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    Toolboard keeps loosing heater 1

    Scheduled Pinned Locked Moved
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    • wdenkerundefined
      wdenker
      last edited by

      I keep getting random failures on my toolboard where it looses heater 1. We thought it was heat caused and we were able to get it under control but now we don't know where to look. Here is the m122 b121 and m122 as well as the config.g I am at a loss. We know our can communication is good at this point as well. 353048714_207127645607570_4429003242776518252_n.jpg config (12).g

      M122 B121
      Diagnostics for board 121:
      Duet TOOL1LC rev 1.1 or later firmware version 3.4.4 (2022-10-14 11:46:33)
      Bootloader ID: SAMC21 bootloader version 2.4 (2021-12-10)
      All averaging filters OK
      Never used RAM 3080, free system stack 45 words
      Tasks: Move(notifyWait,1.7%,91) HEAT(notifyWait,0.1%,115) CanAsync(notifyWait,0.0%,65) CanRecv(notifyWait,0.3%,74) CanClock(notifyWait,0.0%,65) ACCEL(notifyWait,0.0%,61) TMC(delaying,3.1%,57) MAIN(running,89.8%,441) IDLE(ready,0.0%,26) AIN(delaying,5.1%,142), total 100.0%
      Last reset 00:01:42 ago, cause: power up
      Last software reset data not available
      Driver 0: pos 183615, 80.0 steps/mm,ok, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 50700, writes 9, timeouts 0, DMA errors 0, CC errors 0, steps req 230109 done 229541
      Moves scheduled 4302, completed 4296, in progress 1, hiccups 0, step errors 0, maxPrep 595, maxOverdue 59723241, maxInc 59723061, mcErrs 0, gcmErrs 0
      Peak sync jitter 0/4, peak Rx sync delay 216, resyncs 0/0, next step interrupt due in 43 ticks, enabled
      VIN voltage: min 24.3, current 24.4, max 24.6
      MCU temperature: min 59.7C, current 60.3C, max 61.4C
      Last sensors broadcast 0x00000000 found 0 173 ticks ago, 0 ordering errs, loop time 0
      CAN messages queued 842, send timeouts 0, received 5235, lost 0, free buffers 37, min 36, error reg 0
      dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 496, adv -59723030/74654
      Accelerometer: LIS3DH, status: 00
      I2C bus errors 1, naks 3, other errors 0

