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    Error: Probe was not triggered during probing move

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    • milan.bacaundefined
      milan.baca
      last edited by

      Hello, I have this problem when I want to use G32 or G29 command.
      When G32 it check 3 defined point end than stop and it show me this error "

      G32
      Error: Probe was not triggered during probing move
      Error: Compensation or calibration cancelled due to probing errors
      ".

      When G29 common it check 2 points and then stop and show me this error.

      bed.g
      config.g

      Could you help me what could be wrong?

      I have tried stable release and also the newest rc release of firmware.
      I have BLTouch instaled. It looks work well (stop bed when triggered), but when triggered it should show Z-probe value as 1000, but I have always 0.

      Vetiundefined Phaedruxundefined 2 Replies Last reply Reply Quote 0
      • Vetiundefined
        Veti @milan.baca
        last edited by

        if the tilt of your bed is to big. the probing will fail.

        level your bed on the 4 corner manually so that its fairly flat. then try again.

        milan.bacaundefined 1 Reply Last reply Reply Quote 0
        • milan.bacaundefined
          milan.baca @Veti
          last edited by

          @veti I have 3 independent z motor configuration. I thought than G32 command should auto level the bed, without manual bed leveling.

          1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @milan.baca
            last edited by

            @milan-baca said in Error: Probe was not triggered during probing move:

            I have BLTouch instaled. It looks work well (stop bed when triggered), but when triggered it should show Z-probe value as 1000, but I have always 0.

            The value can be very hard to catch on the DWC view because the bltouch triggers and resets again instantly. It doesn't stay triggered.

            Can you post your homeall.g as well?
            Also the results of M122 and M98 P"config.g" please.

            Z-Bot CoreXY Build | Thingiverse Profile

            milan.bacaundefined 1 Reply Last reply Reply Quote 0
            • milan.bacaundefined
              milan.baca @Phaedrux
              last edited by

              @phaedrux
              thank for explanation about Z-probe value.

              because I have duet3 6HC

              I changed line
              M558 P9 C"^io7.in" H15 F100 T6000 R0.2 A5

              to
              M558 P9 C"io7.in" H15 F100 T6000 R0.2 A5

              now I got different error

              Error: This kinematics does not support auto-calibration 😞

              1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                CoreXY certainly does. How are you trying to do the auto calibration?

                G32 calls bed.g

                https://duet3d.dozuki.com/Wiki/Bed_levelling_using_multiple_independent_Z_motors

                Can you post your homeall.g as well?
                Also the results of M122 and M98 P"config.g" please.

                Z-Bot CoreXY Build | Thingiverse Profile

                milan.bacaundefined 1 Reply Last reply Reply Quote 0
                • milan.bacaundefined
                  milan.baca @Phaedrux
                  last edited by milan.baca

