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    G29S1 not loading during print and G32 not leveling properly

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    • moe.adams9093undefined
      moe.adams9093
      last edited by

      @Phaedrux I'm going to drive on top of it and see if that will make it flat

      1 Reply Last reply Reply Quote 1
      • moe.adams9093undefined
        moe.adams9093
        last edited by

        I was thinking a carbon fiber sheet plate

        fcwiltundefined 1 Reply Last reply Reply Quote 0
        • fcwiltundefined
          fcwilt @moe.adams9093
          last edited by

          @moe-adams9093 said in G29S1 not loading during print and G32 not leveling properly:

          I was thinking a carbon fiber sheet plate

          That sounds interesting but I have no idea what it is.

          Frederick

          Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

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          • moe.adams9093undefined
            moe.adams9093
            last edited by

            So after spending lots of hours calibration and testing my G29 S1 command is not loading during print. When I run G32 and G29 I get both messages in blue that adjustment made and calibration good to go but still during print I have monitored my z-axis and they don’t baby steps to compensate with the deviation points at all. I don’t know what causing this . In my gcode start file I included the following code

            G28;
            G32;
            G29 S1;

            My original printer is running on 2.05 duet maestro and it works fine when I run G32 and G29 S1 in my start gcode. So I’m not sure what’s causing this problem.

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            • dc42undefined
              dc42 administrators
              last edited by

              1. If you run G29 S1 from the console, do you see any error messages?

              2. After running G29 S1, run M122. In the resulting report, what does it say after "Bed compensation:" ?

              Duet WiFi hardware designer and firmware engineer
              Please do not ask me for Duet support via PM or email, use the forum
              http://www.escher3d.com, https://miscsolutions.wordpress.com

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              • moe.adams9093undefined
                moe.adams9093
                last edited by

                Ok here's when I run G29 S1 it will give me a green check I will post a screenshot Screenshot 2021-03-11 144744.png.
                after that I ran M122 and here's my results

                M122
                === Diagnostics ===
                RepRapFirmware for Duet 2 WiFi/Ethernet version 3.1.1 running on Duet Ethernet 1.02 or later + DueX5
                Board ID: 08DLM-996RU-N8PS0-7J9D8-3S86T-1B8VP
                Used output buffers: 3 of 24 (17 max)
                === RTOS ===
                Static ram: 27980
                Dynamic ram: 94736 of which 44 recycled
                Exception stack ram used: 488
                Never used ram: 7824
                Tasks: NETWORK(ready,392) HEAT(blocked,1224) DUEX(suspended,160) MAIN(running,1640) IDLE(ready,80)
                Owned mutexes:
                === Platform ===
                Last reset 00:07:49 ago, cause: power up
                Last software reset at 2021-03-11 02:14, reason: Stuck in spin loop, spinning module GCodes, available RAM 7648 bytes (slot 0)
                Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f80f BFAR 0xe000ed38 SP 0x20002e24 Task NETW
                Stack: 00457b03 0045b480 410f0200 3e4ccccd 40a38800 41de202f 37c87400 3331bb4c 40000000 3f317200 b5ddea0e 
                Error status: 0
                MCU temperature: min 17.2, current 26.5, max 26.7
                Supply voltage: min 25.0, current 25.0, max 25.1, under voltage events: 0, over voltage events: 0, power good: yes
                Driver 0: standstill, SG min/max not available
                Driver 1: standstill, SG min/max not available
                Driver 2: standstill, SG min/max 0/271
                Driver 3: standstill, SG min/max not available
                Driver 4: standstill, SG min/max not available
                Driver 5: standstill, SG min/max 0/226
                Driver 6: standstill, SG min/max 0/292
                Driver 7: standstill, SG min/max not available
                Driver 8: standstill, SG min/max 0/230
                Driver 9: standstill, SG min/max not available
                Date/time: 2021-03-11 14:48:25
                Cache data hit count 958208999
                Slowest loop: 20.70ms; fastest: 0.13ms
                I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                === Storage ===
                Free file entries: 10
                SD card 0 detected, interface speed: 20.0MBytes/sec
                SD card longest read time 1.5ms, write time 0.0ms, max retries 0
                === Move ===
                Hiccups: 0(0), FreeDm: 169, MinFreeDm: 165, MaxWait: 118463ms
                Bed compensation in use: mesh, comp offset 0.000
                === MainDDARing ===
                Scheduled moves: 40, completed moves: 40, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                === AuxDDARing ===
                Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                === Heat ===
                Bed heaters = 0 -1 -1 -1, chamberHeaters = 3 -1 -1 -1
                Heater 1 is on, I-accum = 0.0
                === GCodes ===
                Segments left: 0
                Movement lock held by null
                HTTP is idle in state(s) 0
                Telnet is idle in state(s) 0
                File is idle in state(s) 0
                USB is idle in state(s) 0
                Aux is idle in state(s) 0
                Trigger is idle in state(s) 0
                Queue is idle in state(s) 0
                Daemon is idle in state(s) 0
                Autopause is idle in state(s) 0
                Code queue is empty.
                === Network ===
                Slowest loop: 8.92ms; fastest: 0.02ms
                Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                HTTP sessions: 1 of 8
                Interface state active, link 100Mbps full duplex
                === DueX ===
                Read count 6, 0.77 reads/min
                
