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G32 ERROR

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Duet Hardware and wiring
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  • undefined
    Phaedrux Moderator
    last edited by 29 Jan 2021, 16:29

    @moe-adams9093 said in G32 ERROR:

    M574 Z2 S1 p"!exp.e2stop+exp.e3stop+exp.e5stop+exp.e6stop"

    You have one of the switches inverted with !, but not the rest. I assume they are all the same type of switch, yes? If so, you would need a ! before each pin name.

    Z-Bot CoreXY Build | Thingiverse Profile

    undefined 1 Reply Last reply 29 Jan 2021, 16:37 Reply Quote 0
    • undefined
      moe.adams9093
      last edited by 29 Jan 2021, 16:32

      No I will do that tonight when I get back home and do some recrackin.

      1 Reply Last reply Reply Quote 0
      • undefined
        moe.adams9093 @Phaedrux
        last edited by 29 Jan 2021, 16:37

        @Phaedrux man your sharp yes I think thats the problem. I will try it tonight because when I homed only that axis was moving and the rest wasn't moving at all. I thought when I combine all of them they should automatically be the same type. Thanks

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        • undefined
          moe.adams9093
          last edited by 31 Jan 2021, 18:33

          So I went ahead and did combine all of my endstops on a single line in this order

          M574 Z2 S1 p"!exp.e2stop+!exp.e3stop+!exp.e5stop+!exp.e6stop";
          

          it crashed my firmware so I had to do a hard reset and erase firmware and reupload new firmware but this time I did install 3.2. and also I did try just one endstop
          M574 Z2 S1 p"!exp.e2stop . ti did ignore the bed to go down to 500 it went to -500.

          undefined 1 Reply Last reply 31 Jan 2021, 19:22 Reply Quote 0
          • undefined
            Veti
            last edited by 31 Jan 2021, 18:44

            @moe-adams9093 said in G32 ERROR:

            M574 Z2 S1 p

            dunno if it matter but use a capital P

            1 Reply Last reply Reply Quote 0
            • undefined
              moe.adams9093
              last edited by 31 Jan 2021, 19:00

              I tried CAP P still doing the same thing

              1 Reply Last reply Reply Quote 0
              • undefined
                Veti @moe.adams9093
                last edited by 31 Jan 2021, 19:22

                @moe-adams9093 said in G32 ERROR:

                it crashed my firmware

                please post a M122 after the crash

                1 Reply Last reply Reply Quote 0
                • undefined
                  moe.adams9093
                  last edited by 31 Jan 2021, 20:14

                  its to late to post M112 because I already fixed this issue. now Im dealing with homing-all problem it just not working. I don't know if the duet can allow to use EndStops on max and Zprob On MIN

                  undefined 1 Reply Last reply 31 Jan 2021, 20:52 Reply Quote 0
                  • undefined
                    fcwilt @moe.adams9093
                    last edited by 31 Jan 2021, 20:52

                    @moe-adams9093 said in G32 ERROR:

                    its to late to post M112 because I already fixed this issue. now Im dealing with homing-all problem it just not working. I don't know if the duet can allow to use EndStops on max and Zprob On MIN

                    Yes it can - just need to get the settings right.

                    Is homing using the Z end stop sensors working?

                    Frederick

                    Printers: a small Utilmaker style, a small CoreXY and a E3D MS/TC setup. Various hotends. Using Duet 3 hardware running 3.4.6

                    1 Reply Last reply Reply Quote 0
                    • undefined
                      moe.adams9093
                      last edited by 31 Jan 2021, 20:57

                      so now I was able to get one end stop to work but when press the end-stop all 4 z motors stop not individually.

