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    Stall Guard

    Scheduled Pinned Locked Moved
    Tuning and tweaking
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    • BlueDustundefined
      BlueDust
      last edited by

      I don't know if this is actually relevant, but I also read that this Stall Guard may need some fine tuning pointing to this formula sheet.
      I filled it out best to my understanding, but do not know how to use it.

      a2c76831-9e37-4081-8920-7d255b8d89f0-image.png

      Fun, that 3 letter word with "u" in the middle.

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      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        Do you have a link to that sheet?

        Z-Bot CoreXY Build | Thingiverse Profile

        BlueDustundefined 1 Reply Last reply Reply Quote 0
        • Phaedruxundefined
          Phaedrux Moderator
          last edited by

          Have you tried getting it to detect a stall on a pure diagonal move to isolate just a single motor?

          Z-Bot CoreXY Build | Thingiverse Profile

          BlueDustundefined 1 Reply Last reply Reply Quote 0
          • BlueDustundefined
            BlueDust @Phaedrux
            last edited by

            @Phaedrux
            There is a link on the Sensorless homing wiki page that takes you to another page to talk about motors. This site has a link to download the calculation sheet I shared the screen shot of.

            https://duet3d.dozuki.com/Wiki/Choosing_and_connecting_stepper_motors

            Fun, that 3 letter word with "u" in the middle.

            1 Reply Last reply Reply Quote 1
            • BlueDustundefined
              BlueDust @Phaedrux
              last edited by

              @Phaedrux
              I just printed a large print with long movements and held the belts still.

              I can try printing a large calibration cube and see what happens.
              Thanks.

              Fun, that 3 letter word with "u" in the middle.

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              • dc42undefined
                dc42 administrators @BlueDust
                last edited by

                @BlueDust said in Stall Guard:

                M915 X Y S-10 F0 H200 R3

                With S-10 I would expect the motor to register stalled nearly all the time. You can check by sending M122 during a print and looking at the driver status.

                On my delta I have M915 set to warn about motor stalls. Using the same M915 settings as when I test sensorless homing on that machine, I get occasional (false) warnings. So I know that it is working at least some of the time.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

                BlueDustundefined 1 Reply Last reply Reply Quote 0
                • BlueDustundefined
                  BlueDust @dc42
                  last edited by

                  @dc42
                  I have been having a lot of trouble with the nozzle getting stuck in the print, and breaking different Z probes and why I want to fix this feature. I am having a lot of Z probe issues again caused by the crashes and not able to bed level. I will run m122 after I can print again.
                  Thanks

                  Fun, that 3 letter word with "u" in the middle.

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                  • dc42undefined
                    dc42 administrators
                    last edited by dc42

                    I have this on my list to look at, but I need to get firmware 3.01-RC3 released first. Please remind me again on Monday, assuming 3.01-RC3 is released by then.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    BlueDustundefined 1 Reply Last reply Reply Quote 0
                    • BlueDustundefined
                      BlueDust
                      last edited by

                      @dc42 said in Stall Guard:

                      M122

                      As I do use stall guard for homing, I wanted to compare both before and after I enabled it for printing...

                      This is before I enabled stall guard (printing)

                      M122
                      === Diagnostics ===
                      RepRapFirmware for Duet 2 WiFi/Ethernet version 2.05 running on Duet Ethernet 1.02 or later + DueX5
                      Board ID: 08DGM-9T6BU-FG3S0-7JTDL-3SN6N-TS6VG
                      Used output buffers: 3 of 24 (24 max)
                      === RTOS ===
                      Static ram: 25712
                      Dynamic ram: 93836 of which 0 recycled
                      Exception stack ram used: 656
                      Never used ram: 10868
                      Tasks: NETWORK(ready,628) HEAT(blocked,1232) DUEX(suspended,160) MAIN(running,1300) IDLE(ready,160)
                      Owned mutexes:
                      === Platform ===
                      Last reset 70:56:51 ago, cause: software
                      Last software reset at 2020-02-28 21:23, reason: User, spinning module GCodes, available RAM 11240 bytes (slot 2)
                      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
                      Error status: c
                      Free file entries: 8
                      SD card 0 detected, interface speed: 20.0MBytes/sec
                      SD card longest block write time: 17.0ms, max retries 1
                      MCU temperature: min 33.7, current 36.2, max 39.4
                      Supply voltage: min 23.5, current 23.8, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
                      Driver 0: ok, SG min/max 0/201
                      Driver 1: ok, SG min/max 0/205
                      Driver 2: standstill, SG min/max not available
                      Driver 3: ok, SG min/max 0/1023
                      Driver 4: standstill, SG min/max not available
                      Driver 5: standstill, SG min/max not available
                      Driver 6: standstill, SG min/max not available
                      Driver 7: standstill, SG min/max 0/1023
                      Driver 8: standstill, SG min/max 0/1023
                      Driver 9: standstill, SG min/max 0/1023
                      Date/time: 2020-03-02 20:20:51
                      Cache data hit count 4294967295
                      Slowest loop: 261.76ms; fastest: 0.08ms
                      I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                      === Move ===
                      Hiccups: 0, FreeDm: 157, MinFreeDm: 132, MaxWait: 21532997ms
                      Bed compensation in use: none, comp offset 0.000
                      === DDARing ===
                      Scheduled moves: 189, completed moves: 165, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
                      === Heat ===
                      Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
                      Heater 0 is on, I-accum = 0.2
                      Heater 1 is on, I-accum = 0.3
                      === GCodes ===
                      Segments left: 1
                      Stack records: 3 allocated, 0 in use
                      Movement lock held by null
                      http is idle in state(s) 0
                      telnet is idle in state(s) 0
                      file is doing "G1 X170.351 Y213.116 E12.2842" in state(s) 0
                      serial is idle in state(s) 0
                      aux is idle in state(s) 0
                      daemon is idle in state(s) 0
                      queue is idle in state(s) 0
                      autopause is idle in state(s) 0
                      Code queue is empty.
                      === Network ===
                      Slowest loop: 372.96ms; fastest: 0.05ms
                      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
                      HTTP sessions: 1 of 8
                      Interface state 5, link 100Mbps full duplex
                      === Filament sensors ===
                      Extruder 0: pos 280.55, errs: frame 164 parity 0 ovrun 0 pol 5 ovdue 0
                      