                  @phaedrux homeall.g

                  M122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.3RC3 (2021-05-26 12:29:42) running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
                  Board ID: 08DJM-956BA-NA3TJ-6J9FJ-3S86R-1T96T
                  Used output buffers: 1 of 40 (13 max)
                  === RTOS ===
                  Static ram: 150784
                  Dynamic ram: 62052 of which 160 recycled
                  Never used RAM 141196, free system stack 126 words
                  Tasks: SBC(ready,5.2%,338) HEAT(delaying,0.0%,295) Move(notifyWait,0.0%,275) CanReceiv(notifyWait,0.0%,945) CanSender(notifyWait,0.0%,360) CanClock(delaying,0.0%,333) TMC(notifyWait,7.9%,59) MAIN(running,86.8%,922) IDLE(ready,0.0%,29), total 100.0%
                  Owned mutexes: HTTP(MAIN)
                  === Platform ===
                  Last reset 00:38:42 ago, cause: software
                  Last software reset at 2021-06-13 15:27, reason: User, none spinning, available RAM 141196, slot 1
                  Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a000 BFAR 0x00000000 SP 0x00000000 Task SBC Freestk 0 n/a
                  Error status: 0x00
                  Aux0 errors 0,0,0
                  Aux1 errors 0,0,0
                  Step timer max interval 133
                  MCU temperature: min 39.4, current 39.6, max 53.4
                  Supply voltage: min 23.9, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.0, current 12.0, max 12.1, under voltage events: 0
                  Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                  Driver 0: position 66722, standstill, reads 27175, writes 23 timeouts 0, SG min/max 0/227
                  Driver 1: position -24410, standstill, reads 27175, writes 23 timeouts 0, SG min/max 0/227
                  Driver 2: position 28000, standstill, reads 27184, writes 14 timeouts 0, SG min/max 0/0
                  Driver 3: position 0, standstill, reads 27176, writes 22 timeouts 0, SG min/max 0/228
                  Driver 4: position 0, standstill, reads 27176, writes 22 timeouts 0, SG min/max 0/233
                  Driver 5: position 0, standstill, reads 27177, writes 22 timeouts 0, SG min/max 0/246
                  Date/time: 2021-06-13 16:06:00
                  Slowest loop: 177.37ms; fastest: 0.03ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  DMs created 125, maxWait 297675ms, bed compensation in use: none, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves 43, completed moves 43, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === AuxDDARing ===
                  Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === Heat ===
                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  Heater 1 is on, I-accum = 0.0
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is doing "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger* is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === CAN ===
                  Messages queued 20904, send timeouts 20901, received 0, lost 0, longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 49 (min 49), ts 11614/0/0
                  Last cancelled message type 30 dest 127
                  === SBC interface ===
                  State: 4, failed transfers: 0
                  Last transfer: 1ms ago
                  RX/TX seq numbers: 16462/16462
                  SPI underruns 0, overruns 0
                  Number of disconnects: 0, IAP RAM available 0x2c8bc
                  Buffer RX/TX: 0/0-0
                  === Duet Control Server ===
                  Duet Control Server v3.3-rc3
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 35.35
                  Codes per second: 0.09
                  Maximum length of RX/TX data transfers: 2756/864

                  M98 P"config.g"
                  Error: M350: Driver 3 does not support x0 microstepping with interpolation
                  Driver 4 does not support x0 microstepping with interpolation
                  Driver 5 does not support x0 microstepping with interpolation
                  Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
                  Warning: M307: Heater 1 appears to be over-powered. If left on at full power, its temperature is predicted to reach 516C

                  Phaedruxundefined 1 Reply Last reply Reply Quote 0
                  • Phaedruxundefined
                    Phaedrux Moderator @milan.baca
                    last edited by

                    @milan-baca said in Error: Probe was not triggered during probing move:

                    Error: M350: Driver 3 does not support x0 microstepping with interpolation
                    Driver 4 does not support x0 microstepping with interpolation
                    Driver 5 does not support x0 microstepping with interpolation

                    Those are your Z drivers, correct? Have you changed microstepping since posting your config.g above?

                    Z-Bot CoreXY Build | Thingiverse Profile

                    milan.bacaundefined 1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Remove this from your homeall

                      G92 Z0 ; set Z position to axis minimum (you may want to adjust this)

                      Z-Bot CoreXY Build | Thingiverse Profile

                      milan.bacaundefined 1 Reply Last reply Reply Quote 0
                      • milan.bacaundefined
                        milan.baca @Phaedrux
                        last edited by

                        @phaedrux yes I change it to
                        M350 X16 Y16 Z16:16:16 E16 I1

                        I change it back to Z16 and now

                        M98 P"config.g"
                        Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
                        Warning: M307: Heater 1 appears to be over-powered. If left on at full power, its temperature is predicted to reach 516C

                        1 Reply Last reply Reply Quote 0
                        • milan.bacaundefined
                          milan.baca @Phaedrux
                          last edited by

                          @phaedrux
                          I removed G92 Z0 from homeall.g

                          but still same error

                          1 Reply Last reply Reply Quote 0
                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            Reduce your dive height from M558 H15 to H5