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                      • undefined
                        moe.adams9093
                        last edited by 31 Jan 2021, 21:03

                        @moe-adams9093 said in G32 ERROR:
                        when I write this code and hit save and restart the board Deg light will flash red and the bord is not reachable at this stage so I had to manually erase the firmware and reupload all files again

                        M574 Z2 S1 P"!exp.e2stop+!exp.e3stop+!exp.e5stop+!exp.e6stop";
                        
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                        • undefined
                          moe.adams9093
                          last edited by 31 Jan 2021, 21:28

                          M574 Z2 S1 P"!duex.e2stop+!duex.e3stop+!duex.e5stop+!duex.e6stop";

                          this line of Code it did work but when I press any of the end-stop all 4 Z motors Stop not individually

                          undefined 1 Reply Last reply 31 Jan 2021, 22:35 Reply Quote 0
                          • undefined
                            fcwilt @moe.adams9093
                            last edited by 31 Jan 2021, 22:35

                            @moe-adams9093 said in G32 ERROR:

                            M574 Z2 S1 P"!duex.e2stop+!duex.e3stop+!duex.e5stop+!duex.e6stop";

                            this line of Code it did work but when I press any of the end-stop all 4 Z motors Stop not individually

                            I have no idea why you should have had to erase the firmware - that makes no sense at all.

                            In any case since you had to upload all the files again but post config.g and homeall.g using the </> tag to be sure we are looking at the most recent.

                            Frederick

                            Printers: a small Utilmaker style, a small CoreXY and a E3D MS/TC setup. Various hotends. Using Duet 3 hardware running 3.4.6

                            1 Reply Last reply Reply Quote 0
                            • undefined
                              Phaedrux Moderator
                              last edited by 1 Feb 2021, 03:43

                              Can you please send M122 and M98 P"config.g" and post the results?

                              We are assuming you are on RRF3 but I don't think we've actually checked yet.

                              @moe-adams9093 said in G32 ERROR:

                              I don't know if the duet can allow to use EndStops on max and Zprob On MIN

                              It certainly can. The endstops are configured with M574 and called into action with a G1 H1 Z move, and the probe is configured with M558/G31 and called into action with G30. So as long as both are configured, you can choose which to use by either using a G1 H1 Z move or a G30/G29.

                              Z-Bot CoreXY Build | Thingiverse Profile

                              undefined 1 Reply Last reply 1 Feb 2021, 06:18 Reply Quote 0
                              • undefined
                                moe.adams9093 @Phaedrux
                                last edited by 1 Feb 2021, 06:18

                                @Phaedrux Ok so after long hours of troubleshooting and looking on duet documentation and also at duet form to find someone had the same issue. so at first when I added this code line to my config.g

                                M574 Z2 S1 P"!duex.e2stop+!duex.e3stop+!duex.e5stop+!duex.e6stop";

                                the moment when I hit save and restart the system never came back online my Degnostic light on the DuetEthernet Board was flashing red. at that stage, I went and connected via USB to enable M552S1 but my Yat Couldn't find the duet so I went ahead and jumped the 2 erase headers and reinstall the firmware everything came back as it supposed I went back a gain and added same code and it worked fine after that I'm not sure why the board did crash. so now this is my latest configuration files

