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    DUEX 5 V0.8 TO DUEX 5 V0.11

    Scheduled Pinned Locked Moved
    Duet Hardware and wiring
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    • paolozampini1973undefined
      paolozampini1973 @droftarts
      last edited by

      @droftarts I want to ask a question I do not know if I have explained myself you have understood that for me the problem has worsened a lot to install the V 0.11 for me it was much worse I have a lot of problems so many problems that I did not have before please answer me if I have been clear Please please

      tekkydaveundefined 1 Reply Last reply Reply Quote 0
      • tekkydaveundefined
        tekkydave @paolozampini1973
        last edited by

        @paolozampini1973 Yes you are correct. But now you have two choices:

        1. Accept that your new engine is crap and go back to the old one.
        2. Take some advice on how to work round the issues you have and fix them to get your car working again.

        You seem very reluctant to take option 2. If you read back over the advice in this thread all the answers are there. If you supply us with the information we have asked for - the output of the M122 command and your config.g we can help even more.

        ~ tekkydave ~
        D-Bot: 300x300mm | Duet WiFi + Duex2 | 3 independent z motors | X,Y & Z linear rails | E3D Titan Aero + V6 | Precision Piezo z-probe
        FreeCAD, PrusaSlicer

        paolozampini1973undefined 1 Reply Last reply Reply Quote 0
        • tekkydaveundefined
          tekkydave @paolozampini1973
          last edited by

          @paolozampini1973 said in DUEX 5 V0.8 TO DUEX 5 V0.11:

          @droftarts I want to ask a question I do not know if I have explained myself you have understood that for me the problem has worsened a lot to install the V 0.11 for me it was much worse I have a lot of problems so many problems that I did not have before please answer me if I have been clear Please please

          Yes very clear. We all understand it has got worse for you. Move on from that and give us the information we need to help you.

          ~ tekkydave ~
          D-Bot: 300x300mm | Duet WiFi + Duex2 | 3 independent z motors | X,Y & Z linear rails | E3D Titan Aero + V6 | Precision Piezo z-probe
          FreeCAD, PrusaSlicer

          1 Reply Last reply Reply Quote 0
          • paolozampini1973undefined
            paolozampini1973 @tekkydave
            last edited by

            @tekkydave 30273fb4-d2dc-4112-a692-7fbb74328c0d-image.png 73aa5151-9de2-476e-bd78-7fe6c85f9119-image.png 47aabfb4-ee75-423c-b892-66cc8e993c1b-image.png c6c27765-945d-4e05-93bc-fbe65fe5951e-image.png

            droftartsundefined 1 Reply Last reply Reply Quote 0
            • droftartsundefined
              droftarts administrators @paolozampini1973
              last edited by

              @paolozampini1973 You know you can just copy and paste text from the Console window?

              Ian

              Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

              paolozampini1973undefined 1 Reply Last reply Reply Quote 0
              • paolozampini1973undefined
                paolozampini1973 @droftarts
                last edited by

                @droftarts 21/3/2022, 14:42:59 M122
                === Diagnostics ===
                RepRapFirmware for Duet 2 WiFi/Ethernet version 3.3 (2021-06-15 21:44:54) running on Duet WiFi 1.02 or later + DueX2
                Board ID: 0JD0M-9P6M2-NW4SN-6J1DD-3SJ6K-KAURK
                Used output buffers: 3 of 24 (24 max)
                === RTOS ===
                Static ram: 23876
                Dynamic ram: 77448 of which 0 recycled
                Never used RAM 13092, free system stack 184 words
                Tasks: NETWORK(ready,15.8%,233) HEAT(delaying,0.0%,330) Move(notifyWait,0.1%,319) DUEX(notifyWait,0.0%,24) MAIN(running,81.5%,413) IDLE(ready,2.6%,29), total 100.0%
                Owned mutexes: WiFi(NETWORK)
                === Platform ===
                Last reset 00:00:29 ago, cause: power up
                Last software reset at 2022-03-20 12:12, reason: User, GCodes spinning, available RAM 13092, slot 0
                Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                Error status: 0x00
                Aux0 errors 0,0,0
                Step timer max interval 0
                MCU temperature: min 24.0, current 27.5, max 27.7
                Supply voltage: min 25.6, current 25.7, max 25.8, under voltage events: 0, over voltage events: 0, power good: yes
                Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                Driver 0: position 0, standstill, SG min/max not available
                Driver 1: position 0, standstill, SG min/max not available
                Driver 2: position 0, standstill, SG min/max not available
                Driver 3: position 0, standstill, SG min/max not available
                Driver 4: position 0, standstill, SG min/max not available
                Driver 5: position 0, standstill, SG min/max not available
                Driver 6: position 0, standstill, SG min/max not available
                Driver 7: position 0
                Driver 8: position 0
                Driver 9: position 0
                Driver 10: position 0
                Driver 11: position 0
                Date/time: 2022-03-21 14:42:57
                Cache data hit count 1127564131
                Slowest loop: 10.85ms; fastest: 0.18ms
                I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                === Storage ===
                Free file entries: 10
                SD card 0 detected, interface speed: 20.0MBytes/sec
                SD card longest read time 1.0ms, write time 0.0ms, max retries 0
                === Move ===
                DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                === MainDDARing ===
                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                === AuxDDARing ===
                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                === Heat ===
                Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                Heater 1 is on, I-accum = 0.0
                === GCodes ===
                Segments left: 0
                Movement lock held by null
                HTTP is idle in state(s) 0
                Telnet is idle in state(s) 0
                File is idle in state(s) 0
                USB is idle in state(s) 0
                Aux is idle in state(s) 0
                Trigger is idle in state(s) 0
                Queue is idle in state(s) 0
                LCD is idle in state(s) 0
                Daemon is idle in state(s) 0
                Autopause is idle in state(s) 0
                Code queue is empty.
                === Filament sensors ===
                Extruder 0 sensor: no filament
                Extruder 1 sensor: ok
                Extruder 2 sensor: no filament
                Extruder 3 sensor: ok
                === DueX ===
                Read count 1, 2.04 reads/min
                === Network ===
                Slowest loop: 41.04ms; fastest: 0.00ms
                Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                HTTP sessions: 1 of 8

