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    Print stuttering around curves, LaErrors

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    Duet Hardware and wiring
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    • Charlieundefined
      Charlie
      last edited by

      Hello, I have a CR10S5 with an E3D SuperVolcano and Duet WiFi. I noticed during the print that the nozzle was stopping (or at least slowing down dramatically) while printing the perimeter. This left some noticeable "zits" on the surface.

      IMG_8298.jpg

      IMG_8297.jpg

      I cancelled the print.

      ; 0:/sys/config.g
      ; Configuration file for Duet WiFi (firmware version 1.21).
      ; Executed by the firmware on start-up.

      ; General preferences
      G90 ; Set all to absolute positioning
      M83 ; Set extruder to relative positioning

      ; Network
      M552 S1 ; Enable wifi network
      M586 P0 S1 ; Enable HTTP
      M586 P1 S0 ; Disable FTP
      M586 P2 S0 ; Disable Telnet

      ; Drives
      M569 P0 S1 ; Physical drive 0 goes forwards
      M569 P1 S1 ; Physical drive 1 goes forwards
      M569 P2 S1 ; Physical drive 2 goes forwards
      M569 P3 S1 ; Physical drive 3 goes forwards
      M350 X16 Y16 Z16 E16 I1 ; Configure microstepping, interpolation
      M92 X80.00 Y80.00 Z400.00 E824.00 ; Set steps per mm
      M566 X480.00 Y480.00 Z30.00 E10000.00 ; Set maximum instantaneous speed changes (mm/min)
      M203 X21000.00 Y21000.00 Z900.00 E1500.00 ; Set maximum speeds (mm/min)
      M201 X500.00 Y500.00 Z180.00 E10000.00 ; Set maximum print move accelerations (mm/s^2)
      M906 X1400.00 Y1400.00 Z900.00 E1428.00 I30 ; Set motor currents (mA) and motor idle factor percent, 85 percent max stepper current on X, Y, and E. 60 on Z to decrease noise.
      M84 S30 ; Set idle timeout

      ; Axis Limits
      M208 X0 Y0 Z0 S1 ; Set axis minima
      M208 X470 Y500 Z500 S0 ; Set axis maxima

      ; Endstops
      M574 X1 Y1 S1 ; Set active high endstops

      ; Z-Probe
      M574 Z1 S2 ; Set endstops controlled by probe
      M558 P8 F120 H2 I1 R0 T6000 A1 B1 ; Set Z probe type, feed rate, dive height, reading inversion, recovery, travel speed, probe times per point, bed heater while probing.
      G31 P5 X53.100 Y9.000 Z2.102 ; Set Z probe trigger value, x and y probe offsets, and trigger height.
      M557 X56:470 Y25:475 P4 ; Define mesh grid minimum and maximum x and y probe coordinates, and number of probe points for each axis direction.

      ; Heaters
      M305 P0 T100000 B3950 R4700 ; Set thermistor and ADC parameters for heater 0 (bed), resistance at 25 C, beta value, series resistance of controller electronics.
      M143 H0 S120 ; Set temperature limit for heater 0 (bed) (deg C)
      M305 P1 T100000 B4267 R4700 ; Set thermistor and ADC parameters for heater 1 (extruder)
      M143 H1 S285 ; Set temperature limit for heater 1 (extruder) (deg C).
      M307 H1 A1318.4 C689.5 D5.2 I0 V24.1 B0 S1 ; Tune heater 1 (extruder), gain, dominant time (s), dead time (s), PWM signal inversion, calibration voltage, bang bang, max PWM.

      ; Fans
      M106 P0 S0 I0 F500 H-1 ; Set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned off
      M106 P1 S1 I0 F500 H1 T50 ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on

      ; Tools
      M563 P0 D0 H1 ; Define tool 0, extruder drive 0, heater 1.
      G10 P0 X0 Y0 Z0 ; Set tool 0 axis offsets
      G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C
      M591 D0 P2 C3 S1 ; Enable filament sensing, extruder drive 0, simple sensor low with filament, connected to E0, enable filament monitoring.

