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    Jerk & acceleration value change after Resume APF

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    Beta Firmware
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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      Can you verify if the behaviour is the same in 3.4.6?

      Z-Bot CoreXY Build | Thingiverse Profile

      R006undefined 1 Reply Last reply Reply Quote 0
      • R006undefined
        R006 @Phaedrux
        last edited by

        @Phaedrux We have already verified with 3.4.6 and 3.4beta3, and same thing is happening.

        dc42undefined 1 Reply Last reply Reply Quote 0
        • dc42undefined
          dc42 administrators @R006
          last edited by

          @R006 the generated resurrect.g file does not currently restore the M204 acceleration settings or the jerk settings. Feel free to create an issue at https://github.com/Duet3D/RepRapFirmware/issues.

          Duet WiFi hardware designer and firmware engineer
          Please do not ask me for Duet support via PM or email, use the forum
          http://www.escher3d.com, https://miscsolutions.wordpress.com

          1 Reply Last reply Reply Quote 1
          • T3P3Tonyundefined
            T3P3Tony administrators @R006
            last edited by

            @R006 to be clear, the reported values after a restore after power failure are the ones you have set in config.g?

            www.duet3d.com

            R006undefined 1 Reply Last reply Reply Quote 0
            • R006undefined
              R006 @T3P3Tony
              last edited by

              @T3P3Tony
              no in config Acceleration is 3000mm/s2 and jerk is 300mm/s.

              T3P3Tonyundefined 1 Reply Last reply Reply Quote 0
              • T3P3Tonyundefined
                T3P3Tony administrators @R006
                last edited by

                @R006 ok so are the values that are restored related to anything in your settings or gcode file?

                www.duet3d.com

                JayTundefined 1 Reply Last reply Reply Quote 0
                • JayTundefined
                  JayT @T3P3Tony
                  last edited by

                  @T3P3Tony :

                  I use this version too and have observed same problems. The value of acceleration on resume is not something I am able to trace from gcode file or config. Its some random very high value like 20000 or 50000. even jerk changes.

                  I have also observed, that despite setting max acceleration & speeds in config, its not limited on resume after power failure. Can you check this?

                  dc42undefined 1 Reply Last reply Reply Quote 0
                  • dc42undefined
                    dc42 administrators @JayT
                    last edited by

                    @JayT @R006 in the forthcoming 3.5.0-rc.4 the M204 acceleration settings are restored when resuming after power fail.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    JayTundefined R006undefined 2 Replies Last reply Reply Quote 1
                    • JayTundefined
                      JayT @dc42
                      last edited by

                      @dc42 :

                      Noted.
                      However, there are 2 more errors that appear on resume:
                      a) tool0 was not driven because its heater temperature were not high enough. heater fault. Yet it resumes, but why this error?

                      b) Loading the heightmap before setting duetZ0 - warning,

                      dc42undefined 1 Reply Last reply Reply Quote 0
                      • dc42undefined
                        dc42 administrators @JayT
                        last edited by

                        @JayT regarding (a) it's your responsibility to use M116 or a similar command in your resurrect-prologue.g file to wait for temperatures to be reached. Are you doing that?

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        JayTundefined 1 Reply Last reply Reply Quote 0
                        • JayTundefined
                          JayT @dc42
                          last edited by JayT

                          @dc42 :

                          My resurrect-prologue.g file is as below, it has M116 to wait.
                          ;rel
                          G91
                          G1 Z2
                          G28 X Y
                          ;wait
                          M116
                          ;rel
                          M83
                          M21 P1
                          G1 E5 F500
                          ;mesh
                          G29 S1
                          ;Buzz
                          M300 S600 P100
                          ;Buzz
                          M300 S700 P1200
                          ;Buzz
                          M300 S500 P300
                          ;Abs
                          G90

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                          • R006undefined
                            R006 @dc42
                            last edited by R006

                            @dc42 hey,

                            After upgrading to the latest firmware version 3.5.0rc4, we observed improvement in print acceleration settings. However, the travel acceleration is taking random value: while print acceleration seems to be functioning correctly, travel acceleration values are fluctuating unexpectedly.

                            dc42undefined 1 Reply Last reply Reply Quote 1
                            • dc42undefined
                              dc42 administrators @R006
                              last edited by

                              @R006 please check whether the M204 command in resurrect.g is setting the correct travel acceleration for resuming the print.

                              Duet WiFi hardware designer and firmware engineer
                              Please do not ask me for Duet support via PM or email, use the forum
                              http://www.escher3d.com, https://miscsolutions.wordpress.com

                              JayTundefined 1 Reply Last reply Reply Quote 0
                              • JayTundefined
                                JayT @dc42
                                last edited by JayT

                                @dc42 :

                                with RC4, sometimes it resumes fine with minimal offset. Whereas sometimes it shift by 5-8mm in Y direction for me on resume after power failure. Mostly it shifting by >5mm happens when print height is <5mm. So i disabled meshbed compensation & tried. It still has the same problem.

                                There are instances when even at height 3mm, it resumes fine.
                                skew in YZ is included. Does that have any effect?

                                What should I check for ?
                                Shift is always in Y axis & amount of shift is more w.r.t X axis.

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