      M122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.4.5 (2022-11-30 19:35:23) running on Duet 3 MB6HC v1.02 or later (standalone mode)
      Board ID: 08DJM-9P63L-DJ3S0-7J9D4-3SN6J-9UMZA
      Used output buffers: 3 of 40 (40 max)
      === RTOS ===
      Static ram: 152760
      Dynamic ram: 99104 of which 0 recycled
      Never used RAM 97704, free system stack 114 words
      Tasks: NETWORK(ready,65.1%,220) ETHERNET(notifyWait,1.9%,401) HEAT(notifyWait,0.4%,322) Move(notifyWait,40.1%,245) CanReceiv(notifyWait,0.7%,772) CanSender(notifyWait,0.8%,326) CanClock(delaying,0.1%,339) TMC(notifyWait,61.7%,57) MAIN(running,56.1%,925) IDLE(ready,0.0%,30), total 227.1%
      Owned mutexes:
      === Platform ===
      Last reset 27:05:39 ago, cause: power up
      Last software reset at 2023-06-12 23:10, reason: User, GCodes spinning, available RAM 95568, slot 0
      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task MAIN Freestk 0 n/a
      Error status: 0x04
      Aux0 errors 0,3,0
      Step timer max interval 277
      MCU temperature: min 31.8, current 37.6, max 41.8
      Supply voltage: min 23.8, current 24.1, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 11.9, current 12.2, max 12.5, under voltage events: 0
      Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
      Events: 0 queued, 0 completed
      Driver 0: ok, SG min 0, mspos 234, reads 26227, writes 68 timeouts 0
      Driver 1: standstill, SG min n/a, mspos 8, reads 26295, writes 0 timeouts 0
      Driver 2: ok, SG min 0, mspos 579, reads 26226, writes 68 timeouts 0
      Driver 3: ok, SG min 0, mspos 549, reads 26245, writes 50 timeouts 0
      Driver 4: ok, SG min 0, mspos 709, reads 26245, writes 50 timeouts 0
      Driver 5: ok, SG min 0, mspos 234, reads 26227, writes 68 timeouts 0
      Date/time: 2023-06-15 21:27:48
      Slowest loop: 789.25ms; fastest: 0.04ms
      === Storage ===
      Free file entries: 9
      SD card 0 detected, interface speed: 25.0MBytes/sec
      SD card longest read time 4.0ms, write time 43.5ms, max retries 0
      === Move ===
      DMs created 125, segments created 46, maxWait 9424672ms, bed compensation in use: mesh, comp offset 0.000
      === MainDDARing ===
      Scheduled moves 191582, completed 191522, hiccups 0, stepErrors 0, LaErrors 0, Underruns [32, 0, 10], CDDA state 3
      === AuxDDARing ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters 2 -1 -1 -1, ordering errs 0
      Heater 0 is on, I-accum = 0.0
      Heater 2 is on, I-accum = 0.0
      === GCodes ===
      Segments left: 1
      Movement lock held by null
      HTTP is idle in state(s) 0
      Telnet is idle in state(s) 0
      File is doing "G1 F5065.426" in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon is idle in state(s) 0
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      Code queue is empty
      === CAN ===
      Messages queued 3879546, received 2688079, lost 0, boc 0
      Longest wait 7ms for reply type 6024, peak Tx sync delay 571, free buffers 50 (min 36), ts 480652/480652/0
      Tx timeouts 0,0,0,0,0,0
      === Network ===
      Slowest loop: 2628.63ms; fastest: 0.03ms
      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
      HTTP sessions: 1 of 8
      = Ethernet =
      State: active
      Error counts: 0 0 13 0 0 0
      Socket states: 5 2 2 2 2 2 0 2
      = WiFi =
      Network state is disabled
      WiFi module is disabled
      Failed messages: pending 2779096485, notready 2779096485, noresp 2779096485
      Socket states: 0 0 0 0 0 0 0 0
      === Multicast handler ===
      Responder is inactive, messages received 0, responses 0

      www.bd3dcustoms.com | BD3DCUSTOMS Supercube

      elmoretundefined jay_s_ukundefined 2 Replies Last reply Reply Quote 0
      • elmoretundefined
        elmoret @wdenker
        last edited by

        @dc42 @T3P3Tony

        1 Reply Last reply Reply Quote 0
        • jay_s_ukundefined
          jay_s_uk @wdenker
          last edited by

          @wdenker looks like you have a power issue as the toolboard reset 1 min 42 before the M122.
          in RRF 3.4, the firmware doesn't know if a toolboard/expansion board has been lost. This functionality has been added in 3.5b4. you could update to that and keep an eye on things (3.5b4 prints ok for me)

          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

          wdenkerundefined 1 Reply Last reply Reply Quote 0
          • wdenkerundefined
            wdenker @jay_s_uk
            last edited by

            @jay_s_uk sadly the customer likes to pull the power to reset. So that is not the issue.

            www.bd3dcustoms.com | BD3DCUSTOMS Supercube

            jay_s_ukundefined 1 Reply Last reply Reply Quote 0
            • jay_s_ukundefined
              jay_s_uk @wdenker
              last edited by

              @wdenker they pull the power on the toolboard but not the mainboard?
              anyway, if they do that then my comment about the mainboard not knowing still stands

              Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

              wdenkerundefined 1 Reply Last reply Reply Quote 0
              • wdenkerundefined
                wdenker @jay_s_uk
                last edited by wdenker

                @jay_s_uk The heater loss doesn't persist after the pull of power. Because the customer knows hey if I pull power it'll come back and I can start over. He then grabs the m122 separately from each other, one before the power loss and one after.

                www.bd3dcustoms.com | BD3DCUSTOMS Supercube

                jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                • jay_s_ukundefined
                  jay_s_uk @wdenker
                  last edited by

                  @wdenker so why does the M122 for mainboard show an uptime of 27 hours and the M122 for the toolboard shows 1 minute?

