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    Bltouch setup need help

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    • Elvis0zundefined
      Elvis0z
      last edited by

      should I put the same as x and y?

      JoergS5undefined 1 Reply Last reply Reply Quote 0
      • JoergS5undefined
        JoergS5 @Elvis0z
        last edited by JoergS5

        @Elvis0z you have trapezoid at Z, the stepper turns 5 rotations per second, your trapezoid has 2 mm for every rotation, so 10 mm/s, the value for Z should be 600 mm/min. The stepper could run 16 rotations/s maximum, but better be on the safe side.

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        • Elvis0zundefined
          Elvis0z
          last edited by

          Thanks for your help.

          1 Reply Last reply Reply Quote 0
          • Elvis0zundefined
            Elvis0z
            last edited by

            So just to make sure I have to home z before I can do anything else?

            JoergS5undefined 1 Reply Last reply Reply Quote 0
            • Elvis0zundefined
              Elvis0z
              last edited by

              Ahhhhh gets to the same point and deploys probe then nothing like in the video

              JoergS5undefined 1 Reply Last reply Reply Quote 0
              • JoergS5undefined
                JoergS5 @Elvis0z
                last edited by

                @Elvis0z please see above, take 600. 6000 ist too much for the stepper.

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                • JoergS5undefined
                  JoergS5 @Elvis0z
                  last edited by

                  @Elvis0z said in Bltouch setup need help:

                  So just to make sure I have to home z before I can do anything else?

                  the printer want to have homed all axes before it proceeds.

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                  • Elvis0zundefined
                    Elvis0z
                    last edited by

                    G28
                    

                    Error: Z probe was not triggered during probing move
                    Error: Homing failed

                    Just keep getting this error

                    JoergS5undefined 1 Reply Last reply Reply Quote 0
                    • JoergS5undefined
                      JoergS5 @Elvis0z
                      last edited by JoergS5

                      @Elvis0z can you make a M122 after the G28 test please and show?

                      An does G1 Z10 and G1 Z-10 move as expected when you run this commands directly?

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                      • Elvis0zundefined
                        Elvis0z
                        last edited by

                        @JoergS5 said in Bltouch setup need help:

                        G1 Z-10
                        M122
                        === Diagnostics ===
                        RepRapFirmware for Duet 2 WiFi/Ethernet version 3.1.1 running on Duet WiFi 1.02 or later
                        Board ID: 08DGM-9T6BU-FG3SD-6J9D0-3S86Q-1AMBF
                        Used output buffers: 3 of 24 (10 max)
                        === RTOS ===
                        Static ram: 27980
                        Dynamic ram: 93712 of which 44 recycled
                        Exception stack ram used: 264
                        Never used ram: 9072
                        Tasks: NETWORK(ready,384) HEAT(blocked,1224) MAIN(running,1880) IDLE(ready,80)
                        Owned mutexes:
                        === Platform ===
                        Last reset 00:00:35 ago, cause: software
                        Last software reset at 2020-07-09 19:59, reason: User, spinning module GCodes, available RAM 8584 bytes (slot 1)
                        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0xffffffff Task MAIN
                        Error status: 0
                        MCU temperature: min 30.6, current 31.7, max 32.0
                        Supply voltage: min 23.9, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                        Driver 0: standstill, SG min/max not available
                        Driver 1: standstill, SG min/max not available
                        Driver 2: standstill, SG min/max not available
                        Driver 3: standstill, SG min/max not available
                        Driver 4: standstill, SG min/max not available
                        Date/time: 2020-07-09 19:59:45
                        Cache data hit count 60372819
                        Slowest loop: 4.74ms; fastest: 0.13ms
                        I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                        === Storage ===
                        Free file entries: 10
                        SD card 0 detected, interface speed: 20.0MBytes/sec
                        SD card longest read time 3.1ms, write time 0.0ms, max retries 0
                        === Move ===
                        Hiccups: 0(0), FreeDm: 169, MinFreeDm: 169, MaxWait: 0ms
                        Bed compensation in use: none, comp offset 0.000
                        === MainDDARing ===
                        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                        === AuxDDARing ===
                        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                        === Heat ===
                        Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                        === GCodes ===
                        Segments left: 0
                        Movement lock held by null
                        HTTP is idle in state(s) 0
                        Telnet is idle in state(s) 0
                        File is idle in state(s) 0
                        USB is idle in state(s) 0
                        Aux is idle in state(s) 0
                        Trigger is idle in state(s) 0
                        Queue is idle in state(s) 0
                        Daemon is idle in state(s) 0
                        Autopause is idle in state(s) 0
                        Code queue is empty.
                        === Network ===
                        Slowest loop: 41.57ms; fastest: 0.00ms
                        Responder states: HTTP(2) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                        HTTP sessions: 1 of 8