                                ; Configuration file for Duet WiFi (firmware version 3)
                                ; executed by the firmware on start-up
                                ;
                                ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Oct 13 2020 21:14:55 GMT-0500 (Central Daylight Time)
                                ; General preferences
                                G90 ; send absolute coordinates...
                                M83 ; ...but relative extruder moves
                                M550 P"DIVINCI-3D (MP4560)" ; set printer name
                                M669 K1 ; select CoreXY mode
                                ; Network
                                M552 P0.0.0.0 S1 ; enable network and acquire dynamic address via DHCP
                                M586 P0 S1 ; enable HTTP
                                M586 P1 S0 ; disable FTP
                                M586 P2 S0 ; disable Telnet
                                ; Drives
                                M569 P10 R1 T2:2:2:2 S1 ; physical drive 0 goes forwards
                                M569 P11 R1 T2:2:2:2 S1 ; physical drive 1 goes forwards
                                M569 P3 S1 ; physical drive 3 goes forwards
                                M569 P4 S1 ; physical drive 4 goes forwards
                                M569 P5 S1 ; physical drive 5 goes Backwards
                                M569 P6 S1 ; physical drive 6 goes Backwards
                                M569 P8 S0 ; physical drive 7 goes Backwards
                                M569 P9 S0 ; physical drive 9 goes backwards
                                M584 X10 Y11 Z5:6:8:9 E3:4 ; set drive mapping
                                M671 X5.0:455.0:455.0:5.0 Y25.0:25.0:455.0:455.0 S6 ; ZBelts Near Locations
                                M350 X16 Y16 Z16 E16:16 I1 ; configure microstepping with interpolation
                                M92 X40.00 Y40.00 Z410.00 E415.00:415.00 ; set steps per mm
                                M566 X900.00 Y900.00 Z12.00 E120.00:120.00 ; set maximum instantaneous speed changes (mm/min)
                                M203 X6000.00 Y6000.00 Z400 E1200.00:1200.00 ; set maximum speeds (mm/min)
                                M201 X500.00 Y500.00 Z40.00 E250.00:250.00 ; set accelerations (mm/s^2)
                                M906 X1800 Y1800 Z1000 E500:500 I30 ; set motor currents (mA) and motor idle factor in per cent
                                M84 S30 ; Set idle timeout
                                ; Axis Limits
                                M208 X0 Y0 Z0 S1 ; set axis minima
                                M208 X460 Y460 Z460 S0 ; set axis maxima
                                M574 X1 S1 P"!xstop" ; configure active-high endstop for low end on X via pin !xstop
                                M574 Y1 S1 P"!ystop" ; configure active-high endstop for low end on Y via pin !ystop
                                M574 Z1 S2 ; configure Z-probe endstop for low end on Z
                                M574 Z2 S1 P"!exp.e2stop+!exp.e3stop+!exp.e5stop+!exp.e6stop" ; configure Z-probe endstop for low end on Z
                                ; Z-Probe
                                M558 P1 C"zprobe.in" H25 F600 T6000 ; set Z probe type to unmodulated and the dive height + speeds
                                G31 P500 X0 Y0 Z2.5 ; set Z probe trigger value, offset and trigger height
                                M557 X20:440 Y20:440 S20 ; define mesh grid
                                ; Heaters
                                M308 S0 P"bedtemp" Y"thermistor" T100000 B4725 C7.06e-8 ; configure sensor 0 as thermistor on pin bedtemp
                                M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0
                                M307 H0 A11 C99000 D2000 B1 ; enable bang-bang mode for the bed heater and set PWM limit
                                M140 H0 ; map heated bed to heater 0
                                M143 H0 S120 ; set temperature limit for heater 0 to 120C
                                M308 S1 P"spi.cs1" Y"thermocouple-max31856" ; configure sensor 1 as thermocouple via CS pin spi.cs1
                                M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1
                                M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
                                M308 S2 P"spi.cs2" Y"thermocouple-max31856" ; configure sensor 2 as thermocouple via CS pin spi.cs2
                                M950 H2 C"e1heat" T2 ; create nozzle heater output on e1heat and map it to sensor 2
                                M307 H2 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
                                M308 S3 P"duex.e2temp" Y"thermistor" T10000 B3950 ; configure sensor 3 as thermistor on pin duex.e2temp
                                M950 H3 C"duex.e2heat" T3 ; create chamber heater output on duex.e2heat and map it to sensor 3
                                M307 H3 A11 C99000 D2000 B1 ; enable bang-bang mode for the chamber heater and set PWM limit
                                M141 H3 ; map chamber to heater 3
                                ; Fans
                                M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency
                                M106 P0 S1 H-1 ; set fan 0 value. Thermostatic control is turned on
                                M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency
                                M106 P1 S1 H2 T45 ; set fan 1 value. Thermostatic control is turned on
                                M950 F2 C"fan2" Q500 ; create fan 2 on pin fan2 and set its frequency
                                M106 P2 S1 H1:2 T45 ; set fan 2 value. Thermostatic control is turned on
                                ; Tools
                                M563 P0 S"MAIN EXTRUDER" D0 H1 F0 ; define tool 0
                                G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                                G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C
                                M563 P1 S"SECOND EXTRUDER" D1 H2 F0 ; define tool 1
                                G10 P1 X0 Y0 Z0 ; set tool 1 axis offsets
                                G10 P1 R0 S0 ; set initial tool 1 active and standby temperatures to 0C
                                ; Custom settings are not defined