                      This is just what I had used to enable it this time...

                      M915 X Y S3 F1 H100 R3
                      

                      Same print as above Diagnostic text. I just ran the M915 command mentioned above, printer rehomed itself, and I copied the M122 Diagnostic text.

                      M122
                      === Diagnostics ===
                      RepRapFirmware for Duet 2 WiFi/Ethernet version 2.05 running on Duet Ethernet 1.02 or later + DueX5
                      Board ID: 08DGM-9T6BU-FG3S0-7JTDL-3SN6N-TS6VG
                      Used output buffers: 1 of 24 (24 max)
                      === RTOS ===
                      Static ram: 25712
                      Dynamic ram: 93836 of which 0 recycled
                      Exception stack ram used: 656
                      Never used ram: 10868
                      Tasks: NETWORK(ready,628) HEAT(blocked,1232) DUEX(suspended,160) MAIN(running,1300) IDLE(ready,160)
                      Owned mutexes:
                      === Platform ===
                      Last reset 71:04:28 ago, cause: software
                      Last software reset at 2020-02-28 21:23, reason: User, spinning module GCodes, available RAM 11240 bytes (slot 2)
                      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
                      Error status: c
                      Free file entries: 8
                      SD card 0 detected, interface speed: 20.0MBytes/sec
                      SD card longest block write time: 0.0ms, max retries 0
                      MCU temperature: min 38.3, current 38.9, max 39.2
                      Supply voltage: min 23.7, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                      Driver 0: ok, SG min/max 79/192
                      Driver 1: ok, SG min/max 80/184
                      Driver 2: standstill, SG min/max not available
                      Driver 3: ok, SG min/max 0/1023
                      Driver 4: standstill, SG min/max not available
                      Driver 5: standstill, SG min/max not available
                      Driver 6: standstill, SG min/max not available
                      Driver 7: standstill, SG min/max not available
                      Driver 8: standstill, SG min/max not available
                      Driver 9: standstill, SG min/max not available
                      Date/time: 2020-03-02 20:28:27
                      Cache data hit count 4294967295
                      Slowest loop: 3.33ms; fastest: 0.09ms
                      I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                      === Move ===
                      Hiccups: 0, FreeDm: 142, MinFreeDm: 128, MaxWait: 0ms
                      Bed compensation in use: none, comp offset 0.000
                      === DDARing ===
                      Scheduled moves: 4941, completed moves: 4905, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
                      === Heat ===
                      Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
                      Heater 0 is on, I-accum = 0.2
                      Heater 1 is on, I-accum = 0.3
                      === GCodes ===
                      Segments left: 1
                      Stack records: 3 allocated, 0 in use
                      Movement lock held by null
                      http is idle in state(s) 0
                      telnet is idle in state(s) 0
                      file is doing "G1 X208.678 Y124.970 E0.4618" in state(s) 0
                      serial is idle in state(s) 0
                      aux is idle in state(s) 0
                      daemon is idle in state(s) 0
                      queue is idle in state(s) 0
                      autopause is idle in state(s) 0
                      Code queue is empty.
                      === Network ===
                      Slowest loop: 6.89ms; fastest: 0.05ms
                      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
                      HTTP sessions: 1 of 8
                      Interface state 5, link 100Mbps full duplex
                      === Filament sensors ===
                      Extruder 0: pos 280.20, errs: frame 164 parity 0 ovrun 0 pol 5 ovdue 0
                      

                      Fun, that 3 letter word with "u" in the middle.

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                      • BlueDustundefined
                        BlueDust @dc42
                        last edited by BlueDust

                        @dc42
                        I know I am a little late with this... Reminder. 🙂
                        As always, Thank you for your help!

                        Fun, that 3 letter word with "u" in the middle.

                        dc42undefined 1 Reply Last reply Reply Quote 0
                        • dc42undefined
                          dc42 administrators @BlueDust
                          last edited by

                          @BlueDust, have you tried RRF3 yet? That's where development is now focused.

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                          BlueDustundefined 1 Reply Last reply Reply Quote 0
                          • BlueDustundefined
                            BlueDust @dc42
                            last edited by

                            @dc42
                            No. I wanted to wait until there was an official release and not just an RC. Also after I got this working... That way I didn't have to troubleshoot with new code.
                            I may have the time to work on the conversation to RRF3 next weekend... I will follow up again after I upgrade the software and try this again.

                            Thanks.

                            Fun, that 3 letter word with "u" in the middle.

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