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Pressure Advance seems to not be working.

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  • undefined
    Phaedrux Moderator @DIY-O-Sphere
    last edited by 4 Jan 2020, 15:53

    @DIY-O-Sphere said in Pressure Advance seems to not be working.:

    Then above 1.2 the extrusion begins to fail....

    The pressure advance retreat combined with the retraction may have pulled the filament up high enough to get stuck.

    Z-Bot CoreXY Build | Thingiverse Profile

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    • undefined
      zapta @DIY-O-Sphere
      last edited by 4 Jan 2020, 16:00

      @DIY-O-Sphere said in Pressure Advance seems to not be working.:

      I have done that with a custom code in Prusaslicer.

      As a side note, the upcoming PrusaSlicer will make it even easier to set per height configurations.

      alt text

      undefined 1 Reply Last reply 4 Jan 2020, 16:05 Reply Quote 1
      • undefined
        Samuel235 @DIY-O-Sphere
        last edited by 4 Jan 2020, 16:01

        @DIY-O-Sphere - This is a 4:1 ratio extruder

        @zapta - That is such an awesome addition to the slicer!

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        • undefined
          DIY-O-Sphere @zapta
          last edited by 4 Jan 2020, 16:05

          @zapta said in Pressure Advance seems to not be working.:

          As a side note, the upcoming PrusaSlicer will make it even easier to set per height configurations.

          That is exactly the way I have done it ....

          (UTC+1)

          undefined 1 Reply Last reply 4 Jan 2020, 16:14 Reply Quote 0
          • undefined
            DIY-O-Sphere @DIY-O-Sphere
            last edited by DIY-O-Sphere 1 Apr 2020, 17:12 4 Jan 2020, 16:14

            @DIY-O-Sphere said in Pressure Advance seems to not be working.:

            That is exactly the way I have done it ....

            And what is also awesome: If you save the project file as 3mf you will be able to take that as template, without setting up all layer changes....

            (UTC+1)

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            • undefined
              Samuel235
              last edited by 4 Jan 2020, 16:29

              Currently trying the print again with Jerk set to 800 rather than 1000

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              • undefined
                Samuel235
                last edited by 4 Jan 2020, 18:21

                I still believe there is something causing PA to not take full effect, i don't believe there is much change on this new cube either. I've lowered my Jerk even more but the fact that I don't see much change at all up the seam, I don't believe its having full effect. Testing another cube now with a Jerk of 400.

                undefined 1 Reply Last reply 4 Jan 2020, 18:33 Reply Quote 0
                • undefined
                  Phaedrux Moderator
                  last edited by Phaedrux 1 Apr 2020, 18:29 4 Jan 2020, 18:29

                  Lowering the jerk will limit pressure advance even more. Unless you're using a high gear ratio remote direct drive like the Zesty Nimble reducing the jerk isn't really necessary.

                  I believe you're using the Voron2 Mobius extruder? Which is 4:1?

                  I would think that a extruder jerk and acceleration in the 3000 to 6000 range should be suitable.

                  I'm using a 3:1 titan aero with 0.9 degree motor and I use 6000 max speed, and 3000 accel and jerk. Mind you it's direct drive, so my PA value is very low 0.03 to 0.05.

                  Earlier you said you tried values between 0.5 and 7. Did you mean 0.5 and 0.7?

                  If you went up to 7 and nothing change something is wrong. If you only went up to 0.7 you haven't gone high enough.

                  What does the Voron 2 community suggest for extruder value configuration?

                  Z-Bot CoreXY Build | Thingiverse Profile

                  undefined 1 Reply Last reply 4 Jan 2020, 18:33 Reply Quote 0
                  • undefined
                    SnakeSP @Samuel235
                    last edited by 4 Jan 2020, 18:33

                    @Samuel235 I'm facing the similar thing.
                    My extruder is BMG with 3:1 ratio. Bowden 55cm.
                    Printed test cube with jerk set to 600 and PA set to 0.2 through 1.0 - got very minor effect.
                    Previous experiments with python PA test script showed effect with PA set to 1.6-1.65 which made my extruder sing with forward-backward-forward rapid move on every line.
                    Now i think about trying to set jerk to 0 and raise acceleration, as the formula in doc is: actual_extrusion_speed = requested_extrusion_speed + (K * current_extruder_acceleration), which makes me think the jerk should be minimal while acceleration should be high.