                • WiFi -
                  Network state is active
                  WiFi module is connected to access point
                  Failed messages: pending 0, notready 0, noresp 0
                  WiFi firmware version 1.26
                  WiFi MAC address 40:f5:20:0d:6b:49
                  WiFi Vcc 3.37, reset reason Turned on by main processor
                  WiFi flash size 4194304, free heap 23760
                  WiFi IP address 192.168.1.5
                  WiFi signal strength -64dBm, mode 802.11n, reconnections 0, sleep mode modem
                  Clock register 00002002
                  Socket states: 0 0 0 0 0 0 0 0
                  21/3/2022, 14:42:46 Connected to 192.168.1.5
                droftartsundefined 1 Reply Last reply Reply Quote 0
                • droftartsundefined
                  droftarts administrators @paolozampini1973
                  last edited by

                  @paolozampini1973 Great! Now config.g.

                  Ian

                  Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                  paolozampini1973undefined 3 Replies Last reply Reply Quote 0
                  • paolozampini1973undefined
                    paolozampini1973 @droftarts
                    last edited by

                    @droftarts config (17).g

                    1 Reply Last reply Reply Quote 0
                    • paolozampini1973undefined
                      paolozampini1973 @droftarts
                      last edited by paolozampini1973

                      @droftarts I am sending you a photo to make you understand the axes are made up entirely with sfU 1204 and 15 mm linear guides
                      4 ESTRUDE .jpeg

                      droftartsundefined 1 Reply Last reply Reply Quote 0
                      • droftartsundefined
                        droftarts administrators @paolozampini1973
                        last edited by

                        @paolozampini1973 There are a lot of errors in you config.g. Just to start...

                        ; Drives
                        M569 P0 S0 R-1 ;T2.5:2.5:6:5                       ; X    physical drive 0 goes forwards
                        M569 P1 S1 R-1 ;T2.5:2.5:6:5                       ; Y    physical drive 1 goes forwards
                        M569 P2 S1 R1 T5:5:5:5                             ; Z    physical drive 2 goes forwards
                        M569 P3 S0                                         ; E0   physical drive 3 goes forwards
                        M569 P4 S0                                         ; E1   physical drive 4 goes forwards
                        M569 P5 S0                                         ; E2   physical drive 5 goes forwards
                        M569 P6 S0                                         ; E3   physical drive 6 goes forwards
                        M569 P7 S0 R1 T2:2:2:5                         ; E4 X physical drive 7 goes forwards
                        M569 P8 S1 R1 T2:2:2:5                         ; E5 Y physical drive 8 goes forwards
                        M569 P9 S1 R1 T5:5:5:5                             ; E6 Z physical drive 9 goes forwards
                        M584 X7 Y8 Z2:9 E3:4:5:6:7:8:9 S0                  ; set drive mapping
                        

                        Don't set timings for internal TMC drivers. (M569 P2 S1 R1 T5:5:5:5)
                        Your timings for the external drivers are very short.
                        Your M584 should not have the X, Y and Z2 drivers mapped to E. S0 is not needed. Change to:

                        M584 X7 Y8 Z2:9 E3:4:5:6
                        

                        For M350, M92, M566, M203, M201 and M906 commands, make sure E has 4 parameters, eg

                        M350 X16 Y16 Z16 E16:16:16:16 I1
                        

                        Ian

                        Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                        paolozampini1973undefined 1 Reply Last reply Reply Quote 0
                        • paolozampini1973undefined
                          paolozampini1973 @droftarts
                          last edited by

                          @droftarts what idea did you get what you think?

                          1 Reply Last reply Reply Quote 0
                          • paolozampini1973undefined
                            paolozampini1973 @droftarts
                            last edited by paolozampini1973

                            @droftarts Then send me the correct file as you think you are right and I will load it and do the tests you think that for this I lose the steps?

