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    BLTouch stuck at 1000

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    • Messiahmanundefined
      Messiahman
      last edited by

      Just last night i managed to successfully run a print. I went to collect it off my bed this morning and tried to simply run another one. When the printer went to home the z axis, it raised a couple mm before displaying the error that the bltouch was already triggered at the start of movement. Nothing i do seems to resolve this issue. Help?

      Nurgelrotundefined dc42undefined 2 Replies Last reply Reply Quote 0
      • Nurgelrotundefined
        Nurgelrot @Messiahman
        last edited by Nurgelrot

        @messiahman have you tried just resetting the BLtouch? read up on the M280 command. M280 P0 S160 your Px may vary. Otherwise post your config.g and homez.g homeall.g

        Messiahmanundefined 1 Reply Last reply Reply Quote 0
        • Messiahmanundefined
          Messiahman @Nurgelrot
          last edited by

          @nurgelrot interesting, ill give it a try and let you know? I have been trying to turn the printer on and off, unplugged and replugged the bltouch wires, etc. etc., i didnt realize there was an actual function to just reset the bltouch

          Nurgelrotundefined 1 Reply Last reply Reply Quote 0
          • Nurgelrotundefined
            Nurgelrot @Messiahman
            last edited by

            @messiahman Post your configs when you get a chance if its failing that much something isn't right.

            Messiahmanundefined 1 Reply Last reply Reply Quote 0
            • Messiahmanundefined
              Messiahman @Nurgelrot
              last edited by

              @nurgelrot thats the thing though, like i said it was working fine last night and i havent since changed anything, its like the probe just decided “today’s not the day” lol

              Nurgelrotundefined 1 Reply Last reply Reply Quote 0
              • Nurgelrotundefined
                Nurgelrot @Messiahman
                last edited by

                @messiahman Cosmic rays... 🙂 BLtouch are touchy. I had one just go nuts once too would always error out on a G29 ended up just replacing it cuz I never did figure out what was the issue and the config had worked for long time (and still does with the new one). But don't get too drastic yet. fiddle with the pin etc... see if you can see when/why it thinks its deployed. move your signal wires away from steppers etc...

                PCRundefined 1 Reply Last reply Reply Quote 0
                • PCRundefined
                  PCR @Nurgelrot
                  last edited by

                  @nurgelrot Sometimes is the grub screw. The screw has to be at a exact distance. See the manual for it

                  1 Reply Last reply Reply Quote 0
                  • rjenkinsgbundefined
                    rjenkinsgb
                    last edited by

                    Is the BLTouch well clear of the bed when you power on?

                    If the probe touches the bed when it tries to do its self-test, it will fail.

                    Robert J.

                    Printers: Overlord pro, Kossel XL+ with Duet 6HC and "Frankentron", TronXY X5SA Pro converted to E3D toolchange with Duet 6HC and 1LC toolboards.

                    Messiahmanundefined 1 Reply Last reply Reply Quote 0
                    • Messiahmanundefined
                      Messiahman @rjenkinsgb
                      last edited by

                      @rjenkinsgb yeah no the entire extruder head is nearly to the top of the print area cuz my last print ended off pretty high up

                      1 Reply Last reply Reply Quote 0
                      • dc42undefined
                        dc42 administrators @Messiahman
                        last edited by

                        @messiahman if the reading is 1000 when the pin is extended, most likely there is a break in the signal connection. On a genuine BLTouch this is usually the white wire.

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        Messiahmanundefined 1 Reply Last reply Reply Quote 0
                        • Messiahmanundefined
                          Messiahman @dc42
                          last edited by

                          @dc42 I've checked all the wires, theyre all pretty strong connections

                          dc42undefined 1 Reply Last reply Reply Quote 0
                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            Use a multimeter to test continuity of the wires themselves.

                            Z-Bot CoreXY Build | Thingiverse Profile

                            1 Reply Last reply Reply Quote 1
                            • dc42undefined
                              dc42 administrators @Messiahman
                              last edited by

                              @messiahman you can test the Duet and your configuration by disconnecting the white wire and connecting that input on the Duet to ground. That should make the reading go to 0.

                              Duet WiFi hardware designer and firmware engineer
                              Please do not ask me for Duet support via PM or email, use the forum
                              http://www.escher3d.com, https://miscsolutions.wordpress.com

                              Messiahmanundefined 1 Reply Last reply Reply Quote 1
                              • Messiahmanundefined
                                Messiahman @dc42
                                last edited by

                                @dc42 that didn't work

                                dc42undefined 1 Reply Last reply Reply Quote 0
                                • dc42undefined
                                  dc42 administrators @Messiahman
                                  last edited by

                                  @messiahman please post your config.g file and post a photo of the wiring connecting the BLTouch to the Duet.

                                  Duet WiFi hardware designer and firmware engineer
                                  Please do not ask me for Duet support via PM or email, use the forum
                                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                                  Messiahmanundefined 1 Reply Last reply Reply Quote 0
                                  • Messiahmanundefined
                                    Messiahman @dc42
                                    last edited by

                                    @dc42 will do, but i did just unplug the whole bltouch to try and dispel any charge in the capacitor and replugged it all in, and now it won't deploy or retract.