      ; Automatic power saving
      M911 S23.5 R24.0 P"M913 X0 Y0 G91 M83 G1 Z3 E-2 F2400" ; Set auto save on power loss, auto save voltage threshold, resume threshold, and actions to run on power loss.

      ; Temperature Compensation
      M912 P0 S-4.7 ; Set cpu temp sensor correction. Lower number decreases displayed cpu temp.

      ; Pressure Advance
      M572 D0 S0.05 ; Enable pressure advance and set it. Marlin setup used a K of 0.03-0.05. HatchBox Wood K=0.03.

      ; Custom settings are not configured

      ; Miscellaneous
      M501 ; Load saved parameters from non-volatile memory

      T0 ; Select first tool head

      But first I did a diagnostic while it was printing.

      M122
      === Diagnostics ===

      RepRapFirmware for Duet 2 WiFi/Ethernet version 2.02(RTOS) running on Duet WiFi 1.02 or later
      Used output buffers: 1 of 20 (13 max)
      === RTOS ===
      Static ram: 25524
      Dynamic ram: 98604 of which 0 recycled
      Exception stack ram used: 432
      Never used ram: 6512
      Tasks: NETWORK(ready,544) HEAT(blocked,1232) MAIN(running,3788) IDLE(ready,200)
      Owned mutexes:
      === Platform ===
      Last reset 03:39:09 ago, cause: power up
      Last software reset at 2020-04-20 16:40, reason: User, spinning module GCodes, available RAM 6444 bytes (slot 0)
      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
      Error status: 0
      Free file entries: 9
      SD card 0 detected, interface speed: 20.0MBytes/sec
      SD card longest block write time: 11.2ms, max retries 0
      MCU temperature: min 13.2, current 21.4, max 23.3
      Supply voltage: min 23.9, current 24.2, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
      Driver 0: ok, SG min/max 0/350
      Driver 1: ok, SG min/max 0/383
      Driver 2: standstill, SG min/max 0/335
      Driver 3: ok, SG min/max 0/1023
      Driver 4: standstill, SG min/max not available
      Date/time: 2020-04-25 21:55:53
      Cache data hit count 4294967295
      Slowest loop: 22.46ms; fastest: 0.07ms
      I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0
      === Move ===
      Hiccups: 0, StepErrors: 0, LaErrors: 241, FreeDm: 145, MinFreeDm: 133, MaxWait: 522168ms, Underruns: 0, 0
      Scheduled moves: 279730, completed moves: 279701
      Bed compensation in use: mesh
      Bed probe heights: 0.000 0.000 0.000 0.000 0.000
      === Heat ===
      Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
      Heater 0 is on, I-accum = 0.0
      Heater 1 is on, I-accum = 0.3
      === GCodes ===
      Segments left: 1
      Stack records: 1 allocated, 0 in use
      Movement lock held by null
      http is idle in state(s) 0
      telnet is idle in state(s) 0
      file is doing "G1 X67.792 Y284.704 E0.04186" in state(s) 0
      serial is idle in state(s) 0
      aux is idle in state(s) 0
      daemon is idle in state(s) 0
      queue is idle in state(s) 0
      autopause is idle in state(s) 0
      Code queue is empty.
      === Network ===
      Slowest loop: 46.17ms; fastest: 0.00ms
      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
      HTTP sessions: 1 of 8

      • WiFi -
        Network state is running
        WiFi module is connected to access point
        Failed messages: pending 0, notready 0, noresp 0
        WiFi firmware version 1.22
        WiFi MAC address ec:fa:bc:2d:dd:0f
        WiFi Vcc 3.39, reset reason Turned on by main processor
        WiFi flash size 4194304, free heap 27952
        WiFi IP address 192.168.1.44
        WiFi signal strength -77dBm, reconnections 0, sleep mode modem
        Socket states: 0 0 0 0 0 0 0 0
        === Filament sensors ===
        Extruder 0 sensor: ok

      M122 P104 S[FILE SIZE IN MB]
      SD write speed for 1.0Mbyte file was 2.23MBytes/sec

      Three things that I noticed.

