Like Z Banding
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@Notepad Well, I have now changed the SSR, but I am still getting some fluctuation, but at least some are fault free. Here are the results:
M307 H0 R0.863 K0.260:0.000 D5.37 E1.35 S1.00 B0 XXXXXX
M307 H0 R0.875 K0.265:0.000 D5.36 E1.35 S1.00 B0 XXXXXX
M307 H0 R0.874 K0.346:0.000 D5.72 E1.35 S1.00 B0
M307 H0 R0.856 K0.307:0.000 D4.85 E1.35 S1.00 B0
M307 H0 R0.852 K0.301:0.000 D5.32 E1.35 S1.00 B0 XXXXXXXXXXXX = Warning: heater behaviour was not consistent during tuning
My next step of thinking down this rabbit hole of fluctuation is, where I have used RTV to refix the silicon heater could the layer be too thick or uneven (It’s not easy stuff to work with) causing a slow transition of heat, resulting in a slow reaction that the PID loop is struggling with?
Does anyone know of anywhere in the UK, where I can get a good 330 x 330mm 240v high temp (I print a lot of ABS and the like) silicon heater. At a good price and quick delivery? As even Keenovo has started using a NTC 100K thermistor on there heaters which from what I understand can be a pain to setup and not that great for the higher temps.
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@Ce72 said in Like Z Banding:
NTC 100K thermistor on there heaters which from what I understand can be a pain to setup and not that great for the higher temps.
Bed temps are pretty low compared to extruder temps. I don't see a problem here?
Whenever a NTC failed on me, it was a lousy crimpjob or broken thermistor leg from too much motion. -
@o_lampe Thank you for pointing that out, I have ordered a new heater, and when it's been installed I will post back here the results hopefully it will cure the banding issue.
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So, this is now confusing, I have replaced the relay and fitted a new Silicon heater back to the original setup, which ran perfectly fine for 2 years. And when I run the PID tuning cycle I now constantly get:
Warning: heater behaviour was not consistent during tuning
M307 H0 R0.779 K0.208:0.000 D5.70 E1.35 S1.00 B0
M307 H0 R0.776 K0.270:0.000 D5.24 E1.35 S1.00 B0
M307 H0 R0.789 K0.265:0.000 D5.85 E1.35 S1.00 B0
M307 H0 R0.779 K0.247:0.000 D5.35 E1.35 S1.00 B0
M307 H0 R0.778 K0.257:0.000 D5.49 E1.35 S1.00 B0Could it be the heater output on the mainboard? Is it possible to use a spare extruder output as I’m running through a relay? To test.
Has anyone got any suggestions?
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@Ce72 Most likely is that the thermal pad's thermistor is too close to the heating element, so reads higher than the rest of the bed surface when the heater is on (localised hotter temperature), then cools quicker than expected as heat dissipates through the bed. This tends to make the heating cycles shorter as they go on, causing the inconsistent behaviour, and long tuning cycle.
However, the tuning numbers you're getting are all pretty close, I'd think choosing the median for each parameter would be fine. If it triggers heater errors when heating normally, you can manually adjust it, see https://docs.duet3d.com/User_manual/Connecting_hardware/Heaters_tuning#manual-adjustments-to-the-heater-model-parameters
Ian
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Hi Ian thank you for pointing me in the right direction to set the PID tune.
Then I run some tests to see If the banding had finally gone, unfortunately not so I decided to run some other tests to see if I could isolate the problem or ever just work out what effects the banding pattern.
This is the first test print after changing the heater and SSR as well as retuning the extruder PID. banding is the same as before.
The next test I turned off the bed heater after the first couple of layers. To see if the banding was being affected by the bang-bang theory being caused by the bed heater but the banding was still the same. This left me wondering if it was a back to a mechanical issue the good old Z wobble as nothing electrical or extruder seemed to be affecting the outcome.
The last test I did after reimaging the pi (hey try anything at this point ) This time I resized the test model from a 40mm cube the a 80mm square by 25mm high same slicing profile as before but this time the banding was a lot closer together than before, To me me this eliminates a mechanical problem as the pattern frequence is so far away from the ball screw pitch.
As mentioned earlier in this thread I have also tried a diffent slicer, so it’s also not that
I’m running out of things to try so any further suggestions from anyonre would be greatly appreciated
And sorry for the long post. -
@Ce72 Just to eliminate it as a possibility can you turn of Pressure Advance to see if there is any effect.
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@tas Hi, Here's the result of of No PA
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I'm inclined to think it's a mechanical issue either in the extruder or Z axis.
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Here's a wild theory - there's some interaction between the bed heater and the extruder heater, such that when the bed heater turns on, the power to the extruder heater is reduced slightly, leading to small variations in the flow of plastic. If the duty cycle on the bed heater is regular, it could lead to a regular pattern in the output.
It seems unlikely because the relay you pictured shows your bed is heated by AC. But maybe something on the control side is sinking too much current.
You could test by monitoring the voltage and duty cycle to the extruder heater.
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@mikeabuilder Hi, Thank you for your thoughts, but after going down the rabbit hole replacing the SSR and bed heater, I tried running a test print with the bed heater turned off to try and eliminate the bed heater and I still had the same results. but I'm not that clued up on electrics to know if that would negate any effects.
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@Ce72 Hi, thank you for your input and any suggested test are much appreciated. I have tried changing the extruder gears and that unfortunatly had no effect, as for z wobble I would have thought the pattern would be the same on all faces, but what I have noticed is that the pattern changes direction and not on opposite face so it just adds to my confusion