                  Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                  wdenkerundefined 1 Reply Last reply Reply Quote 0
                  • wdenkerundefined
                    wdenker @jay_s_uk
                    last edited by

                    @jay_s_uk because the m122 was pulled for one before the power was pulled and one after.

                    www.bd3dcustoms.com | BD3DCUSTOMS Supercube

                    jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                    • jay_s_ukundefined
                      jay_s_uk @wdenker
                      last edited by

                      @wdenker its probably a communication/cable issue anyway but you won't know with 3.4.5 as it doesn't tell you

                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                      wdenkerundefined 1 Reply Last reply Reply Quote 0
                      • wdenkerundefined
                        wdenker @jay_s_uk
                        last edited by

                        @jay_s_uk the can cable communication light never blinks irratic. We originally had an issue with the can connection. We have resolved it since and now getting this error vs stuff just stopping like it lost connection briefly. Which is how a bad can cable presents itself.

                        www.bd3dcustoms.com | BD3DCUSTOMS Supercube

                        jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                        • jay_s_ukundefined
                          jay_s_uk @wdenker
                          last edited by

                          @wdenker update to 3.5b4 so you can see if there are any reports of a CAN board not communicating.

                          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                          wdenkerundefined 1 Reply Last reply Reply Quote 1
                          • wdenkerundefined
                            wdenker @jay_s_uk
                            last edited by

                            @jay_s_uk found a good indicator... I2C bus errors 1 is what shows when it is having the issue, errors 0 when not having the issue. So am I safe to assume it is can connection again even though nothing else indicating can connection issues? I also updated to 3.5.0-beta.4 and am not getting any notifications about can timeout or connection issues which I would have expected.

                            www.bd3dcustoms.com | BD3DCUSTOMS Supercube

                            wdenkerundefined 1 Reply Last reply Reply Quote 0
                            • wdenkerundefined
                              wdenker @wdenker
                              last edited by

                              @wdenker @dc42 any insight?

                              www.bd3dcustoms.com | BD3DCUSTOMS Supercube

                              T3P3Tonyundefined 1 Reply Last reply Reply Quote 0
                              • T3P3Tonyundefined
                                T3P3Tony administrators @wdenker
                                last edited by

                                @wdenker Do you have the opportunity to swap the toolboard in case its a hardware issue? The I2C bus error is not directly related to the heater (its used for the LIS3DH only, however its interesting that they happen at the same time.

                                How hot are you running the toolboard?

                                www.duet3d.com

                                wdenkerundefined 1 Reply Last reply Reply Quote 0
                                • wdenkerundefined
                                  wdenker @T3P3Tony
                                  last edited by

                                  @T3P3Tony we swapped to new board and still getting the same issue just not as frequent. So we then decided to swap the thermistor ports to a phoenix connector instead of the JST. Seems like this has resolved the issue. What else does that error indicate or work with other than the accelerometer?

                                  www.bd3dcustoms.com | BD3DCUSTOMS Supercube

                                  dc42undefined wdenkerundefined 2 Replies Last reply Reply Quote 0
                                  • dc42undefined
                                    dc42 administrators @wdenker
                                    last edited by

                                    @wdenker the message "Board 121 does not have heater 1" implies that the tool board has reset. The M122 B121 report indicates that it was not a firmware crash or other software reset, because the Last Software Reset Data is shown as "not available". So it must have been a watchdog reset, hardware reset, or power failure. Therefore, we need to see M122 reports for both boards before pulling the power, to determine the reason for the tool board reset. Please ask your customer to provide this next time the fault occurs.