      First is that there arent any hiccups, so I think that I can rule out microstepping issues (Potentially?).

      Second is that the SD card appears to be okay. Please let me know if this is incorrect.

      Third is that there appear to be LaErrors (I have no clue what those actually represent though, lol) and a relatively high MaxWait time (also have no clue what this means other than that the Duet is waiting for commands (Maybe?)).

      Slicer is Cura. Outer wall acceleration is 300 mm/s^2, outer wall jerk is 5 mm/s. Ive run these parameters on other printers (UM2 Ext.+) without issue. "Compensate wall overlaps" is enabled, and Ive heard that there may be issues with this, but I havent noticed issues on other printers.

      Please let me know what may be the cause of this issue. I really have no clue what is going on. Any help is greatly appreciated! 🙂

      Phaedruxundefined 1 Reply Last reply Reply Quote 0
      • brismaundefined
        brisma
        last edited by

        M566 X480.00 Y480.00 Z30.00 E10000.00 ; Set maximum instantaneous speed changes (mm/min)
        

        166mm/s of jerk on extruder? Try lowering to 600 (10mm/s) 🙂

        M906 X1400.00 Y1400.00 Z900.00 E1428.00 I30
        

        Why 1428 (that's useless) and not 1400 on extruder?

        Are you on direct or bowden system? Can you try a print without PA?
        Just comment this line:

        ; Pressure Advance
        ; M572 D0 S0.05 ; Enable pressure advance and set it. Marlin setup used a K of 0.03-0.05. HatchBox Wood K=0.03.
        
        CCS86undefined 1 Reply Last reply Reply Quote 0
        • dc42undefined
          dc42 administrators
          last edited by

          The LA errors should't be there. Please upgrade to firmware 2.05.1 and try again.

          Duet WiFi hardware designer and firmware engineer
          Please do not ask me for Duet support via PM or email, use the forum
          http://www.escher3d.com, https://miscsolutions.wordpress.com

          1 Reply Last reply Reply Quote 0
          • Charlieundefined
            Charlie
            last edited by

            @dc42 Thank you very much for your reply. I updated to 2.05.1. Unfortunately the problem persists.

            M122
            === Diagnostics ===
            RepRapFirmware for Duet 2 WiFi/Ethernet version 2.05.1 running on Duet WiFi 1.02 or later
            Board ID: 08DGM-917DA-G4MS8-6J1DD-3S46R-1STHB
            Used output buffers: 3 of 24 (8 max)
            === RTOS ===
            Static ram: 25712
            Dynamic ram: 93224 of which 0 recycled
            Exception stack ram used: 432
            Never used ram: 11704
            Tasks: NETWORK(ready,628) HEAT(blocked,1232) MAIN(running,3736) IDLE(ready,160)
            Owned mutexes:
            === Platform ===
            Last reset 00:13:52 ago, cause: power up
            Last software reset at 2020-04-20 16:40, reason: User, spinning module GCodes, available RAM 6444 bytes (slot 0)
            Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
            Error status: 0
            Free file entries: 9
            SD card 0 detected, interface speed: 20.0MBytes/sec
            SD card longest block write time: 9.7ms, max retries 0
            MCU temperature: min 14.6, current 21.4, max 21.4
            Supply voltage: min 23.9, current 24.2, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
            Driver 0: ok, SG min/max 16/317
            Driver 1: ok, SG min/max 48/382
            Driver 2: standstill, SG min/max 0/339
            Driver 3: standstill, SG min/max 0/1023
            Driver 4: standstill, SG min/max not available
            Date/time: 2020-04-26 14:52:04
            Cache data hit count 2367661333
            Slowest loop: 24.37ms; fastest: 0.07ms
            I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
            === Move ===
            Hiccups: 0, FreeDm: 157, MinFreeDm: 103, MaxWait: 193254ms
            Bed compensation in use: mesh, comp offset 0.000
            === DDARing ===
            Scheduled moves: 7078, completed moves: 7070, StepErrors: 0, LaErrors: 9, Underruns: 0, 0
            === Heat ===
            Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
            Heater 0 is on, I-accum = 0.0
            Heater 1 is on, I-accum = 0.3
            === GCodes ===
            Segments left: 1
            Stack records: 1 allocated, 0 in use
            Movement lock held by null
            http is idle in state(s) 0
            telnet is idle in state(s) 0
            file is doing "G1 F4200 X238.49 Y261.575 E1.08288" in state(s) 0
            serial is idle in state(s) 0
            aux is idle in state(s) 0
            daemon is idle in state(s) 0
            queue is idle in state(s) 0
            autopause is idle in state(s) 0
            Code queue is empty.
            === Network ===
            Slowest loop: 22.61ms; fastest: 0.00ms
            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
            HTTP sessions: 1 of 8