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                    • undefined
                      Samuel235 @Phaedrux
                      last edited by 4 Jan 2020, 18:33

                      @Phaedrux I did mean 0.5-0.7 sorry. I'm currently getting the printer ready for the print I said I'm running so I will change some settings back now then. I will put the Jerk back to the original 8000 (this is the default for this extruder, the majority of the community are running this value, with PA), and will change my test to range from 0.8 to 1.5 to see if I see any changes there.

                      How does that sound, too much or still too little PA?

                      undefined 1 Reply Last reply 4 Jan 2020, 18:37 Reply Quote 0
                      • undefined
                        Phaedrux Moderator @Samuel235
                        last edited by 4 Jan 2020, 18:37

                        @Samuel235 Ok that makes some more sense then. 0.7 may simply not be enough.

                        Jerk of 8000 simply removes jerk from the equation, which is fine if the extruder motor can handle it rapid direction changes. This is a problem for the Nimble because of the high gear ratio and the high speed it would need to rotate and the back emf that results. But in your case I don't think it will be an issue at all. It may be a bit noisy though.

                        0.8 to 1.5 would be the logical next range to test with. 650mm bowden tube is fairly long, so I would think closer to the 1.5 mark.

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • undefined
                          DIY-O-Sphere
                          last edited by 4 Jan 2020, 18:53

                          My BMG was skipping at such a high jerk. And that will also result in an annoying nocking noise....

                          (UTC+1)

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                          • undefined
                            Samuel235
                            last edited by 4 Jan 2020, 19:11

                            Printing now with a Jerk of 5000 to give the extruder some chance of not being the fault of the next print (I will see if I hear any skipped steps), PA ranging from 0.8 to 1.5 with 0 between every 25 layers. Will post back shortly when its all finished.

                            undefined 1 Reply Last reply 4 Jan 2020, 19:45 Reply Quote 0
                            • undefined
                              DIY-O-Sphere @Samuel235
                              last edited by 4 Jan 2020, 19:45

                              @Samuel235
                              Just for information, what is the retraction distance and speed? Material?

                              (UTC+1)

                              undefined 1 Reply Last reply 4 Jan 2020, 20:10 Reply Quote 0
                              • undefined
                                Samuel235 @DIY-O-Sphere
                                last edited by Samuel235 1 Apr 2020, 20:27 4 Jan 2020, 20:10

                                @DIY-O-Sphere - Retraction is 4mm at 60mm/s with a prime at 30mm/s and with Rigid Ink ABS in Black.

                                Edit: Correcting a typo

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                                • undefined
                                  Samuel235
                                  last edited by 4 Jan 2020, 20:35

                                  This cube has come out with no visual difference up the seam again. I had the following PA values at the respected layers:

                                  Layer | PA Value
                                  25 | 0.7
                                  50 | 0
                                  75 | 0.9
                                  100 | 0
                                  125 | 1.1
                                  150 | 0
                                  175 | 1.3
                                  200 | 0
                                  225 | 1.5

                                  No change at all other than it stopped extruding a little for 6/7 layers during the 1.1 value set of layers (layers 125 to 150).

                                  M122 for this print:

                                  M122
                                  === Diagnostics ===
                                  RepRapFirmware for Duet 2 WiFi/Ethernet version 2.03 running on Duet WiFi 1.02 or later + DueX5
                                  Board ID: 08DGM-956GU-DJMSN-6J1F4-3SJ6N-1BNBF
                                  Used output buffers: 5 of 24 (18 max)
                                  === RTOS ===
                                  Static ram: 25680
                                  Dynamic ram: 94256 of which 308 recycled
                                  Exception stack ram used: 492
                                  Never used ram: 10336
                                  Tasks: NETWORK(ready,524) HEAT(blocked,1236) DUEX(suspended,156) MAIN(running,1668) IDLE(ready,160)
                                  Owned mutexes:
                                  === Platform ===
                                  Last reset 02:37:52 ago, cause: software
                                  Last software reset time unknown, reason: User, spinning module GCodes, available RAM 10312 bytes (slot 1)
                                  Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
                                  Error status: 0
                                  Free file entries: 10
                                  SD card 0 detected, interface speed: 20.0MBytes/sec
                                  SD card longest block write time: 0.0ms, max retries 0
                                  MCU temperature: min 54.2, current 54.3, max 57.1
                                  Supply voltage: min 24.0, current 24.3, max 24.6, under voltage events: 0, over voltage events: 0, power good: yes
                                  Driver 0: standstill, SG min/max 0/1023
                                  Driver 1: standstill, SG min/max 0/243
                                  Driver 2: standstill, SG min/max not available
                                  Driver 3: standstill, SG min/max 0/972
                                  Driver 4: standstill, SG min/max not available
                                  Driver 5: standstill, SG min/max 9/249
                                  Driver 6: standstill, SG min/max 14/254
                                  Driver 7: standstill, SG min/max 0/255
                                  Driver 8: standstill, SG min/max 0/259
                                  Driver 9: standstill, SG min/max not available
                                  Date/time: 1970-01-01 00:00:00
                                  Cache data hit count 4294967295
                                  Slowest loop: 100.31ms; fastest: 0.08ms
                                  I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                                  === Move ===
                                  Hiccups: 0, FreeDm: 169, MinFreeDm: 159, MaxWait: 7ms
                                  Bed compensation in use: mesh, comp offset 0.000
                                  === DDARing ===
                                  Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
                                  === Heat ===
                                  Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
                                  Heater 0 is on, I-accum = 0.0
                                  Heater 1 is on, I-accum = 0.5
                                  === GCodes ===
                                  Segments left: 0
                                  Stack records: 4 allocated, 0 in use
                                  Movement lock held by null
                                  http is idle in state(s) 0
                                  telnet is idle in state(s) 0
                                  file is idle in state(s) 0
                                  serial is idle in state(s) 0
                                  aux is idle in state(s) 0
                                  daemon is idle in state(s) 0
                                  queue is idle in state(s) 0
                                  autopause is idle in state(s) 0
                                  Code queue is empty.
                                  === Network ===
                                  Slowest loop: 202.15ms; fastest: 0.08ms
                                  Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
                                  HTTP sessions: 1 of 8
                                  - WiFi -
                                  Network state is running
                                  WiFi module is connected to access point
                                  Failed messages: pending 0, notready 0, noresp 3
                                  WiFi firmware version 1.23
                                  WiFi MAC address XXXXXXXXXXXXXX
                                  WiFi Vcc 3.32, reset reason Turned on by main processor
                                  WiFi flash size 4194304, free heap 24592
                                  WiFi IP address XXXXXXXXXXXXXX
                                  WiFi signal strength -56dBm, reconnections 0, sleep mode modem
                                  Socket states: 0 0 0 0 0 0 0 0

                                  How far before the seam point on each layer should PA start to kick in because its literally right on top of the seam that the extruder shows some movement for PA. It doesn't change at all for the corners, its one continuous extrusion from start of layer to the end of the layer. I'm not sure it should really be like that....

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                                  • undefined
                                    Phaedrux Moderator
                                    last edited by 4 Jan 2020, 22:51

                                    How fast are you printing? Is Cura limiting your acceleration and jerk?

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    undefined 1 Reply Last reply 5 Jan 2020, 06:08 Reply Quote 0
                                    • undefined
                                      Samuel235 @Phaedrux
                                      last edited by 5 Jan 2020, 06:08

                                      7a3136aa-7d4d-48dd-8c08-644b14948d3b-image.png

                                      Neither of them are enabled and my speed is what I would class as fairly slow if i'm honest with you.. 17mm/s (i'm only printing a single wall)

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                                      • undefined
                                        Phaedrux Moderator
                                        last edited by 5 Jan 2020, 06:58

                                        That's really slow. Pressure advance is meant to reduce the effects of pressure build up. At such low speeds you're not building much pressure.

                                        Try using 2 walls with some amount of infill to increase layer time. 5% will do. And increase your print speeds to something closer to a normal print. 50mm/s or more.

                                        Z-Bot CoreXY Build | Thingiverse Profile

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                                        • undefined
                                          Phaedrux Moderator
                                          last edited by 5 Jan 2020, 07:00

                                          I assumed you'd seen this, but maybe not?

                                          https://duet3d.dozuki.com/Wiki/Pressure_advance

                                          Z-Bot CoreXY Build | Thingiverse Profile

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