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    2 weeks and already went bad? Duet 2 Wifi?

    Scheduled Pinned Locked Moved
    Duet Hardware and wiring
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    • EzeEundefined
      EzeE
      last edited by

      ; Configuration file for Duet WiFi (firmware version 2.03)
      ; executed by the firmware on start-up
      ;
      ; generated by RepRapFirmware Configuration Tool v2.1.8 on Sat Apr 04 2020 15:16:06 GMT-0700 (Pacific Daylight Time)

      ; General preferences
      G90 ; send absolute coordinates...
      M83 ; ...but relative extruder moves
      M550 P"Tronxy X5ST-500" ; set printer name

      M667 S1 ; select CoreXY mode

      ; Network
      M550 PTronxy X5S ; Set machine name
      M552 S1 ; enable network
      M586 P0 S1 ; enable HTTP
      M586 P1 S0 ; disable FTP
      M586 P2 S0 ; disable Telnet

      ; Drives
      M569 P0 S0 ; physical drive 0 goes forwards
      M569 P1 S0 ; physical drive 1 goes forwards
      M569 P2 S1 ; physical drive 2 goes backwards
      M569 P3 S1 ; physical drive 3 goes backwards
      M584 X0 Y1 Z2 E3 ; set drive mapping
      M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
      M92 X80.00 Y80.00 Z400.00 E142.00 ; set steps per mm
      M566 X600.00 Y600.00 Z12.00 E120.00 ; set maximum instantaneous speed changes (mm/min)
      M203 X18000.00 Y18000.00 Z180.00 E1500.00 ; set maximum speeds (mm/min)
      M201 X3000.00 Y3000.00 Z100.00 E250.00 ; set accelerations (mm/s^2)
      M906 X1680 Y1680 Z1680 E950 I30 ; set motor currents (mA) and motor idle factor in per cent
      M84 S30 ; Set idle timeout

      ; Axis Limits
      M208 X0 Y0 Z0 S1 ; set axis minima
      M208 X500 Y500 Z600 S0 ; set axis maxima

      ; Endstops
      M574 X1 Y1 Z1 S0 ; set active low and disabled endstops

      ; Z-Probe
      M558 P5 H5 F0 T6000 ; set Z probe type to switch and the dive height + speeds
      G31 P600 X0 Y0 Z0 ; set Z probe trigger value, offset and trigger height
      M557 X15:215 Y15:195 S20 ; define mesh grid

      ; Heaters
      ;M305 P0 T100000 B4138 R4700 ; set thermistor + ADC parameters for heater 0
      ;M143 H0 S120 ; set temperature limit for heater 0 to 120C
      ;M305 P1 T100000 B4138 R4700 ; set thermistor + ADC parameters for heater 1
      ;M143 H1 S280 ; set temperature limit for heater 1 to 280C

      ; Fans
      M106 P0 S0 I0 F500 H-1 ; set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned off
      M106 P1 S1 I0 F500 H1 T45 ; set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on
      M106 P2 S1 I0 F500 H1 T45 ; set fan 2 value, PWM signal inversion and frequency. Thermostatic control is turned on

      ; Tools
      M563 P0 D0 H1 F0 ; define tool 0
      G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
      G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

      ; Custom settings are not defined

      ; Miscellaneous
      M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss

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      • EzeEundefined
        EzeE @A Former User
        last edited by

        @bearer No overrides

        1 Reply Last reply Reply Quote 0
        • A Former User?
          A Former User @EzeE
          last edited by

          @EzeE said in 2 weeks and already went bad? Duet 2 Wifi?:

          Also now when I try to home Y access I get a message saying phase A may be disconnected while it actually runs X motor and not Y.

          M667 S1 ; select CoreXY mode

          thats kinda relevant i suspect, but i'll defer to the others for config and corexy stuff.

          meanwhile, maybe throw in the homeall, homex and homey files

          1 Reply Last reply Reply Quote 0
          • EzeEundefined
            EzeE
            last edited by

            ; homex.g
            ; called to home the X axis
            ;
            ; generated by RepRapFirmware Configuration Tool v2.1.8 on Sat Apr 04 2020 15:16:06 GMT-0700 (Pacific Daylight Time)
            G91 ; relative positioning
            G1 H2 Z5 F6000 ; lift Z relative to current position
            G1 H1 X-505 F1800 ; move quickly to X axis endstop and stop there (first pass)
            G1 X5 F6000 ; go back a few mm
            G1 H1 X-505 F360 ; move slowly to X axis endstop once more (second pass)
            G1 H2 Z-5 F6000 ; lower Z again
            G90 ; absolute positioning