            • WiFi -
              Network state is running
              WiFi module is connected to access point
              Failed messages: pending 0, notready 0, noresp 0
              WiFi firmware version 1.22
              WiFi MAC address ec:fa:bc:2d:dd:0f
              WiFi Vcc 3.39, reset reason Turned on by main processor
              WiFi flash size 4194304, free heap 29640
              WiFi IP address 192.168.1.44
              WiFi signal strength -75dBm, reconnections 0, sleep mode modem
              Socket states: 0 0 0 0 0 0 0 0
              === Filament sensors ===
              Extruder 0 sensor: ok

            There are less LA Errors, but this was also only a few minutes into the print. Also, what specifically are LA Errors?

            Also appears to be "MaxWait: 193254ms." Is this okay? What specifically does this mean?

            1 Reply Last reply Reply Quote 0
            • NitroFreakundefined
              NitroFreak
              last edited by

              I have the same problem, the printhead stops randomly when extruding, producing blobs and a highly irregular surface.
              IMG_8498.JPG IMG_8499.JPG
              The face shield perimeter in the middle is printed at 30mm/s, the right one is printed at 80mm/s. It gets much worse.
              I then tried to replicate it with a 100mm circle printed with two perimeters at 80mm/s and one could easily see the printhead stopping mid line. How can that be? None of the blobs are a start/stop line.

              M122
              === Diagnostics ===
              RepRapFirmware for Duet 2 WiFi/Ethernet version 2.03 running on Duet WiFi 1.02 or later
              Board ID: 08DGM-917NK-F23T0-6J9DJ-3S86S-TWBWD
              Used output buffers: 3 of 24 (16 max)
              === RTOS ===
              Static ram: 25680
              Dynamic ram: 94004 of which 0 recycled
              Exception stack ram used: 476
              Never used ram: 10912
              Tasks: NETWORK(ready,524) HEAT(blocked,812) MAIN(running,3744) IDLE(ready,160)
              Owned mutexes:
              === Platform ===
              Last reset 08:05:39 ago, cause: power up
              Last software reset at 2020-03-17 21:06, reason: User, spinning module GCodes, available RAM 10944 bytes (slot 2)
              Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
              Error status: 16
              Free file entries: 10
              SD card 0 detected, interface speed: 20.0MBytes/sec
              SD card longest block write time: 0.0ms, max retries 0
              MCU temperature: min 40.3, current 42.4, max 44.1
              Supply voltage: min 24.3, current 24.6, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
              Driver 0: standstill, SG min/max 0/458
              Driver 1: standstill, SG min/max 0/467
              Driver 2: standstill, SG min/max 0/275
              Driver 3: standstill, SG min/max 0/1023
              Driver 4: standstill, SG min/max not available
              Date/time: 2020-04-26 21:28:53
              Cache data hit count 4294967295
              Slowest loop: 47.11ms; fastest: 0.08ms
              I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
              === Move ===
              Hiccups: 38319, FreeDm: 169, MinFreeDm: 133, MaxWait: 19487ms
              Bed compensation in use: none, comp offset 0.000
              === DDARing ===
              Scheduled moves: 5, completed moves: 5, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
              === Heat ===
              Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
              Heater 0 is on, I-accum = 0.3
              Heater 1 is on, I-accum = 0.3
              === GCodes ===
              Segments left: 0
              Stack records: 1 allocated, 0 in use
              Movement lock held by null
              http is idle in state(s) 0
              telnet is idle in state(s) 0
              file is idle in state(s) 0
              serial is idle in state(s) 0
              aux is idle in state(s) 0
              daemon is idle in state(s) 0
              queue is idle in state(s) 0
              autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 201.17ms; fastest: 0.08ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
              HTTP sessions: 1 of 8