                                    Duet WiFi hardware designer and firmware engineer
                                    Please do not ask me for Duet support via PM or email, use the forum
                                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                                    1 Reply Last reply Reply Quote 0
                                    • wdenkerundefined
                                      wdenker @wdenker
                                      last edited by

                                      @dc42 or @T3P3Tony Here are the M122 from each board prior to power restart. Looks like toolboard ran out of memory. 2023-06-21 10:39, reason: OutOfMemory, How do I resolve that?

                                      M122
                                      === Diagnostics ===
                                      RepRapFirmware for Duet 3 MB6HC version 3.5.0-beta.4 (2023-06-08 23:41:30) running on Duet 3 MB6HC v1.02 or later (standalone mode)
                                      Board ID: 08DJM-9P63L-DJ3S0-7J9D4-3SN6J-9UMZA
                                      Used output buffers: 9 of 40 (40 max)
                                      === RTOS ===
                                      Static ram: 155012
                                      Dynamic ram: 121824 of which 52 recycled
                                      Never used RAM 67352, free system stack 122 words
                                      Tasks: NETWORK(1,ready,33.0%,139) ETHERNET(5,nWait,2.1%,317) HEAT(3,nWait,1.3%,323) Move(4,nWait,88.6%,214) CanReceiv(6,nWait,1.7%,642) CanSender(5,nWait,2.0%,326) CanClock(7,delaying,0.3%,349) TMC(4,nWait,131.2%,59) MAIN(1,running,137.7%,137) IDLE(0,ready,0.5%,30), total 398.4%
                                      Owned mutexes:
                                      === Platform ===
                                      Last reset 50:22:42 ago, cause: power up
                                      Last software reset at 2023-06-17 02:19, reason: User, Gcodes spinning, available RAM 68440, slot 1
                                      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0043c000 BFAR 0x00000000 SP 0x00000000 Task MAIN Freestk 0 n/a
                                      Error status: 0x14
                                      Aux0 errors 0,6,0
                                      MCU temperature: min 30.3, current 40.2, max 43.8
                                      Supply voltage: min 23.8, current 24.1, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
                                      12V rail voltage: min 11.9, current 12.2, max 12.6, under voltage events: 0
                                      Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                                      Events: 13 queued, 13 completed
                                      Driver 0: standstill, SG min 0, mspos 976, reads 2699, writes 208 timeouts 0
                                      Driver 1: standstill, SG min n/a, mspos 8, reads 2896, writes 11 timeouts 0
                                      Driver 2: standstill, SG min 0, mspos 80, reads 2707, writes 200 timeouts 0
                                      Driver 3: standstill, SG min 0, mspos 112, reads 2738, writes 169 timeouts 0
                                      Driver 4: standstill, SG min 0, mspos 880, reads 2738, writes 169 timeouts 0
                                      Driver 5: standstill, SG min 0, mspos 464, reads 2700, writes 208 timeouts 0
                                      Date/time: 2023-06-21 11:11:07
                                      Slowest loop: 1000.15ms; fastest: 0.05ms
                                      === Storage ===
                                      Free file entries: 18
                                      SD card 0 detected, interface speed: 25.0MBytes/sec
                                      SD card longest read time 4.5ms, write time 380.9ms, max retries 0
                                      === Move ===
                                      DMs created 125, segments created 73, maxWait 5933869ms, bed compensation in use: mesh, height map offset 0.000, ebfmin 0.00, ebfmax 0.00
                                      no step interrupt scheduled
                                      === DDARing 0 ===
                                      Scheduled moves 102436, completed 102436, hiccups 0, stepErrors 0, LaErrors 0, Underruns [341, 0, 24], CDDA state -1
                                      === DDARing 1 ===
                                      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                      === Heat ===
                                      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters 2 -1 -1 -1, ordering errs 0
                                      Heater 0 is on, I-accum = 0.0
                                      Heater 2 is on, I-accum = 0.0
                                      === GCodes ===
                                      Movement locks held by null, null
                                      HTTP is idle in state(s) 0
                                      Telnet is idle in state(s) 0
                                      File is idle in state(s) 0
                                      USB is idle in state(s) 0
                                      Aux is idle in state(s) 0
                                      Trigger is idle in state(s) 0
                                      Queue is idle in state(s) 0
                                      LCD is idle in state(s) 0
                                      SBC is idle in state(s) 0
                                      Daemon is idle in state(s) 0
                                      Aux2 is idle in state(s) 0
                                      Autopause is idle in state(s) 0
                                      File2 is idle in state(s) 0
                                      Queue2 is idle in state(s) 0
                                      Q0 segments left 0, axes/extruders owned 0x80000007
                                      Code queue 0 is empty
                                      Q1 segments left 0, axes/extruders owned 0x0000000
                                      Code queue 1 is empty
                                      === CAN ===
                                      Messages queued 7095317, received 5098900, lost 0, boc 56
                                      Longest wait 5ms for reply type 6029, peak Tx sync delay 623, free buffers 50 (min 47), ts 906815/906786/0
                                      Tx timeouts 0,0,0,0,0,0
                                      === Network ===
                                      Slowest loop: 8427.39ms; fastest: 0.03ms
                                      Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
                                      HTTP sessions: 1 of 8
                                      = Ethernet =
                                      Interface state: active
                                      Error counts: 0 0 0 1 0 0
                                      Socket states: 5 2 2 2 2 2 0 2
                                      = WiFi =
                                      Interface state: disabled
                                      Module is disabled
                                      Failed messages: pending 0, notready 0, noresp 0
                                      Socket states: 0 0 0 0 0 0 0 0
                                      === Multicast handler ===
                                      Responder is inactive, messages received 0, responses 0