                

                and here's my latest config file

                ; Configuration file for Duet WiFi (firmware version 3)
                ; executed by the firmware on start-up
                ;
                ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Oct 13 2020 21:14:55 GMT-0500 (Central Daylight Time)
                
                ; General preferences
                G90                                                     	; send absolute coordinates...
                M83                                                     	; ...but relative extruder moves
                M550 P"DIVINCI-3D (MP4560)"                             	; set printer name
                M669 K1                                                 	; select CoreXY mode
                
                ; Network
                M552 P0.0.0.0 S1                                        	; enable network and acquire dynamic address via DHCP
                M586 P0 S1                                              	; enable HTTP
                M586 P1 S0                                              	; disable FTP
                M586 P2 S0                                              	; disable Telnet
                
                
                ; Drives
                M569 P10  R1  T3:3:10:10  S1  								; physical drive 0 goes forwards
                M569 P11  R1  T3:3:10:10  S1  								; physical drive 1 goes forwards
                M569 P3 S1                                             		; physical drive 3 goes forwards
                M569 P4 S0                                              	; physical drive 4 goes forwards
                M569 P5 S1                                              	; physical drive 5 goes Backwards
                M569 P6 S1 													; physical drive 6 goes Backwards
                M569 P8 S1			          								; physical drive 7 goes Backwards 
                M569 P2 S1                                              	; physical drive 9 goes backwards 
                M584 X10 Y11 Z5:6:8:2 E3:4                              	; set drive mapping
                M671 X50.0:450.0:450.0:50.0 Y50.0:50.0:450.0:450.0 S2   	; ZBelts Near Locations                    
                M350 X16 Y16 Z16 E16:16 I1                              	; configure microstepping with interpolation
                M92 X40 Y40 Z412.00 E420.00:420.00 					; set steps per mm
                M566 X10000 Y10000 Z800 E600:600              	; set maximum instantaneous speed changes (mm/min)
                M203 X6000.00 Y6000.00 Z800 E6000:6000      		; set maximum speeds (mm/min)
                M201 X8000 Y8000 Z800 5000:5000     		; set accelerations (mm/s^2)
                M906 X1800 Y1800 Z1000 E600:600 I30                     	; set motor currents (mA) and motor idle factor in per cent
                M84 S30                                                 	; Set idle timeout
                
                
                ; Axis Limits
                M208 X0 Y0 Z0 S1                                        	; set axis minima
                M208 X500 Y500 Z500 S0                                  	; set axis maxima
                
                M574 X1 S1 P"!xstop"                                    	; configure active-high endstop for low end on X via pin !xstop
                M574 Y1 S1 P"!ystop"                                    	; configure active-high endstop for low end on Y via pin !ystop
                M574 Z1 S2                                              	; configure Z-probe endstop for low end on Z
                M574 Z2 S1 P"!zstop+!duex.e2stop+!duex.e3stop+!duex.e5stop" ; configure active-high endstop for high end on Z
                
                 
                
                
                
                ; Z-Probe
                M558 P1 C"zprobe.in" H5 F120 T6000                   	; set Z probe type to unmodulated and the dive height + speeds
                G31 P500 X5 Y29 Z0.551                                	; set Z probe trigger value, offset and trigger height
                M557 X50:450 Y50:450 S40                                	; define mesh grid
                
                
                ; Heaters
                M308 S0 P"bedtemp" Y"thermistor" T100000 B4725 C7.06e-8 	; configure sensor 0 as thermistor on pin bedtemp
                M950 H0 C"bedheat" T0                                   	; create bed heater output on bedheat and map it to sensor 0
                M307 H0 A11 C99000 D2000 B1                  				; enable bang-bang mode for the bed heater and set PWM limit
                M140 H0                                                 	; map heated bed to heater 0
                M143 H0 S120                                            	; set temperature limit for heater 0 to 120C
                M308 S1 P"spi.cs2" Y"thermocouple-max31856"     ; configure sensor 1 as thermocouple via CS pin spi.cs1
                M950 H1 C"e0heat" T1                            ; create nozzle heater output on e0heat and map it to sensor 1
                M307 H1 B0 S1.00                                ; disable bang-bang mode for heater  and set PWM limit
                M143 H1 S360                                    ; set temperature limit for heater 1 to 280C
                M308 S3 P"duex.e2temp" Y"thermistor" T10000 B3950       	; configure sensor 3 as thermistor on pin duex.e2temp
                M950 H3 C"e1heat" T3                               	; create chamber heater output on duex.e2heat and map it to sensor 3
                M307 H3 A11 C99000 D2000 B1                             	; enable bang-bang mode for the chamber heater and set PWM limit
                M141 H3                                                 	; map chamber to heater 3
                
