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Steps per mm keep changing

Scheduled Pinned Locked Moved
Tuning and tweaking
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  • undefined
    fcwilt
    last edited by 27 Dec 2020, 18:53

    I used these for my belt driven Z axis conversion.

    The 5-to-1 is a true 5-to-1.

    They have a similar "economy" line product which is not.

    Frederick

    Printers: a small Utilmaker style, a small CoreXY and a E3D MS/TC setup. Various hotends. Using Duet 3 hardware running 3.4.6

    1 Reply Last reply Reply Quote 0
    • undefined
      JoergS5
      last edited by 27 Dec 2020, 19:06

      yes, looks like a true 5:1

      1 Reply Last reply Reply Quote 0
      • undefined
        JoergS5 @akhilnex
        last edited by 27 Dec 2020, 19:12

        @akhilnex did you check M122 after running the steppers for some time? M122 reports several possible problems, please post the result. (one is hiccups, but also stepper problems, voltage problems etc.).

        undefined 1 Reply Last reply 27 Dec 2020, 19:16 Reply Quote 1
        • undefined
          akhilnex @JoergS5
          last edited by 27 Dec 2020, 19:16

          @JoergS5 M122
          === Diagnostics ===
          RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (standalone mode)
          Board ID: 08DJM-956L2-G43S8-6J9D0-3S46Q-9U2GD
          Used output buffers: 3 of 40 (40 max)
          === RTOS ===
          Static ram: 154604
          Dynamic ram: 162740 of which 20 recycled
          Exception stack ram used: 376
          Never used ram: 75476
          Tasks: NETWORK(ready,356) ETHERNET(blocked,436) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1424) TMC(blocked,60) MAIN(running,4512) IDLE(ready,76)
          Owned mutexes:
          === Platform ===
          Last reset 00:31:39 ago, cause: software
          Last software reset at 2020-12-27 10:43, reason: User, spinning module GCodes, available RAM 75476 bytes (slot 3)
          Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
          Error status: 4
          MCU temperature: min 40.6, current 41.1, max 41.5
          Supply voltage: min 24.0, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
          12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
          Driver 0: standstill, reads 20644, writes 14 timeouts 0, SG min/max 0/0
          Driver 1: standstill, reads 20632, writes 27 timeouts 0, SG min/max 0/81
          Driver 2: standstill, reads 20645, writes 14 timeouts 0, SG min/max 0/0
          Driver 3: standstill, reads 20646, writes 14 timeouts 0, SG min/max 0/0
          Driver 4: standstill, reads 20646, writes 14 timeouts 0, SG min/max 0/0
          Driver 5: standstill, reads 20634, writes 27 timeouts 0, SG min/max 0/431
          Date/time: 1970-01-01 00:00:00
          Slowest loop: 999.77ms; fastest: 0.13ms
          === Storage ===
          Free file entries: 10
          SD card 0 detected, interface speed: 25.0MBytes/sec
          SD card longest read time 2.8ms, write time 29.6ms, max retries 0
          === Move ===
          Hiccups: 0(0), FreeDm: 375, MinFreeDm: 373, MaxWait: 1347113ms
          Bed compensation in use: none, comp offset 0.000
          === MainDDARing ===
          Scheduled moves: 12, completed moves: 12, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
          === AuxDDARing ===
          Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
          === Heat ===
          Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
          === GCodes ===
          Segments left: 0
          Movement lock held by null
          HTTP is idle in state(s) 0
          Telnet is idle in state(s) 0
          File is idle in state(s) 0
          USB is idle in state(s) 0
          Aux is idle in state(s) 0
          Trigger is idle in state(s) 0
          Queue is idle in state(s) 0
          LCD is idle in state(s) 0
          SBC is idle in state(s) 0
          Daemon is idle in state(s) 0
          Aux2 is idle in state(s) 0
          Autopause is idle in state(s) 0
          Code queue is empty.
          === Network ===
          Slowest loop: 57.01ms; fastest: 0.03ms
          Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
          HTTP sessions: 1 of 8