                                ; Miscellaneous
                                M575 P1 S1 B57600 ; enable support for PanelDue
                                M501 ; load saved parameters from non-volatile memory
                                M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
                                T0 ; select first tool
                                ; homeall.g
                                ; called to home all axes
                                ;
                                ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Oct 13 2020 21:14:55 GMT-0500 (Central Daylight Time)
                                G91 ; relative positioning
                                G1 H1 Z500 F6000 ; lift Z relative to current position
                                G1 H1 X-465 F8000 ; move quickly to X endstop and stop there (first pass)
                                G1 H1 Y-465 F8000 ; move quickly to Y endstop and stop there (first pass)
                                G1 H2 X5 Y5 F6000 ; go back a few mm
                                G1 H1 X-465 F360 ; move slowly to X axis endstop once more (second pass)
                                G1 H1 Y-465 F360 ; then move slowly to Y axis endstop
                                G1 X235 Y235 F6000 ; Prob at Center
                                M558 F600 A1 ; Dive fast once
                                G30 ; probe Z
                                M558 F300 A10 ; Slow second dive with more accuracy
                                G30 ; probe z again
                                1/31/2021, 11:51:21 PM: M122: === Diagnostics ===
                                RepRapFirmware for Duet 2 WiFi/Ethernet version 3.2 running on Duet Ethernet 1.02 or later + DueX5
                                Board ID: 08DLM-996RU-N8PS0-7J9D8-3S86T-1B8VP
                                Used output buffers: 3 of 24 (24 max)
                                === RTOS ===
                                Static ram: 23460
                                Dynamic ram: 70344 of which 40 recycled
                                Never used RAM 18236, free system stack 210 words
                                Tasks: NETWORK(ready,173) HEAT(blocked,309) DUEX(blocked,35) MAIN(running,452) IDLE(ready,19)
                                Owned mutexes:
                                === Platform ===
                                Last reset 00:02:05 ago, cause: power up
                                Last software reset at 2021-01-31 23:46, reason: User, GCodes spinning, available RAM 18236, slot 0
                                Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                                Error status: 0x04
                                Aux0 errors 0,0,0
                                MCU temperature: min 26.3, current 26.8, max 27.1
                                Supply voltage: min 25.0, current 25.0, max 25.1, under voltage events: 0, over voltage events: 0, power good: yes
                                Driver 0: position 0, standstill, SG min/max not available
                                Driver 1: position 0, standstill, SG min/max not available
                                Driver 2: position 0, standstill, SG min/max not available
                                Driver 3: position 0, standstill, SG min/max not available
                                Driver 4: position 0, standstill, SG min/max not available
                                Driver 5: position 0, standstill, SG min/max not available
                                Driver 6: position 0, standstill, SG min/max not available
                                Driver 7: position 0, standstill, SG min/max not available
                                Driver 8: position 0, standstill, SG min/max not available
                                Driver 9: position 0, standstill, SG min/max not available
                                Driver 10: position 0
                                Driver 11: position 0
                                Date/time: 2021-01-31 23:51:20
                                Cache data hit count 194997097
                                Slowest loop: 8.94ms; fastest: 0.21ms
                                I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                                === Storage ===
                                Free file entries: 10
                                SD card 0 detected, interface speed: 20.0MBytes/sec
                                SD card longest read time 3.9ms, write time 2.4ms, max retries 0
                                === Move ===
                                DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                                === MainDDARing ===
                                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                === AuxDDARing ===
                                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                === Heat ===
                                Bed heaters = 0 -1 -1 -1, chamberHeaters = 3 -1 -1 -1
                                Heater 1 is on, I-accum = 0.0
                                === GCodes ===
                                Segments left: 0
                                Movement lock held by null
                                HTTP is idle in state(s) 0
                                Telnet is idle in state(s) 0
                                File is idle in state(s) 0
                                USB is idle in state(s) 0
                                Aux is idle in state(s) 0
                                Trigger is idle in state(s) 0
                                Queue is idle in state(s) 0
                                LCD is idle in state(s) 0
                                Daemon is idle in state(s) 0
                                Autopause is idle in state(s) 0
                                Code queue is empty.
                                === Network ===
                                Slowest loop: 25.61ms; fastest: 0.07ms
                                Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                                HTTP sessions: 2 of 8
                                Interface state active, link 100Mbps full duplex
                                === DueX ===
                                Read count 0, 0.00 reads/min

