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Not Homing correctly At all. and nozzle issues

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  • undefined
    Phaedrux Moderator @moe.adams9093
    last edited by 1 May 2020, 22:50

    @moe-adams9093 said in Not Homing correctly At all. and nozzle issues:

    ; Drives
    M569 P0 S1 ; physical drive 0 goes forwards
    M569 P1 S1 ; physical drive 1 goes forwards
    M569 P2 S0 ; physical drive 2 goes backwards
    M569 P3 S0 ; physical drive 3 goes backwards
    M584 X0 Y1 Z2 E3 ; set drive mapping

    You're going to need to define drive 4 for use as a second Z axis in config.g and change your bed.g to do the probing for the leveling adjustment.

    ; Drives
    M569 P0 S1 ; physical drive 0 goes forwards (X axis)
    M569 P1 S1 ; physical drive 1 goes forwards (Y axis)
    M569 P2 S0 ; physical drive 2 goes backwards (Z1 axis)
    M569 P3 S0 ; physical drive 3 goes backwards (E axis)
    M569 P4 S0 ; physical drive 4 goes backwards (Z2 axis)
    M584 X0 Y1 Z2:4 E3 ; set drive mapping
    M671 X-20:220 Y0:0 S0.5 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis

    For the points in M671 you need to find the coordinates of your own bed to measure, you can't just use the example points.

    You will connect one Z motor to the Z1 (drive 2), put the jumpers back in the second port. Then connect the other Z motor to the E1 (drive 4)

    alt text

    For bed.g you'll also have to find the points to probe with G30

    G28 ; home
    M401 ; deploy Z probe (omit if using bltouch)
    G30 P0 X20 Y100 Z-99999 ; probe near a leadscrew, half way along Y axis
    G30 P1 X180 Y100 Z-99999 S2 ; probe near a leadscrew and calibrate 2 motors
    M402 ; retract probe (omit if using bltouch)

    The G30 P1 will likely be further to the right on your larger bed so adjust the CX position accordingly.

    Z-Bot CoreXY Build | Thingiverse Profile

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    • undefined
      moe.adams9093
      last edited by 2 May 2020, 05:16

      Thank you very much for all your help. I will make these adjustments tomorrow, but how can I find points in M671 coordinates of my own bed measuring, is their sort of documentation can explain how to find the coordinate positions of my bed. thank you again

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      • undefined
        Phaedrux Moderator
        last edited by 2 May 2020, 05:29

        You just need to choose a point close to the lead screw but still on the bed and both need to be in line on the Y axis.

        Z-Bot CoreXY Build | Thingiverse Profile

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        • undefined
          moe.adams9093
          last edited by 3 May 2020, 05:05

          @Phaedrux said in Not Homing correctly At all. and nozzle issues:

          G28 ; home M401 ; deploy Z probe (omit if using bltouch) G30 P0 X20 Y100 Z-99999 ; probe near a leadscrew, half way along Y axis G30 P1 X180 Y100 Z-99999 S2 ; probe near a leadscrew and calibrate 2 motors M402 ; retract probe (omit if using bltouch)

          THANK YOU. it worked and I found my correct bed coordinate points. do I have to change any config for my BLtouch current settings are

          Z-Probe
          M558 P9 H2 F120 T6000 ; set Z probe type to bltouch and the dive height + speeds
          G31 P500 X0 Y0 Z2 ; set Z probe trigger value, offset and trigger height
          M557 X5:350 Y5:350 S50 ; define mesh grid
          I have version 3

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          • undefined
            Phaedrux Moderator
            last edited by Phaedrux 5 Mar 2020, 17:10 3 May 2020, 17:09

            The dive height is a little low. It should be at least a mm more than the trigger height. Try M558 H3

            Also change G31 P500 to G31 P25

            Have you calibrated our probe and measured the offsets yet?

            https://duet3d.dozuki.com/Wiki/Test_and_calibrate_the_Z_probe

            Z-Bot CoreXY Build | Thingiverse Profile

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            • undefined
              moe.adams9093
              last edited by 4 May 2020, 09:45

              so I have adjusted all the settings accordingly here's a photo of the hight mapScreenshot (4).png so I don't if that's ok or it should be 0 all the way I tried to print a file 340 x 340 and it looks like it's not adjusting probably. here's my updated file config.g

              ; Configuration file for Duet Maestro (firmware version 2.03)
              ; executed by the firmware on start-up
              ;
              ; generated by RepRapFirmware Configuration Tool v2.1.8 on Thu Apr 30 2020 23:57:45 GMT-0500 (Central Daylight Time)

              ; General preferences
              G90 ; send absolute coordinates...
              M83 ; ...but relative extruder moves
              M550 P"Ender5Plus" ; set printer name

              ; Network
              M552 P0.0.0.0 S1 ; enable network and acquire dynamic address via DHCP
              M586 P0 S1 ; enable HTTP
              M586 P1 S0 ; disable FTP
              M586 P2 S0 ; disable Telnet

