1 X108.786 Y129.904 E1.61464" in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
File2 is idle in state(s) 0
Queue2 is idle in state(s) 0
Q0 segments left 1, axes/extruders owned 0x0000807
Code queue 0 is empty
Q1 segments left 0, axes/extruders owned 0x0000000
Code queue 1 is empty
=== CAN ===
Messages queued 150740, received 0, lost 0, errs 79636997, boc 0
Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 26 (min 26), ts 83746/0/0
Tx timeouts 0,0,83745,0,0,66993 last cancelled message type 30 dest 127
=== Network ===
Slowest loop: 80.64ms; fastest: 0.03ms
Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
HTTP sessions: 1 of 8
= Ethernet =
Interface state: active
Error counts: 0 0 0 0 0 0
Socket states: 5 2 2 2 2 0 0 0