              • WiFi -
                Network state is running
                WiFi module is connected to access point
                Failed messages: pending 0, notready 0, noresp 18580
                WiFi firmware version 1.23
                WiFi MAC address b4:e6:2d:52:f6:45
                WiFi Vcc 3.35, reset reason Turned on by main processor
                WiFi flash size 4194304, free heap 24632
                WiFi IP address 192.168.0.93
                WiFi signal strength -61dBm, reconnections 0, sleep mode modem
                Socket states: 0 0 0 0 0 0 0 0
              1 Reply Last reply Reply Quote 0
              • Charlieundefined
                Charlie
                last edited by

                @brisma Thank you for your response! You bring up some really good points.

                Regarding the overzealous extruder jerk, Ive been told that its too high ever since I found that I could mess with it! I was under the assumption that the print moves would be dictated by the speed, acceleration, and jerk of the least responsive axis (at least I thought that was correct in Marlin). Therefore, I wanted to make sure that the extruder was unlikely to be the least responsive axis. Is this incorrect? Or maybe I shouldn't be considering it in that way?

                Regarding the M906, I was just making it 85% of the max motor current (which is 1680). I could change it to 1400, though Im not sure that it would change much (though I could be very mistaken!).

                My setup is Direct Drive. E3D Titan Aqua to a Supervolcano running 24V. As represented by the very low pressure advance value, PA isnt doing too much, so I could remove it.

                Thanks again for your time.

                1 Reply Last reply Reply Quote 0
                • Charlieundefined
                  Charlie
                  last edited by

                  @NitroFreak First of all, thank you for printing items to fight COVID!

                  Looks like you have many "Hiccups." In my experience, this has to do with very high microstepping. In your config.g file, what does it show under "M350"? For instance, mine is "M350 X16 Y16 Z16 E16 I1".

                  1 Reply Last reply Reply Quote 1
                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    Yup definitely a large number of hiccups. @NitroFreak usually a result of using too high microstepping. x16 with interpolation to x256 is recommended.

                    Regarding the halting movement behaviour I may have noticed something similar myself on curved surfaces lately but I was also testing a new slicer release and wrote it off as something I had changed there. I did not look at a M122 at the time. I'll keep that in mind on my next print.

                    Z-Bot CoreXY Build | Thingiverse Profile

                    1 Reply Last reply Reply Quote 0
                    • Charlieundefined
                      Charlie
                      last edited by

                      @Phaedrux If the slicer matters, Im running cura 4.6.0 (newest release). Im still getting no hiccups, some LA Errors, and stuttering behavior.