            ; homey.g
            ; called to home the Y axis
            ;
            ; generated by RepRapFirmware Configuration Tool v2.1.8 on Sat Apr 04 2020 15:16:06 GMT-0700 (Pacific Daylight Time)
            G91 ; relative positioning
            G1 H2 Z5 F6000 ; lift Z relative to current position
            G1 H1 Y-505 F1800 ; move quickly to Y axis endstop and stop there (first pass)
            G1 Y5 F6000 ; go back a few mm
            G1 H1 Y-505 F360 ; move slowly to Y axis endstop once more (second pass)
            G1 H2 Z-5 F6000 ; lower Z again
            G90 ; absolute positioning

            ; homez.g
            ; called to home the Z axis
            ;
            ; generated by RepRapFirmware Configuration Tool v2.1.8 on Sat Apr 04 2020 15:16:06 GMT-0700 (Pacific Daylight Time)
            G91 ; relative positioning
            G1 H2 Z5 F6000 ; lift Z relative to current position
            G1 H1 Z-605 F1800 ; move Z down until the endstop is triggered
            G92 Z0 ; set Z position to axis minimum (you may want to adjust this)

            ; Uncomment the following lines to lift Z after probing
            ;G91 ; relative positioning
            ;G1 Z5 F100 ; lift Z relative to current position
            ;G90 ; absolute positioning

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            • Phaedruxundefined
              Phaedrux Moderator
              last edited by

              @EzeE said in 2 weeks and already went bad? Duet 2 Wifi?:

              Also now when I try to home Y access I get a message saying phase A may be disconnected while it actually runs X motor and not Y.

              Check your wiring. With CoreXY two motors produce the X and Y motion, not just one. So if only one is moving and it's complaining that there may be phases disconnected, it's probably right. Check you crimps on the motors cables.

              Z-Bot CoreXY Build | Thingiverse Profile

              EzeEundefined 3 Replies Last reply Reply Quote 0
              • EzeEundefined
                EzeE @Phaedrux
                last edited by

                This post is deleted!
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                • EzeEundefined
                  EzeE @Phaedrux
                  last edited by

                  @Phaedrux @Phaedrux said in 2 weeks and already went bad? Duet 2 Wifi?:

                  @EzeE said in 2 weeks and already went bad? Duet 2 Wifi?:

                  Also now when I try to home Y access I get a message saying phase A may be disconnected while it actually runs X motor and not Y.

                  Check your wiring. With CoreXY two motors produce the X and Y motion, not just one. So if only one is moving and it's complaining that there may be phases disconnected, it's probably right. Check you crimps on the motors cables.

                  Not sure exactly what you mean about checking the wiring they were working fine, no nicks felt wires look the same, none are loose. When I would hit home previous times it would move the Y motor just fine in fact it moved and homed it prior to the print. Now it throws an error and the X motor turns on when I hit home on the Y with no changes in wiring. Crimps look tight, I assumed they would I used proper crimping tool.

                  Also again Hotbed and Hotend both started reading 2k at same time, and z probe not working. I thought Z-probe was just cheap and I was using z-stop instead so didn't think much of it since I was going to replace with a BL-touch.

                  Hitting E-stop on webpage should not cause a board to wig out. If it does cause Duet problems why is it there?

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                  • EzeEundefined
                    EzeE @Phaedrux
                    last edited by

                    @Phaedrux I also understand that the X and Y motors produce the movement. If I take the belt off the y motor is does not spin. If I move my z cable to the Y motor it spins. If I use Y cable on X motor it spins. If I plug any motor into Y port it does not spin.

                    1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      It sounds like you've had a failure of the Y driver for sure. Possibly more.

                      Can you post some close up well lit high res photos of the board? Do you see any areas that look damaged, burnt, etc?

                      Z-Bot CoreXY Build | Thingiverse Profile

                      EzeEundefined 1 Reply Last reply Reply Quote 0
                      • EzeEundefined
                        EzeE @Phaedrux
                        last edited by

                        @Phaedrux I'll take some pictures just post them here? Nothing looks burned that I can tell, I do know I do not smell any of that lovely ozone of burnt electronics.

                        1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          Yes please post them here, or on an online file sharing folder like dropbox or google drive.

