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    unusual/unnerving noises + error codes

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    • PR1ORundefined
      PR1OR @Phaedrux
      last edited by

      @Phaedrux Thanks! and apologises for the screenshot i will know for the future (rofl)

      so that config.json doesnt download unfortunately, however i have seen that the pre configured ender 3 pro so i will probably use that. I have just the ender 3 but i believe they use the same original board and believe that the are the same except the frame is more sterdy and the PCU is better. but will check the measurements because the print sizes maybe slightly different also. from what ive read on the above links it should just be slight amendments to the gcodes which doesnt seem tooo difficult :s but makinig sure i know what im doing

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      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        @Phaedrux said in unusual/unnerving noises + error codes:

        config.json

        You might have to right click and save as and rename it config.json. I just tested it and it works.

        the only thing I changed was the board type, the firmware version, and the bltouch, plus a few other minor things.

        Z-Bot CoreXY Build | Thingiverse Profile

        PR1ORundefined 1 Reply Last reply Reply Quote 0
        • PR1ORundefined
          PR1OR @Phaedrux
          last edited by

          @Phaedrux So i have not uploaded this why is great. however when just trying to home the x axis. it keeps eratically shaking and throwing out these error codes. I have looked for the G1 code but it only seems to be on the tool section of the config.g so im now confused again.

          Can you help?

          Warning: Obsolete use of S parameter on G1 command. Use H parameter instead.

          G28 X Warning: Obsolete use of S parameter on G1 command. Use H parameter instead.

          jay_s_ukundefined 1 Reply Last reply Reply Quote 0
          • jay_s_ukundefined
            jay_s_uk @PR1OR
            last edited by

            @PR1OR check your homing files and everywhere the G1 command uses an S command e.g.

            G1 S1 X-500
            

            change it to H

            G1 H1 X-500
            

            Check your homeall.g, homex.g, homey.g and homez.g

            Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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            • PR1ORundefined
              PR1OR @jay_s_uk
              last edited by

              @jay_s_uk said in unusual/unnerving noises + error codes:

              here the G1

              this has removed this message. thanks!

              now it just shakes still for a while then gives me this

              G28 X
              Error: Homing failed

              PR1ORundefined 1 Reply Last reply Reply Quote 0
              • PR1ORundefined
                PR1OR @PR1OR
                last edited by

                if i try and home all i get the same weird shaking on the X and Y axis the Z doesnt move and i eventually get this error message

                G28
                Error: G0/G1: insufficient axes homed

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                • jay_s_ukundefined
                  jay_s_uk
                  last edited by

                  i would suggest looking at your wiring for the x axis motor then.
                  My guess is you have some of the cables mixed up.
                  I would suggest reading this https://duet3d.dozuki.com/Wiki/Choosing_and_connecting_stepper_motors#Section_Connecting_stepper_motors

                  Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                  PR1ORundefined 1 Reply Last reply Reply Quote 1
                  • PR1ORundefined
                    PR1OR @jay_s_uk
                    last edited by

                    @jay_s_uk So after following the link i can confirm that all motors are connected correctly now and sound alot better. Now to the end stops + Probe.

                    Obviously at the moment i still cant home the axis (X and Y) because the end stops seem to not be working. Ive done some reading and found that M574 give a status, which is below. However when putting the gcode in it send a message saying 'Response too long see console'

                    m574
                    

                    Endstop configuration:
                    X: low end motor stall (any motor)
                    Y: low end motor stall (any motor)
                    Z: low end Z probe

                    any ideas?

                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                    • jay_s_ukundefined
                      jay_s_uk
                      last edited by

                      can you post your latest config.g?
                      That response seems to indicate that you're trying to use stall detection rather than an actual endstop

                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                      • Phaedruxundefined
                        Phaedrux Moderator @PR1OR
                        last edited by

                        @PR1OR said in unusual/unnerving noises + error codes:

                        'Response too long see console'

                        And if you go to the console do you see the result?

                        How do you have the endstops wired? The two wires from the endstops should be connected to the outer two pins of the board connector. Doesn't really matter which wire goes where.