                      1 Reply Last reply Reply Quote 0
                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        I was using this version of Cura which is built on 4.6

                        https://www.dropbox.com/sh/s43vqzmi4d2bqe2/AAADdYdSu9iwcKa0Knqgurm4a?dl=0&lst=

                        Z-Bot CoreXY Build | Thingiverse Profile

                        1 Reply Last reply Reply Quote 0
                        • NitroFreakundefined
                          NitroFreak
                          last edited by

                          @Phaedrux said in Print stuttering around curves, LaErrors:

                          Yup definitely a large number of hiccups. @NitroFreak usually a result of using too high microstepping. x16 with interpolation to x256 is recommended.

                          Regarding the halting movement behaviour I may have noticed something similar myself on curved surfaces lately but I was also testing a new slicer release and wrote it off as something I had changed there. I did not look at a M122 at the time. I'll keep that in mind on my next print.

                          I have nothing out of the ordinary, apart from an external Y servo that i run with no microstepping.
                          Also two X axis motors that i do indeed run with x16 and interpolation.

                          M350 Y1 Z64 ;E16:16I0 ; Configure microstepping without interpolation
                          M350 X16:16 I1 E16:16 I1 ; Configure microstepping with interpolation
                          M92 X88.89 Y360.00 Z3200.00 E411:430 ; Set steps per mm, mk8 extruder 94.3

                          Any idea what else it could be?

                          1 Reply Last reply Reply Quote 0
                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            @NitroFreak said in Print stuttering around curves, LaErrors:

                            Z3200.00

                            Are you using z hop or something? I might try dropping the Z axis back to x16.

                            The external stepper could be something but I'm not familiar.

                            Z-Bot CoreXY Build | Thingiverse Profile

                            1 Reply Last reply Reply Quote 0
                            • Charlieundefined
                              Charlie
                              last edited by

                              Are you sure that your M350 commands are all after your M584 commands?

                              1 Reply Last reply Reply Quote 0
                              • Charlieundefined
                                Charlie
                                last edited by

                                As an update, decreasing extruder jerk did not improve or worsen the artifacts. The issue persists.

                                1 Reply Last reply Reply Quote 0
                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  I'm about to try a print. The mesh isn't very high resolution though so the curves are pretty facetted.

                                  Z-Bot CoreXY Build | Thingiverse Profile

                                  1 Reply Last reply Reply Quote 0
                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    === DDARing ===
                                    Scheduled moves: 11250, completed moves: 11225, StepErrors: 0, LaErrors: 1, Underruns: 34, 0
                                    

                                    Only a few minutes into the print and there is 1 La error and a few under runs.

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    1 Reply Last reply Reply Quote 0
                                    • Charlieundefined
                                      Charlie
                                      last edited by

                                      Changing X, Y, and E instantaneous speed (jerk) settings dramatically (both high and low) did not affect the outcome.

                                      IMG_8301.jpg

                                      Changing pressure advance mid print (through M572 command on the gcode console during the print) also did not change the fact that it still stopped while traveling around the large radius arcs.

                                      Below is a link to the GCode for the affected print.

                                      https://drive.google.com/file/d/17gsPftKUcRSPVDl176A_GBqD7sG8GH9i/view?usp=sharing
                                      

                                      Please let me know if there is a better way to post gcode, as it exceeded the maximum file size for uploading.

                                      1 Reply Last reply Reply Quote 0
                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        From the end of the print:

                                        === DDARing === Scheduled moves: 18, completed moves: 18, StepErrors: 0, LaErrors: 14, Underruns: 698, 0