              ; Drives
              M569 P0 S1 ; physical drive 0 goes forwards
              M569 P1 S1 ; physical drive 1 goes forwards
              M569 P2 S0 ; physical drive 2 goes backwards
              M569 P3 S0 ; physical drive 3 goes backwards
              M569 P4 S0 ; physical drive 4 goes backwards (Z2 axis)
              M584 X0 Y1 Z2:4 E3 ; set drive mapping
              M671 X0:285 Y0:180 S0.5 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis
              M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
              M92 X80.00 Y80.00 Z800.00 E96.00 ; set steps per mm
              M566 X480.00 Y480.00 Z24.00 E300.00 ; set maximum instantaneous speed changes (mm/min)
              M203 X30000.00 Y30000.00 Z600.00 E3000.00 ; set maximum speeds (mm/min)
              M201 X500.00 Y500.00 Z100.00 E5000.00 ; set accelerations (mm/s^2)
              M906 X960 Y980 Z960 E960 I30 ; set motor currents (mA) and motor idle factor in per cent
              M84 S30 ; Set idle timeout

              ; Axis Limits
              M208 X0 Y0 Z0 S1 ; set axis minima
              M208 X365 Y365 Z415 S0 ; set axis maxima

              ; Endstops
              M574 X1 Y1 S1 ; set active low and disabled endstops
              M574 Z1 S2 ; set endstops controlled by probe

              ; Z-Probe
              M558 P9 H3 F120 T6000 ; set Z probe type to bltouch and the dive height + speeds
              G31 P25 X0 Y0 Z1.758 ; set Z probe trigger value, offset and trigger height
              M557 X5:335 Y5:335 S20 ; define mesh grid

              ; Heaters
              M141 H2 ;Assign chamber heater to heater 2
              M307 H2 A11 C99000 D2000 B1 ; chamber heater operates in bang-bang mode
              M305 P2 T10000 B3988 C0 R2200 ; Set thermistor + ADC parameters for bed
              M143 H2 S80 ; set temperature limit for heater 2 to 80C
              M305 P0 T98801 B4138 R2200 ; set thermistor + ADC parameters for heater 0
              M143 H0 S130 ; set temperature limit for heater 0 to 130C
              M305 P1 T98801 B4138 R2200 ; set thermistor + ADC parameters for heater 1
              M143 H1 S300 ; set temperature limit for heater 1 to 300C

              ; Fans
              M106 P0 S0.5 I0 F500 H1 T45 ; set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned on
              M106 P1 S0.5 I0 F500 H1 T45 ; set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on

              ; Tools
              M563 P0 S"Nozzle" D0 H1 F0 ; define tool 0
              G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
              G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

              ; Custom settings are not defined

              ; Miscellaneous
              M501 ; load saved parameters from non-volatile memory
              M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
              T0 ; select first tool

              and file bed.g
              ; bed.g

              G28 ; home
              M401 ; deploy Z probe (omit if using bltouch)
              G30 P0 X0 Y180 Z-99999 ; probe near a leadscrew, half way along Y axis
              G30 P1 X285 Y180 Z-99999 S2 ; probe near a leadscrew and calibrate 2 motors
              M402 ; retract probe (omit if using bltouch)

              G29 S0
              G29 S1

              I don't know if i have to enable some settings to run hight map while it prints maybe from slicer or from DWC. thank you for all your help

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              • undefined
                moe.adams9093
                last edited by 4 May 2020, 09:52

                when I run G32 here's the message I getScreenshot (5).png
                does that meat its successfully calibrated.

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                • undefined
                  moe.adams9093
                  last edited by 4 May 2020, 10:03

                  also here's the message when I run G29. Screenshot (6).png
                  please let me know if that looks good sorry I know I have been asking you a lot. Thanks again

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                  • undefined
                    Phaedrux Moderator
                    last edited by 4 May 2020, 16:27

                    Print a test file like this one with mesh enabled and again disabled. You should be able to tell if it's being applied correctly.

                    bedlevel_nozzle_0.4_200x200-0.3-0.8.stl

                    Z-Bot CoreXY Build | Thingiverse Profile

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                    • undefined
                      moe.adams9093
                      last edited by 6 May 2020, 07:52

                      Yes I did what you told me and it looks like its not working properly. Any other suggestions would be helpful. Thanks

                      undefined 1 Reply Last reply 6 May 2020, 08:50 Reply Quote 0
                      • undefined
                        PaulHew @moe.adams9093
                        last edited by 6 May 2020, 08:50

                        @moe-adams9093 What slicer are you using? Please post your start GCode from your slicer.

                        Regards,
                        Paul

                        RailCore II - Duet Mini + 1LC, Voron V0.1 - Duet Mini
                        Voron 2.4 disassembled..... Waiting for the RailCore Mini....

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                        • undefined
                          Phaedrux Moderator
                          last edited by Phaedrux 5 Jun 2020, 18:12 6 May 2020, 18:07

                          @moe-adams9093 said in Not Homing correctly At all. and nozzle issues:

                          G31 P25 X0 Y0 Z1.758

                          You need to measure your X and Y probe offset otherwise the corrections will be off in X Y position.

                          https://duet3d.dozuki.com/Wiki/Test_and_calibrate_the_Z_probe?revisionid=HEAD#Section_Measuring_Probe_X_Y_Offset

                          The heightmap itself looks ok. After measuring the offset redo the G29 and reprint the test file to see if it's behaving better.

                          Z-Bot CoreXY Build | Thingiverse Profile

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                          • undefined
                            moe.adams9093
                            last edited by 9 May 2020, 06:08

                            Thank you for the additional information so my x offset is 44mm and the y offset is -5mm but when I try to run mesh compensation its starting from 44 to 285 and my actual build volume is 350 x 350 so please correct me on that one am I loosing that left over space since it only probing from 44 to 285. Also when I checked my old configuration from the original bord it says offest x0 y0 z1.78 so I don't if that does matter or not. Please let me know thank you

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