                        https://duet3d.dozuki.com/Guide/Ender+3+Pro+and+Duet+Maestro+Guide+Part+1:+Wiring/37#s119

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • PR1ORundefined
                          PR1OR
                          last edited by

                          ![0_1600205801008_IMG_1528.JPEG](Uploading 100%) @Phaedrux said in unusual/unnerving noises + error codes:

                          w do you have the endstops wired

                          so that was the result :s

                          Screenshot 2020-09-15 at 22.33.45.png

                          Below is a picture of the wiring, ive been using dupont wire until ive made sure they are wired correctly. but from what you are saying the seem to be fine. The LEDs are on (green, i read somewhere they should be red but i assume this was an old/new board) when the the endstop switch isnt pressed. When it is it turns off. So i found from wiring diagram that the LEDs didnt correspond to the plugs like it does in the diagram

                          Untitled.png

                          PR1ORundefined 1 Reply Last reply Reply Quote 0
                          • PR1ORundefined
                            PR1OR @PR1OR
                            last edited by

                            just had a thought and checked the axis limits as the ender 3 pro has a bigger print area. i have now updated that but still having issues

                            PR1ORundefined 1 Reply Last reply Reply Quote 0
                            • PR1ORundefined
                              PR1OR @PR1OR
                              last edited by

                              could it be something to do with the gcodes for the end stops?

                              Like the changing S to H?

                              ; Endstops
                              M574 X1 Y1 S3 ; set endstops controlled by motor stall detection
                              M574 Z1 S2 ; set endstops controlled by probe

                              Phaedruxundefined 1 Reply Last reply Reply Quote 0
                              • Phaedruxundefined
                                Phaedrux Moderator @PR1OR
                                last edited by

                                @PR1OR said in unusual/unnerving noises + error codes:

                                ; Endstops
                                M574 X1 Y1 S3 ; set endstops controlled by motor stall detection

                                S3 is stall detection. Try S1.

                                Z-Bot CoreXY Build | Thingiverse Profile

                                PR1ORundefined 1 Reply Last reply Reply Quote 0
                                • PR1ORundefined
                                  PR1OR @Phaedrux
                                  last edited by

                                  @Phaedrux updated to S1 and i got this

                                  G28
                                  Error: Failed to enable endstops

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                                  • PR1ORundefined
                                    PR1OR
                                    last edited by

                                    however i played with it a little and S2 works but it only moves each axis by a couple of mm before stoping

                                    but it does say its homed which i think is getting somewhere

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                                    • Phaedruxundefined
                                      Phaedrux Moderator
                                      last edited by Phaedrux

                                      ; Endstops
                                      M574 X1 S1 P"xstop" ; configure active-high endstop for low end on X via pin xstop
                                      M574 Y1 S1 P"ystop" ; configure active-high endstop for low end on Y via pin ystop

                                      Try that instead

                                      It looks like you had stall detection for homing selected in the configurator so it didn't have any endstop switches defined.

                                      Z-Bot CoreXY Build | Thingiverse Profile

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                                      • ziggymanpopoundefined
                                        ziggymanpopo
                                        last edited by

                                        From what i seen in the video im wondering are you sure the z stepper is wired correctly
                                        It sounds like one of the steppers is not paired properly y moves then x .... does it start the noise before it hits the x stop?? If so you wont know the z is correct untill it hits the x stop if the shaking starts then ...when you hit the xstop i would say the z stepper is causing the problem with the strpper fighting itself... i noticed that the x gantry didnt start down. It might be the video. Or just me 😁 ill watch it again

                                        PR1ORundefined 1 Reply Last reply Reply Quote 0
                                        • ziggymanpopoundefined
                                          ziggymanpopo
                                          last edited by

                                          What i do is start homming then manualy trip the limit to see if it in fact work.. just cause the led goes out doent mean the g code responded

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                                          • PR1ORundefined
                                            PR1OR @Phaedrux
                                            last edited by

                                            @Phaedrux said in unusual/unnerving noises + error codes:

                                            ; Endstops
                                            M574 X1 S1 P"xstop" ; configure active-high endstop for low end on X via pin xstop
                                            M574 Y1 S1 P"ystop" ; configure active-high endstop for low end on Y via pin ystop

                                            Perfect thank you!! this has worked!! i can now home my X and Y axis

                                            is there anything for the Z probe though?

                                            i get this as a return when homing all

                                            Error: in file macro line 9: G30: Z probe 0 not found
                                            Error: Homing failed

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