                        • WiFi -
                          Network state is active
                          WiFi module is connected to access point
                          Failed messages: pending 0, notready 0, noresp 0
                          WiFi firmware version 1.23
                          WiFi MAC address ec:fa:bc:2d:b3:11
                          WiFi Vcc 3.36, reset reason Unknown
                          WiFi flash size 4194304, free heap 20056
                          WiFi IP address 192.168.50.68
                          WiFi signal strength -46dBm, reconnections 0, sleep mode modem
                          Socket states: 0 0 0 0 0 0 0 0

                        09/07/2020, 20:00:48 G1 Z10
                        Error: G0/G1: insufficient axes homed
                        09/07/2020, 20:01:17 G1 Z-10
                        Error: G0/G1: insufficient axes homed

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                        • Elvis0zundefined
                          Elvis0z
                          last edited by

                          When I do a G28 command once z probe deploys the console just spins around and I can't put any commands in till I restart control board

                          JoergS5undefined 1 Reply Last reply Reply Quote 0
                          • JoergS5undefined
                            JoergS5 @Elvis0z
                            last edited by

                            @Elvis0z first sorry for my G1 Z-10 and G1 Z10. This will not work because Z is not homed. The correct commands are G1 H2 Z-10 and H1 H2 Z10 to move even when the Z is not homed. Just to check Z can move at all at this position.

                            I was searching what this fast white LED blinking means, but I can only find fast red blinking (which would be eg white and black cables switched).

                            Can you please make an image of the wiring of the Duet Wifi and the cables at the 5-pin connector of the BLTouch?

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                            • Elvis0zundefined
                              Elvis0z
                              last edited by

                              @JoergS5 said in Bltouch setup need help:

                              G1 H2 Z-10

                              Yep moves up and down with new commands

                              JoergS5undefined 1 Reply Last reply Reply Quote 0
                              • JoergS5undefined
                                JoergS5 @Elvis0z
                                last edited by JoergS5

                                @Elvis0z I have no more ideas.
                                Two things I found in my research:

                                • often it was a wiring problem. Wrong wiring, wiring or connector broke or disturbance by heat or magnets
                                • on reddit was a report of a damaged charge of BLtouch 3.1. But you tried 2 BLtouch, I think probability is low for this reason

                                I have only one idea left: please recheck wiring and connections. And the other idea to find out the reason for the error message of M98 P"config.g".

                                If I have a new idea, I'll tell you.

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                                • Elvis0zundefined
                                  Elvis0z
                                  last edited by

                                  Wiring for bltouch

                                  bltouch.wire.jpg bltouch.wire.1.jpg
                                  bltouch.wire.2.jpg

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                                  • Elvis0zundefined
                                    Elvis0z
                                    last edited by

                                    Black wire is connected to white
                                    Blue wire is connected to black

                                    JoergS5undefined 2 Replies Last reply Reply Quote 0
                                    • JoergS5undefined
                                      JoergS5 @Elvis0z
                                      last edited by

                                      @Elvis0z looks all ok.

                                      1 Reply Last reply Reply Quote 0
                                      • JoergS5undefined
                                        JoergS5 @Elvis0z
                                        last edited by

                                        @Elvis0z what you can try is the G30 has some options:
                                        https://duet3d.dozuki.com/Wiki/Gcode#Section_G30_Single_Z_Probe
                                        e.g. you could try the
                                        G30 P0 X20 Y50 Z-99999
                                        or
                                        G30 S-1
                                        etc.
                                        and try to find out why Z is not moving with the G30 without parameters.

                                        I would run homeall to home X and Y and position in the middle of the bed, comment out the rest of homall and make the tests with G30 from the console input field.

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                                        • Elvis0zundefined
                                          Elvis0z
                                          last edited by

                                          Thanks for your help so far. Bit of a mystery

                                          1 Reply Last reply Reply Quote 0
                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            Does your Z axis move at all? Does it raise and lower slightly when you do home all?

                                            If you send G92 Z100 to mark it as homed and at position 100mm, then send G91 for relative moves, and then G1 Z10 it should move up 10mm.

                                            Z-Bot CoreXY Build | Thingiverse Profile

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