          • Ethernet -
            State: active
            Error counts: 0 0 0 0 0
            Socket states: 5 2 2 2 2 0 0 0
            === CAN ===
            Messages sent 7600, longest wait 0ms for type 0
            === Linux interface ===
            State: 0, failed transfers: 0
            Last transfer: 1899941ms ago
            RX/TX seq numbers: 0/1
            SPI underruns 0, overruns 0
            Number of disconnects: 0
            Buffer RX/TX: 0/0-0
          undefined 1 Reply Last reply 27 Dec 2020, 20:48 Reply Quote 0
          • undefined
            akhilnex
            last edited by akhilnex 27 Dec 2020, 19:47

            Since X,Y and Z gantries are working fine, I am wondering if the NEMA 17 motors on E0,1,2 that I purchased from stepperonline are faulty. I am thinking about ordering atleast one different brand NEMA 17 and a regular extruder hob gear to check and see if it works any better.

            undefined 1 Reply Last reply 3 Jan 2021, 18:46 Reply Quote 0
            • undefined
              akhilnex
              last edited by akhilnex 27 Dec 2020, 20:17

              Can an issue arise from having NEMA 23 and NEMA 17 running on the same board? Should they all be the same 23s or 17s?

              ? 1 Reply Last reply 27 Dec 2020, 20:40 Reply Quote 0
              • ?
                A Former User @akhilnex
                last edited by 27 Dec 2020, 20:40

                @akhilnex said in Steps per mm keep changing:

                Can an issue arise from having NEMA 23 and NEMA 17 running on the same board? Should they all be the same 23s or 17s?

                as long as the individual motors are suited for the drivers then you can mix and match whatever you like. (you'd probably want to have the same specs motor if you run multiple motors in parallel or serial on a single driver)

                the nema number has more to do with physical dimensions than electrical parameters, so not directly relevant even though physically larger motors usually have lower impedance and higher current ratings.

                1 Reply Last reply Reply Quote 1
                • undefined
                  JoergS5 @akhilnex
                  last edited by JoergS5 27 Dec 2020, 20:48

                  @akhilnex M122 looks ok, but only a part of the drivers were used. You can repeat M122 after a longer test again. The short test didn't show problems.

                  I thought about that maybe your multi extruder causes the difference. Depending on pressure and temperature, the speed could vary.

                  undefined 1 Reply Last reply 27 Dec 2020, 21:28 Reply Quote 1
                  • undefined
                    akhilnex @JoergS5
                    last edited by 27 Dec 2020, 21:28

                    @JoergS5 I haven't even gotten to the multi extruder yet. Just trying to get the extruder steppers to run correctly.

                    Once I get accurate reading on the filament movement, my next step will be to pass it through the heated multi-extruder. I guess that's the fun of building random design from scratch as every new step brings a brand new set of challenge! 🙃

                    undefined 1 Reply Last reply 27 Dec 2020, 22:58 Reply Quote 0
                    • undefined
                      JoergS5 @akhilnex
                      last edited by JoergS5 27 Dec 2020, 22:58

                      @akhilnex If the extruder speed is still wrong, you could try separating the problem into it's possible single problems. The problem could be the stepper speed, the hob nut, hob nut slipping, filament slipping, different diameters of the filament.

                      I would use the stepper with a normal pulley first and measure the speed and verify that it has the expected speed. You could use a belt and measure the distance. When it's ok, the problem is behind the stepper shaft. If it's wrong, it can be a configuration, electronics with wiring, stepper, shaft problem.

                      Developing something new is without question an exciting journey for you!

                      undefined 1 Reply Last reply 27 Dec 2020, 23:48 Reply Quote 0
                      • undefined
                        akhilnex @JoergS5
                        last edited by 27 Dec 2020, 23:48

                        @JoergS5 you are right. I will decouple the motor and test everything separately. I am not sure if slippage is an issue as its running over (+10% approx.) rather then under after calibrating for one distance setting.