                            Z-Bot CoreXY Build | Thingiverse Profile

                            milan.bacaundefined 1 Reply Last reply Reply Quote 0
                            • milan.bacaundefined
                              milan.baca @Phaedrux
                              last edited by

                              @phaedrux not helped, Error: This kinematics does not support auto-calibration is still there

                              dc42undefined 1 Reply Last reply Reply Quote 0
                              • dc42undefined
                                dc42 administrators @milan.baca
                                last edited by

                                @milan-baca I think you must have made another change to config.g. Please post it as it is now.

                                Duet WiFi hardware designer and firmware engineer
                                Please do not ask me for Duet support via PM or email, use the forum
                                http://www.escher3d.com, https://miscsolutions.wordpress.com

                                milan.bacaundefined 1 Reply Last reply Reply Quote 0
                                • milan.bacaundefined
                                  milan.baca @dc42
                                  last edited by

                                  @dc42 config.g

                                  jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                                  • jay_s_ukundefined
                                    jay_s_uk @milan.baca
                                    last edited by jay_s_uk

                                    easier to read

                                    ; Configuration file for Duet 3 (firmware version 3)
                                    ; executed by the firmware on start-up
                                    ;
                                    ; generated by RepRapFirmware Configuration Tool v3.2.3 on Sun Apr 04 2021 22:18:55 GMT+0200 (CEST)
                                    
                                    ; General preferences
                                    G90                                                  ; send absolute coordinates...
                                    M83                                                  ; ...but relative extruder moves
                                    M550 P"Duet 3"                                       ; set printer name
                                    M669 K1                                              ; select CoreXY mode
                                    M912 S-13.7										     ; mcu temperature correction
                                    
                                    ; Drives
                                    M569 P0.0 S0 ;H50 V50 D3                             ; physical drive 0.0 goes forwards axis X
                                    M569 P0.1 S0 ;H50 V50 D3                             ; physical drive 0.1 goes forwards axis Y
                                    M569 P0.2 S0                                         ; physical drive 0.2 goes forwards EXTRUDER
                                    M569 P0.3 S0 ;H50 V50 D3                             ; physical drive 0.3 goes forwards
                                    M569 P0.4 S0 ;H50 V50 D3                             ; physical drive 0.3 goes forwards
                                    M569 P0.5 S0 ;H50 V50 D3                             ; physical drive 0.3 goes forwards
                                    M584 X0.0 Y0.1 Z0.3:0.4:0.5 E0.2                     ; set drive mapping
                                    M671 X-26,188:155,021:331,23 Y-20,717:307,493:-20,717 S50 ;Z Lift Point position
                                    
                                    M350 X16 Y16 Z16 E16 I1                        	 	 ; configure microstepping with interpolation
                                    M92 X160.00 Y160.00 Z1600.00 E712.00                 ; set steps per mm
                                    M566 X1200.00 Y1200.00 Z30.00 E120.00                ; set maximum instantaneous speed changes (mm/min)
                                    M203 X18000.00 Y18000.00 Z1800.00 E1200.00           ; set maximum speeds (mm/min)
                                    M201 X1600.00 Y1600.00 Z100.00 E250.00               ; set accelerations (mm/s^2)
                                    M906 X1400 Y1400 Z1400 E300 I30                      ; set motor currents (mA) and motor idle factor in per cent
                                    M84 S30                                              ; Set idle timeout
                                    
                                    ; Axis Limits
                                    M208 X0 Y0 Z0 S1                                     ; set axis minima
                                    M208 X320 Y320 Z321 S0                               ; set axis maxima
                                    
                                    ; Endstops
                                    M574 X1 S1 P"io0.in"                                 ; configure active-high endstop for low end on X via pin io0.in
                                    M574 Y1 S1 P"io1.in"                                 ; configure active-high endstop for low end on Y via pin io1.in
                                    