                                **The Problem now when I click HomeZ only driver number 6 moves down (!exp.e6stop) and if press any end-stop it will stop it but the rest they do not move at all this is the problem I have I don't know if the Duex5 is bad and not communicating effectively with the duet ethernet board. **

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                                • undefined
                                  Phaedrux Moderator
                                  last edited by Phaedrux 2 Jan 2021, 06:51 1 Feb 2021, 06:50

                                  @Phaedrux said in G32 ERROR:

                                  M98 P"config.g" and post the results?

                                  And just to confirm, you have all Z motors and endstops connected to the Duex?

                                  And your duex is wired up for power/ground as shown here?

                                  https://duet3d.dozuki.com/Wiki/Duex2_and_Duex5_Features#Section_Wiring

                                  Z-Bot CoreXY Build | Thingiverse Profile

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                                  • undefined
                                    moe.adams9093
                                    last edited by 1 Feb 2021, 13:27

                                    1/31/2021, 11:51:56 PM: M98 P"config.g": HTTP is enabled on port 80
                                    FTP is disabled
                                    TELNET is disabled
                                    Error: bad grid definition: Too many grid points; suggest increase spacing to 21.0mm
                                    Warning: Macro file config-override.g not found

                                    sorry I thought I did post my M98. but everything works correctly on my duex5 except my end stops. If I run M564 S0 H0 all Zmotors work correctly. the duex5 is wired correctly as and all endstops wired correctly as well

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                                    • undefined
                                      fcwilt
                                      last edited by 1 Feb 2021, 13:34

                                      @moe-adams9093 said in G32 ERROR:

                                      M569 P8 S0 ; physical drive 7 goes Backwards

                                      The comment says 7 the command specifies 8.

                                      Have you manually activated each Z end stop sensor, one at a time, and run M119 to verify the reported end stop state?

                                      Frederick

                                      Printers: a small Utilmaker style, a small CoreXY and a E3D MS/TC setup. Various hotends. Using Duet 3 hardware running 3.4.6

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                                      • undefined
                                        moe.adams9093
                                        last edited by 1 Feb 2021, 14:20

                                        Yes I did and they all trigger as Z max endstop on m119

                                        undefined 1 Reply Last reply 1 Feb 2021, 16:28 Reply Quote 0
                                        • undefined
                                          moe.adams9093
                                          last edited by 1 Feb 2021, 14:29

                                          M569 P5 S1
                                          M569 P6 S1
                                          M569 P8 S0
                                          M569 P9 S0
                                          Yes this is the correct format for all of my z axis motors 2 motors are mirror to the other 2 thats why I have p8 s0 and p9 s0

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