                        1 Reply Last reply Reply Quote 0
                        • undefined
                          akhilnex
                          last edited by 3 Jan 2021, 16:58

                          Still unsolved: Error stays (2.5mm increase in distance traveled for every 50mm movement) for all steppers on my board:

                          1. Tried to erase and write firmware and new reprap code files.
                          2. Tried different steppers, extrusion hob drivers( with and without).
                          3. Played with speed, current, microsteps (with and without interpolation)

                          f3ab8f3d-0f66-47a9-a445-90c14b4617a4-image.png

                          undefined 2 Replies Last reply 3 Jan 2021, 17:55 Reply Quote 0
                          • undefined
                            JoergS5 @akhilnex
                            last edited by JoergS5 1 Mar 2021, 18:06 3 Jan 2021, 17:55

                            This post is deleted!
                            1 Reply Last reply Reply Quote 0
                            • undefined
                              JoergS5 @akhilnex
                              last edited by 3 Jan 2021, 18:36

                              @akhilnex I want to try to help you, but we should concentrate on one stepper and one driver. Are the values for extruder or the XYZ axes?

                              please tell

                              • config setting for this driver M350, M92
                              • gear or not
                              • if extruder, how do you measure
                              1 Reply Last reply Reply Quote 0
                              • undefined
                                theruttmeister @akhilnex
                                last edited by 3 Jan 2021, 18:46

                                @akhilnex said in Steps per mm keep changing:

                                Since X,Y and Z gantries are working fine, I am wondering if the NEMA 17 motors on E0,1,2 that I purchased from stepperonline are faulty. I am thinking about ordering atleast one different brand NEMA 17 and a regular extruder hob gear to check and see if it works any better.

                                @akhilnex said in Steps per mm keep changing:

                                Still unsolved: Error stays (2.5mm increase in distance traveled for every 50mm movement) for all steppers on my board:

                                Just to check, the distance error is on the extruder motors or on all motors?

                                If its only on the extruder motors, given that its a linear error, I'm going to say you calculated your steps/mm incorrectly (which is common on an extruder). Just do the 'measure 100mm, extrude 100mm, recalculate' dance.

                                Isolate, substitute, verify.

                                1 Reply Last reply Reply Quote 0
                                • undefined
                                  akhilnex
                                  last edited by 25 Feb 2021, 02:36

                                  Gentlemen, Thank you very much for all your help. I knew it was another 250 bucks at risk but I did order a new board and the problem is solved! I can put video file to share the difference. Does any one know if I can send the old board back for the RMA?

                                  Phaedruxundefined 1 Reply Last reply 25 Feb 2021, 19:23 Reply Quote 0
                                  • Phaedruxundefined
                                    Phaedrux Moderator @akhilnex
                                    last edited by 25 Feb 2021, 19:23

                                    @akhilnex When and where did you purchase the first board?

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    undefined 1 Reply Last reply 27 Feb 2021, 05:55 Reply Quote 0
                                    • undefined
                                      akhilnex @Phaedrux
                                      last edited by akhilnex 27 Feb 2021, 05:55

                                      @Phaedrux Filastruder in USA was the supplier I used for both my old and new board. The purchase was first made on 26th May 2020.

                                      1 Reply Last reply Reply Quote 0
                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by 27 Feb 2021, 05:57

                                        Please contact filastruder and initiate a warranty exchange. Include a link to this forum thread as authorization.

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        undefined 1 Reply Last reply 27 Feb 2021, 05:58 Reply Quote 0
                                        • undefined
                                          akhilnex @Phaedrux
                                          last edited by 27 Feb 2021, 05:58

                                          @Phaedrux thank you for your prompt response.

                                          1 Reply Last reply Reply Quote 0
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