                                    ; Configuration file for Duet WiFi (firmware version 3)
                                    ; executed by the firmware on start-up
                                    ;
                                    ; generated by RepRapFirmware Configuration Tool v3.3.3 on Wed Oct 06 2021 12:37:23 GMT-0400 (Eastern Daylight Time)

                                    ; General preferences
                                    G90 ; send absolute coordinates...
                                    M83 ; ...but relative extruder moves
                                    M550 P"The Print-inator" ; set printer name
                                    M918 P1 E4 F2000000 ; configure direct-connect display

                                    ; Network
                                    M552 S1 ; enable network
                                    M586 P0 S1 ; enable HTTP
                                    M586 P1 S0 ; disable FTP
                                    M586 P2 S0 ; disable Telnet

                                    ; Drives
                                    M569 P0 S0 ; physical drive 0 goes backwards
                                    M569 P1 S0 ; physical drive 1 goes backwards
                                    M569 P2 S0 ; physical drive 2 goes backwards
                                    M569 P3 S1 ; physical drive 3 goes forwards
                                    M584 X0 Y1 Z2 E3 ; set drive mapping
                                    M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
                                    M92 X80.00 Y80.00 Z400.00 E136.79 ; set steps per mm
                                    M566 X1200.00 Y1200.00 Z24.00 E300.00 ; set maximum instantaneous speed changes (mm/min)
                                    M203 X9000.00 Y9000.00 Z180.00 E6000.00 ; set maximum speeds (mm/min)
                                    M201 X500.00 Y500.00 Z100.00 E5000.00 ; set accelerations (mm/s^2)
                                    M906 X800 Y800 Z800 E1000 I50 ; set motor currents (mA) and motor idle factor in per cent
                                    M84 S30 ; Set idle timeout

                                    ; Axis Limits
                                    M208 X0 Y0 Z0 S1 ; set axis minima
                                    M208 X235 Y235 Z260 S0 ; set axis maxima

                                    ; Endstops
                                    M574 X2 S1 P"xstop" ; configure active-high endstop for high end on X via pin xstop
                                    M574 Y2 S1 P"ystop" ; configure active-high endstop for high end on Y via pin ystop
                                    M574 Z1 S2 ; configure Z-probe endstop for low end on Z

                                    ; Z-Probe
                                    M950 S0 C"exp.heater3" ; create servo pin 0 for BLTouch
                                    M558 P9 C"^zprobe.in" H3 F120 T6000 ; set Z probe type to bltouch and the dive height + speeds
                                    G31 P500 X40.00 Y5.0 Z1.250 ; set Z probe trigger value, offset and trigger height
                                    M557 X40:220 Y25:220 S41 ; define mesh grid

                                    ; Heaters
                                    M308 S0 P"bedtemp" Y"thermistor" T100000 B4092 ; configure sensor 0 as thermistor on pin bedtemp
                                    M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0
                                    M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
                                    M140 H0 ; map heated bed to heater 0
                                    M143 H0 S150 ; set temperature limit for heater 0 to 150C
                                    M308 S1 P"e0temp" Y"thermistor" T100000 B4092 ; configure sensor 1 as thermistor on pin e0temp
                                    M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1
                                    M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
                                    M143 H1 S275 ; set temperature limit for heater 1 to 275C

                                    ; Fans
                                    M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency
                                    M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
                                    M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency
                                    M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on
                                    M950 F2 C"fan2" Q500 ; create fan 2 on pin fan2 and set its frequency
                                    M106 P2 S1 H1:0 T45 ; set fan 2 value. Thermostatic control is turned on

                                    ; Tools
                                    M563 P0 D0 H1 F0 ; define tool 0
                                    G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                                    G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

                                    ; Custom settings are not defined

                                    ; Miscellaneous
                                    M501 ; load saved parameters from non-volatile memory
                                    M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss

                                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                    • Phaedruxundefined
                                      Phaedrux Moderator @Messiahman
                                      last edited by

                                      @messiahman said in BLTouch stuck at 1000:

                                      and now it won't deploy or retract.

                                      Does it light up at all? The plug at the BLTouch end is very delicate.

                                      Z-Bot CoreXY Build | Thingiverse Profile

                                      Messiahmanundefined 1 Reply Last reply Reply Quote 0
                                      • Messiahmanundefined
                                        Messiahman @Phaedrux
                                        last edited by

                                        @phaedrux the red light comes on yes, but not the blue. it also goes through the startup sequence

                                        1 Reply Last reply Reply Quote 0
                                        • wieman01undefined
                                          wieman01
                                          last edited by wieman01

                                          Could you also post the contents of "deployprobe.g" and "retractprobe.g" please? There is a chance that's the source of your problem.

                                          1 Reply Last reply Reply Quote 1
                                          • wieman01undefined
                                            wieman01
                                            last edited by

                                            The reason why I am asking is this:

                                            When you are issuing either M401 or M402 your BL's pin should move down or retract. If it does not, then either these files are missing altogether or they are referring to the wrong servo pin number.

                                            M950 S0 C"exp.heater3"
                                            

                                            The contents of deployprobe.g should look like this based upon your config.g (P0 = S0 = pin number):

                                            M280 P0 S10 
                                            

                                            And second your retractprobe.g would be:

                                            M280 P0 S90
                                            

                                            Issue single M401 and M402 to see if your BL responds.

                                            Messiahmanundefined 1 Reply Last reply Reply Quote 0
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