                                      M122 B121
                                      Diagnostics for board 121:
                                      Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-beta.4 (2023-06-08 16:22:30)
                                      Bootloader ID: SAMC21 bootloader version 2.4 (2021-12-10)
                                      All averaging filters OK
                                      Never used RAM 1812, free system stack 88 words
                                      Tasks: Move(3,nWait,0.7%,111) HEAT(2,nWait,0.1%,101) CanAsync(5,nWait,0.0%,54) CanRecv(3,nWait,0.1%,75) CanClock(5,nWait,0.0%,66) ACCEL(3,nWait,0.0%,53) TMC(2,delaying,3.1%,57) MAIN(1,running,90.8%,444) IDLE(0,ready,0.0%,27) AIN(2,delaying,5.1%,142), total 100.0%
                                      Last reset 00:10:46 ago, cause: power up
                                      Last software reset at 2023-06-21 10:39, reason: OutOfMemory, available RAM 12, slot 0
                                      Software reset code 0x01c0 ICSR 0x00000000 SP 0x200054a8 Task Move Freestk 137 ok
                                      Stack: 20005600 000062df 00000000 2000554c a5a5a5a5 00009f99 00000000 00008a67 0001f1c6 00000000 477e8400 477e8400 0000005b 007e8400 a625a5a5 a5a5a5a5 0001ee68 477e8400 477fa700 2e57b417 2e57b417 2000554c 20007100 20005108 3627cde7 00008c77 bdd53594
                                      Driver 0: pos 0, 80.0 steps/mm, standstill, SG min 0, read errors 0, write errors 0, ifcnt 9, reads 59686, writes 9, timeouts 3, DMA errors 0, CC errors 0, failedOp 0x72, steps req 0 done 1157273
                                      Moves scheduled 13624, completed 13624, in progress 0, hiccups 468, step errors 0, maxPrep 602, maxOverdue 2022819261, maxInc 2022780880, mcErrs 0, gcmErrs 0, ebfmin 0.00, ebfmax 1.00
                                      Peak sync jitter 0/5, peak Rx sync delay 261, resyncs 0/0, no timer interrupt scheduled
                                      VIN voltage: min 24.6, current 24.7, max 24.8
                                      MCU temperature: min 58.7C, current 60.5C, max 61.1C
                                      Last sensors broadcast 0x00000000 found 0 30 ticks ago, 0 ordering errs, loop time 0
                                      CAN messages queued 5200, send timeouts 0, received 19467, lost 0, free buffers 18, min 16, error reg 0
                                      dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 837, adv -2022819048/74672
                                      Accelerometer: LIS3DH, status: 00
                                      I2C bus errors 0, naks 3, other errors 0