                          Z-Bot CoreXY Build | Thingiverse Profile

                          EzeEundefined 1 Reply Last reply Reply Quote 0
                          • EzeEundefined
                            EzeE @Phaedrux
                            last edited by

                            @Phaedrux Hopefully this works

                            https://drive.google.com/file/d/1l2wgaa3ZwHttCgenJIocm9l2QrbCGfBl/view?usp=sharing
                            https://drive.google.com/file/d/12Wt7HpUuwI5AxnGoN1vUtaYQgV5DXQV4/view?usp=sharing
                            https://drive.google.com/file/d/1maniM2el2XS4bAmyNfQ9xHAxUgfsI_gy/view?usp=sharing
                            https://drive.google.com/file/d/1A0D3gYaJUDsKnR63bWMDxyIBUiGFhl0R/view?usp=sharing
                            https://drive.google.com/file/d/1byWBEEtQa-88TeLkCA9kk5uMx245rpxX/view?usp=sharing
                            https://drive.google.com/file/d/1dD33aAgnptyP5pg68S3bUfBujc2Z32J4/view?usp=sharing
                            https://drive.google.com/file/d/1HD7ZJEE6i7H-KXD0x2lMC1UCaxksfRVa/view?usp=sharing

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                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by

                              I can't see any obvious signs of burnt chips.

                              Are you using the nylon washers to isolate the board from the mounting screws?

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • EzeEundefined
                                EzeE
                                last edited by

                                yes I am using nylon washers and stand off posts

                                1 Reply Last reply Reply Quote 0
                                • elmoretundefined
                                  elmoret
                                  last edited by

                                  @dc42 , does this quality for warranty replacement?

                                  1 Reply Last reply Reply Quote 0
                                  • Phaedruxundefined
                                    Phaedrux Moderator @EzeE
                                    last edited by

                                    @EzeE said in 2 weeks and already went bad? Duet 2 Wifi?:

                                    I started a print and the bed did not trip my z stop

                                    What exactly do you mean by this? Was there a head crash? The Y driver not working is one thing, but the thermistor reading 2000 would indicate a possible short.

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    EzeEundefined 3 Replies Last reply Reply Quote 0
                                    • EzeEundefined
                                      EzeE @Phaedrux
                                      last edited by

                                      @Phaedrux

                                      So when I started the print the X, Y, and Z all homed properly. The Z axis moved down and the extruder moved to the center of the bed. What should have happened but didn't is the Z should have moved up which usually trips Z sensor. Instead it sat there like it maybe thought it made the move and then started extruding with the bed not in place. Which is why I tripped the stop.

                                      The Z not moving into position could be my fault since I unplugged z probe since it stopped working, but code is still in there.

                                      There was no bed crash.

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                                      • EzeEundefined
                                        EzeE @Phaedrux
                                        last edited by

                                        @Phaedrux

                                        Also when the Hot end started reading 2l the Bed went to 2k as well.

                                        droftartsundefined 1 Reply Last reply Reply Quote 0
                                        • EzeEundefined
                                          EzeE @Phaedrux
                                          last edited by

                                          @Phaedrux

                                          Just fixed the Thermistors reading 2k. Found an old post about a delta printer having similar issue and the M305 lines being commented out. Scrolled up to look at config.g I posted and my M305 were commented. Loaded the backed up config.g file from printer and readings are 21 degrees idle.

                                          So now just the Y not working. And possibly z-probe.

                                          droftartsundefined 1 Reply Last reply Reply Quote 0
                                          • droftartsundefined
                                            droftarts administrators @EzeE
                                            last edited by

                                            @EzeE Please send M115 to the Duet, and post reply, to report the firmware version.

                                            Were the X and Y axes moving particularly fast when you pressed estop? What motors do you have on X and Y? Standard TronXY X5ST-500? I notice you have the max speed, accelerations and motor currents set quite high:

                                            M566 X600.00 Y600.00 Z12.00 E120.00 ; set maximum instantaneous speed changes (mm/min)
                                            M203 X18000.00 Y18000.00 Z180.00 E1500.00 ; set maximum speeds (mm/min)
                                            M201 X3000.00 Y3000.00 Z100.00 E250.00 ; set accelerations (mm/s^2)
                                            M906 X1680 Y1680 Z1680 E950 I30 ; set motor currents (mA) and motor idle factor in per cent
                                            

                                            Thinking maybe sudden stop during fast move caused a voltage spike back through the driver, killing the driver.

                                            Ian

                                            Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                            EzeEundefined 2 Replies Last reply Reply Quote 0
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