                                        m122
                                        === Diagnostics ===
                                        RepRapFirmware for Duet 2 WiFi/Ethernet version 2.05.1 running on Duet WiFi 1.02 or later
                                        Board ID: 08DDM-9FAM2-LW4SD-6JKF0-3SN6N-T2ZBY
                                        Used output buffers: 1 of 24 (16 max)
                                        === RTOS ===
                                        Static ram: 25712
                                        Dynamic ram: 93328 of which 228 recycled
                                        Exception stack ram used: 544
                                        Never used ram: 11260
                                        Tasks: NETWORK(ready,628) HEAT(blocked,1176) MAIN(running,3728) IDLE(ready,160)
                                        Owned mutexes:
                                        === Platform ===
                                        Last reset 03:48:36 ago, cause: power up
                                        Last software reset at 2020-03-30 17:04, reason: User, spinning module GCodes, available RAM 11148 bytes (slot 2)
                                        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
                                        Error status: 0
                                        Free file entries: 10
                                        SD card 0 detected, interface speed: 20.0MBytes/sec
                                        SD card longest block write time: 0.0ms, max retries 0
                                        MCU temperature: min 27.2, current 29.2, max 30.7
                                        Supply voltage: min 23.7, current 24.0, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                                        Driver 0: standstill, SG min/max 0/1023
                                        Driver 1: standstill, SG min/max 0/1023
                                        Driver 2: standstill, SG min/max 0/279
                                        Driver 3: standstill, SG min/max 0/1023
                                        Driver 4: standstill, SG min/max not available
                                        Date/time: 2020-04-26 19:43:09
                                        Cache data hit count 4294967295
                                        Slowest loop: 67.26ms; fastest: 0.07ms
                                        I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                                        === Move ===
                                        Hiccups: 0, FreeDm: 160, MinFreeDm: 98, MaxWait: 60049ms
                                        Bed compensation in use: mesh, comp offset 0.000
                                        === DDARing ===
                                        Scheduled moves: 18, completed moves: 18, StepErrors: 0, LaErrors: 14, Underruns: 698, 0
                                        === Heat ===
                                        Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
                                        Heater 0 is on, I-accum = 0.2
                                        Heater 1 is on, I-accum = 0.4
                                        === GCodes ===
                                        Segments left: 0
                                        Stack records: 3 allocated, 0 in use
                                        Movement lock held by null
                                        http is idle in state(s) 0
                                        telnet is idle in state(s) 0
                                        file is idle in state(s) 0
                                        serial is idle in state(s) 0
                                        aux is idle in state(s) 0
                                        daemon is idle in state(s) 0
                                        queue is idle in state(s) 0
                                        autopause is idle in state(s) 0
                                        Code queue is empty.
                                        === Network ===
                                        Slowest loop: 200.47ms; fastest: 0.08ms
                                        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
                                        HTTP sessions: 1 of 8
                                        - WiFi -
                                        Network state is running
                                        WiFi module is connected to access point 
                                        Failed messages: pending 0, notready 0, noresp 2
                                        WiFi firmware version 1.23
                                        WiFi MAC address 5c:cf:7f:ef:4a:74
                                        WiFi Vcc 3.31, reset reason Turned on by main processor
                                        WiFi flash size 4194304, free heap 24512
                                        WiFi IP address 10.10.0.95
                                        WiFi signal strength -44dBm, reconnections 0, sleep mode modem
                                        Socket states: 0 0 0 0 0 0 0 0
                                        

                                        I did not have any of the pausing I saw previously on the more detailed mesh.

                                        Z-Bot CoreXY Build | Thingiverse Profile

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                                        • Charlieundefined
                                          Charlie
                                          last edited by

                                          @Phaedrux Hmmm, seems like you still have LA Errors, though you didn't have any pausing. If you are using Cura, may I ask what your Maximum Resolution, Maximum Travel Resolution, and Maximum Deviation settings are? Mine are 0.833 mm, 0.7 mm, and 0.015 mm respectively. Do you think that this may be the cause of my issue? They may be too low.

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                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            No stutters this time, but the model was very low res by comparison. In the next couple days I'll be printing another bunch of high resolution curved models. I'll check again then.

                                            Max res : 0.05
                                            Max travel res 0.1094
                                            Max deviation 0.05

                                            And this last print was with that custom cura build from just the other day. Maybe give that build a try.

                                            Z-Bot CoreXY Build | Thingiverse Profile

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