                                      Diagnostics for board 1:
                                      Duet EXP3HC rev 1.02 or later firmware version 3.5.0-beta.4 (2023-06-08 16:24:05)
                                      Bootloader ID: SAME5x bootloader version 2.3 (2021-01-26b1)
                                      All averaging filters OK
                                      Never used RAM 156016, free system stack 172 words
                                      Tasks: Move(3,nWait,1.1%,104) HEAT(2,nWait,1.2%,82) CanAsync(5,nWait,0.0%,67) CanRecv(3,nWait,1.4%,79) CanClock(5,nWait,0.4%,70) TMC(2,nWait,135.7%,69) MAIN(1,running,46.7%,456) IDLE(0,ready,0.0%,40) AIN(2,delaying,61.7%,265), total 248.2%
                                      Last reset 50:23:10 ago, cause: power up
                                      Last software reset data not available
                                      Driver 0: pos -6382700, 320.0 steps/mm, standstill, SG min 0, mspos 464, reads 3139, writes 165 timeouts 0, steps req 6 done 4042678
                                      Driver 1: pos -6382777, 320.0 steps/mm, standstill, SG min 0, mspos 880, reads 3140, writes 165 timeouts 0, steps req 6 done 4042745
                                      Driver 2: pos 0, 80.0 steps/mm, standstill, SG min 0, mspos 8, reads 3295, writes 11 timeouts 0, steps req 0 done 0
                                      Moves scheduled 1377083, completed 1377083, in progress 0, hiccups 0, step errors 0, maxPrep 52, maxOverdue 41, maxInc 11, mcErrs 0, gcmErrs 0, ebfmin 0.00, ebfmax 0.00
                                      Peak sync jitter -8/9, peak Rx sync delay 188, resyncs 0/0, no timer interrupt scheduled
                                      VIN voltage: min 24.2, current 24.3, max 24.4
                                      V12 voltage: min 12.3, current 12.3, max 12.4
                                      MCU temperature: min 43.1C, current 47.2C, max 51.2C
                                      Last sensors broadcast 0x00000000 found 0 30 ticks ago, 0 ordering errs, loop time 0
                                      CAN messages queued 1451192, send timeouts 0, received 3716073, lost 0, free buffers 38, min 38, error reg ff0000
                                      dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 420, adv 8041/74573

                                      www.bd3dcustoms.com | BD3DCUSTOMS Supercube

                                      jay_s_ukundefined dc42undefined 2 Replies Last reply Reply Quote 0
                                      • jay_s_ukundefined
                                        jay_s_uk @wdenker
                                        last edited by

                                        @wdenker see this thread https://forum.duet3d.com/topic/32694/3-5-0-b4-having-random-can-error-timeouts/14

                                        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                        wdenkerundefined 1 Reply Last reply Reply Quote 0
                                        • wdenkerundefined
                                          wdenker @jay_s_uk
                                          last edited by

                                          @jay_s_uk already have tried that.

                                          www.bd3dcustoms.com | BD3DCUSTOMS Supercube

                                          wdenkerundefined 1 Reply Last reply Reply Quote 0
                                          • dc42undefined
                                            dc42 administrators @wdenker
                                            last edited by

                                            @wdenker the out of memory issue is new in firmware 3.5.0-beta.4. If you have already tried using a less demanding input shaping method then I suggest you revert to firmware 3.4.5 on the main board (and 3.4.4 on the tool board, which is the version included in the 3.4.5 release). Then when the problem happens again, get a M122 B121 report again before powering down.

                                            Duet WiFi hardware designer and firmware engineer
                                            Please do not ask me for Duet support via PM or email, use the forum
                                            http://www.escher3d.com, https://miscsolutions.wordpress.com

                                            wdenkerundefined 1 Reply Last reply Reply Quote 0
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