                ; Fans
                M950 F0 C"fan1" Q500                                    ; create fan 0 on pin fan1 and set its frequency
                M106 P0 C"WATER COOLING" S1 H1 T45                      ; set fan 0 name and value. Thermostatic control is turned on
                
                M950 F1 C"duex.fan6" Q500                               ; create fan 1 on pin duex.fan6 and set its frequency
                M106 P1 S1 H1 T45                                       ; set fan 1 value. Thermostatic control is turned on
                M950 F2 C"duex.fan7" Q500                               ; create fan 2 on pin duex.fan7 and set its frequency
                M106 P2 S1 H1 T45                                       ; set fan 2 value. Thermostatic control is turned on
                
                ;Led-Indicators
                
                M950 P6 C"duex.e2heat" Q500 ; Assign to P6
                M950 P7 C"duex.e3heat" Q500 ; Assign to P7
                M950 P8 C"duex.e4heat" Q500 ; Assign to P8
                M950 P9 C"duex.e5heat" Q500 ; Assign to P9
                M42 P6 S0; 
                M42 P7 S0;
                M42 P8 S0;
                M42 P9 S0;
                
                ; Tools
                M563 P0 S"MAIN EXTRUDER " D0 H1 F0              ; define tool 0
                G10 P0 X0 Y0 Z0                                 ; set tool 0 axis offsets
                G10 P0 R0 S0                                    ; set initial tool 0 active and standby temperatures to 0C
                M563 P1 S"SECOND EXTRUDER" D1 H1 F0             ; define tool 1
                G10 P1 X0 Y0 Z0                                 ; set tool 1 axis offsets
                G10 P1 R0 S0                                    ; set initial tool 1 active and standby temperatures to 0C
                
                ; Custom settings are not defined
                
                ; Miscellaneous
                M575 P1 S1 B57600                                       	; enable support for PanelDue
                M501                                                    	; load saved parameters from non-volatile memory
                M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000"      	; set voltage thresholds and actions to run on power loss
                T0                                                      	; select first tool
                
                
                
                Phaedruxundefined 1 Reply Last reply Reply Quote 0
                • Phaedruxundefined
                  Phaedrux Moderator @moe.adams9093
                  last edited by

                  @moe-adams9093 said in G29S1 not loading during print and G32 not leveling properly:

                  Bed compensation in use: mesh

                  So it is active.

                  If you put a piece of tape on the Z axis motor shafts or lead screw do you see it move during the first layer?

                  Z-Bot CoreXY Build | Thingiverse Profile

                  moe.adams9093undefined 1 Reply Last reply Reply Quote 0
                  • moe.adams9093undefined
                    moe.adams9093 @Phaedrux
                    last edited by

                    I took the bottom plate off to see if my Z motors are compensating and they do move but they move very slow so I don't know if there's an option where I can make my Zmotors to compensate equivalent with the same speed of the X&Y axis while printing

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                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Your Z accelerations are very slow. M201 Z80 but the jerk is very high. M566 Z800. Try swapping those two values.

                      Such a high jerk is making the firmware think the z axis is able to keep up to rapid changes in z position, but it can't actually. So the z movement is probably lagging behind where it thinks it is.

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • moe.adams9093undefined
                        moe.adams9093
                        last edited by

                        Ok I will try to change these settings and see how’s it going to behavior. Thank you

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                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          How is the Z axis setup? What kind of speeds can we realistically expect from it?

                          Z-Bot CoreXY Build | Thingiverse Profile

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                          • moe.adams9093undefined
                            moe.adams9093
                            last edited by moe.adams9093

                            the Zaxis runs by 4 gearbox motors belt-driven. Expecting 100mm high-quality print speed

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                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by

                              Did swapping those values help?

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • moe.adams9093undefined
                                moe.adams9093
                                last edited by moe.adams9093

                                Yes it did little bit I also ran a quick print test and the results not really promising. Looks like some vibration issues from the X&Y Im note sure if it’s my external driver or maybe my linear rail. 2D8E8A6C-B11F-458A-920B-A18DECB57192.jpeg 980EAAA2-9104-4FA3-812B-2DBFD261EC5E.jpeg 02A225C9-B0A1-498A-8A0C-6C43D596F17C.jpeg

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                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  M566 X10000 Y10000

                                  your jerk on the X and Y is insanely high. Try reduce that to 1000.