                                    ; Z-Probe
                                    M950 S0 C"io7.out"                                   ; create servo pin 0 for BLTouch
                                    M558 P9 C"io7.in" H15 F150 T6000 R0.2 A5
                                    G31 P25 X22.775 Y5.21 Z2.5                           ; set Z probe trigger value, offset and trigger height
                                    M557 X25:282 Y10:282 P5:5                            ; define mesh grid
                                    
                                    ; Heaters
                                    M308 S0 P"temp0" Y"thermistor" T100000 B4267         ; configure sensor 0 as thermistor on pin temp0
                                    M950 H0 C"out0" T0                                   ; create bed heater output on out0 and map it to sensor 0
                                    M307 H0 B1 S1.00                                     ; enable bang-bang mode for the bed heater and set PWM limit
                                    
                                    M140 H0                                              ; map heated bed to heater 0
                                    M143 H0 S120                                         ; set temperature limit for heater 0 to 120C
                                    M308 S1 P"temp1" Y"thermistor" T100000 B3950         ; configure sensor 1 as thermistor on pin temp1
                                    M950 H1 C"out1" T1                                   ; create nozzle heater output on out1 and map it to sensor 1
                                    M307 H1 R3.678 C133.6 D6.67 S1.00 V24.0
                                    M143 H1 S280                                         ; set temperature limit for heater 1 to 280C
                                    
                                    ; Fans
                                    M950 F0 C"out7" ;Q250                                 ; create fan 0 on pin out7 and set its frequency
                                    M106 P0 S0 H1 T45                                    ; set fan 0 value. Thermostatic control is turned on
                                    M950 F1 C"out4" Q500                                 ; create fan 1 on pin out4 and set its frequency
                                    M106 P1 S1 H-1                                    	 ; set fan 1 value. Thermostatic control is turned of
                                    
                                    ; Tools
                                    M563 P0 D0 H1 F0                                     ; define tool 0
                                    G10 P0 X0 Y0 Z0                                      ; set tool 0 axis offsets
                                    G10 P0 R0 S0                                         ; set initial tool 0 active and standby temperatures to 0C
                                    
                                    ; Custom settings are not defined
                                    
                                    ;M581 Y S1 T2
                                    ; Miscellaneous
                                    M308 S10 Y"mcu-temp" A"MCU"
                                    
                                    M501
                                    M911 S22 R23.5 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
                                    T0
                                    

                                    Your M671 doesn't look valid to me
                                    how is your bed supported? what are the co-ordinates of the screws?

                                    Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                    dc42undefined milan.bacaundefined 2 Replies Last reply Reply Quote 0
                                    • dc42undefined
                                      dc42 administrators @jay_s_uk
                                      last edited by

                                      I agree with @jay_s_uk. Change the commas in the M671 command to fullstops.

                                      Duet WiFi hardware designer and firmware engineer
                                      Please do not ask me for Duet support via PM or email, use the forum
                                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                                      milan.bacaundefined 2 Replies Last reply Reply Quote 0
                                      • milan.bacaundefined
                                        milan.baca @jay_s_uk
                                        last edited by

                                        @jay_s_uk
                                        I am using calculator from this project
                                        https://miragec79.github.io/HevORT/firmwaresettings.html

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                                        • milan.bacaundefined
                                          milan.baca @dc42
                                          last edited by

                                          @dc42 thank you very much guys problem was in M671 command in numbers

                                          I look at it many times but after you point to that command I saw the problem. It was decimal separator in coordinates 🙂

                                          1 Reply Last reply Reply Quote 1
                                          • milan.bacaundefined
                                            milan.baca @dc42
                                            last edited by

                                            @dc42
                                            G32 command now work well

                                            still have a problem with G29
                                            after few points I got
                                            Error: Probe already triggered before probing move started

                                            ps: should I make a new thread or can I continue here?

                                            dc42undefined 1 Reply Last reply Reply Quote 0
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