                                  Z-Bot CoreXY Build | Thingiverse Profile

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                                  • moe.adams9093undefined
                                    moe.adams9093
                                    last edited by

                                    Ok I will do that over the weekend do you have any resources regarding the T parameters for external driver I need to understand what each number represent and how it can affect. I’m using theses motors they are Nema 23 with integrated rotary encoder. I order today RS232 Cable so I can connect them to my pc and se if I can change so of the settings to match with my config.g FAB41018-5AE5-486D-A777-2C06BCCAFC18.jpeg 807FEEA7-F873-4A87-8927-3B3837D69D1A.jpeg . Thanks for all your help I really appreciate it

                                    fcwiltundefined 1 Reply Last reply Reply Quote 0
                                    • fcwiltundefined
                                      fcwilt @moe.adams9093
                                      last edited by

                                      @moe-adams9093

                                      If you do not have the specs for those drivers try T2:2:10:10 for starters.

                                      Frederick

                                      Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

                                      1 Reply Last reply Reply Quote 1
                                      • moe.adams9093undefined
                                        moe.adams9093
                                        last edited by

                                        So I did some lots of tweaking and here some results for a first full print it’s ABS print speed 3600mm/min Zaxis at 600mm/min print size 40x40x40 simplify 3D gave 1:18 hr/min estimate print time and it took about 1:40 hr/min. Bedtemp set at 100C and extruded at 235C But the quality is awful.

                                        Here’s my new motor settings.

                                        
                                        ; Drives
                                        M569 P10  R1  T3:3:6:10 S1   ; physical drive 0 goes forwards
                                        M569 P11  R1  T3:3:6:10 S1   ; physical drive 1 goes forwards
                                        M569 P3 S1                                             ; physical drive 3 goes forwards
                                        M569 P4 S0                                               ; physical drive 4 goes forwards
                                        M569 P5 S1                                               ; physical drive 5 goes Backwards
                                        M569 P6 S1 ; physical drive 6 goes Backwards
                                        M569 P8 S1           ; physical drive 7 goes Backwards 
                                        M569 P2 S1                                               ; physical drive 9 goes backwards 
                                        M584 X10 Y11 Z5:6:8:2 E3:4                               ; set drive mapping
                                        M671 X50.0:480.0:480.0:50.0 Y50.0:50.0:460.0:460.0 S5   ; ZBelts Near Locations                  
                                        M350 X16 Y16 Z16 E16:16 I1                               ; configure microstepping with interpolation
                                        M92 X160 Y160 Z412.00 E420.00:420.00 ; set steps per mm
                                        M566 X500 Y500 Z60 E500:500               ; set maximum instantaneous speed changes (mm/min)
                                        M203 X6000 Y6000 Z800 E6000:6000     ; set maximum speeds (mm/min)
                                        M201 X1000 Y1000 Z400 5000:5000     ; set accelerations (mm/s^2)
                                        M906 X2600 Y2600 Z1100 E800:800 I30                     ; set motor currents (mA) and motor idle factor in per cent
                                        M84 S30                                                 ; Set idle timeout
                                        
                                        
                                        

                                        Here’s a picture of the actual print.

                                        1FC79C11-5292-40AB-9769-5D08AA07FC15.jpeg C1C7AA38-AACA-4DC9-853E-50643010BC50.jpeg 81B5C307-93AF-47C0-AAC4-6BE85FF12D24.jpeg 1C372A95-0AF7-4E4D-B37E-11FB0902623B.jpeg

                                        Even with that low jerk settings the printer is shaking from the external driver. Printer weights about 270 Ib I don’t know if I need to go lower value on any of the settings or maybe the external driver not override Correct value from the config. G file or any other suggestions

                                        Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                        • Phaedruxundefined
                                          Phaedrux Moderator @moe.adams9093
                                          last edited by

                                          @moe-adams9093 said in G29S1 not loading during print and G32 not leveling properly:

                                          M201 X1000 Y1000 Z400 5000:5000 ; set accelerations (mm/s^2)

                                          You're missing an E on the extruder values.

                                          Can you send M98 P"config.g" and post any errors that come up?

                                          Z-Bot CoreXY Build | Thingiverse Profile

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                                          • moe.adams9093undefined
                                            moe.adams9093
                                            last edited by

                                            3/17/2021, 2:10:30 PM	M98 P"config.g"
                                            HTTP is enabled on port 80
                                            FTP is disabled
                                            TELNET is disabled
                                            

                                            this is before I changed it didn't give me any error.

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