                            at this point what do I do I reassemble the v08 or I leave the V 011 I am willing to do any test Thank you please fill in the config file for me and I will load it exactly as you give it to me and I will let you know

                            droftartsundefined 2 Replies Last reply Reply Quote 0
                            • droftartsundefined
                              droftarts administrators @paolozampini1973
                              last edited by

                              @paolozampini1973 What exact thermistors are you using? You have set the default, which will not be correct, and probably why temperature is incorrect.

                              M308 S0 P"bedtemp" Y"thermistor" T100000 B4138
                              

                              And you need to move Z2 from driver 9 on DueX to driver 0 or 1 on Duet 2. You DueX is being recognised as a DueX2, so probably driver 9 is not working. If it is using an external driver, don't do that; drives on a shared axis need to be identical.

                              Ian

                              Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                              paolozampini1973undefined 2 Replies Last reply Reply Quote 0
                              • paolozampini1973undefined
                                paolozampini1973 @droftarts
                                last edited by

                                @droftarts Yes I set it to DUEX2 because the axes moved when I turned on the electronics Now I can't on DUEX5 Thanks for the dictation problems but for now it is more important to solve the problem of pitch loss and axis movement

                                1 Reply Last reply Reply Quote 0
                                • paolozampini1973undefined
                                  paolozampini1973 @droftarts
                                  last edited by

                                  @droftarts Yes I know that the engines must be identical and are identical

                                  1 Reply Last reply Reply Quote 0
                                  • droftartsundefined
                                    droftarts administrators @paolozampini1973
                                    last edited by

                                    @paolozampini1973 said in DUEX 5 V0.8 TO DUEX 5 V0.11:

                                    @droftarts Then send me the correct file as you think you are right and I will load it and do the tests you think that for this I lose the steps?

                                    at this point what do I do I reassemble the v08 or I leave the V 011 I am willing to do any test Thank you please fill in the config file for me and I will load it exactly as you give it to me and I will let you know

                                    It will have to be later, I have other things I must do.

                                    I'd keep the V011 in for now.

                                    Please show how you have wired the 74HC level shifters. Wiring diagram and/or photo.

                                    Ian

                                    Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                    paolozampini1973undefined 3 Replies Last reply Reply Quote 0
                                    • paolozampini1973undefined
                                      paolozampini1973 @droftarts
                                      last edited by paolozampini1973

                                      @droftarts Listen to the 74hc I have to take it apart Because it gives me more problems it practically skips the steps at the entrance I have to give it three times and 8 and it doesn't skip my steps but if I give it 5 volts it skips my steps it practically gets worse

                                      I did as you told me but the axes move by themselves without command Both X and Y

                                      droftartsundefined 1 Reply Last reply Reply Quote 0
                                      • paolozampini1973undefined
                                        paolozampini1973 @droftarts
                                        last edited by paolozampini1973

                                        @droftarts I would like to leave V 011 but the Y x move without giving it the command so it is useless to talk about other problems there is to solve the first This is the problem Okay I'll wait when you get free I'll publish the config file thanks

                                        21/3/2022, 15:38:13 Error: short-to-ground reported by driver(s) 7 8
                                        Error: over temperature shutdown reported by driver(s) 7 8
                                        21/3/2022, 15:38:08 Error: short-to-ground reported by driver(s) 7 8
                                        Error: over temperature shutdown reported by driver(s) 7 8
                                        21/3/2022, 15:38:04 Error: short-to-ground reported by driver(s) 7 8
                                        Error: over temperature shutdown reported by driver(s) 7 8
                                        21/3/2022, 15:37:59 Error: short-to-ground reported by driver(s) 7 8
                                        Error: over temperature shutdown reported by driver(s) 7 8
                                        21/3/2022, 15:37:55 Error: short-to-ground reported by driver(s) 7 8
                                        Error: over temperature shutdown reported by driver(s) 7 8
                                        21/3/2022, 15:37:50 Error: short-to-ground reported by driver(s) 7 8
                                        Error: over temperature shutdown reported by driver(s) 7 8
                                        21/3/2022, 15:37:49 M122
                                        === Diagnostics ===
                                        RepRapFirmware for Duet 2 WiFi/Ethernet version 3.3 (2021-06-15 21:44:54) running on Duet WiFi 1.02 or later + DueX5
                                        Board ID: 0JD0M-9P6M2-NW4SN-6J1DD-3SJ6K-KAURK
                                        Used output buffers: 3 of 24 (20 max)
                                        === RTOS ===
                                        Static ram: 23876
                                        Dynamic ram: 77448 of which 0 recycled
                                        Never used RAM 13092, free system stack 184 words
                                        Tasks: NETWORK(ready,10.4%,231) HEAT(delaying,0.1%,330) Move(notifyWait,0.1%,319) DUEX(notifyWait,0.0%,24) MAIN(running,86.5%,411) IDLE(ready,3.0%,29), total 100.0%
                                        Owned mutexes:
                                        === Platform ===
                                        Last reset 00:00:25 ago, cause: software
                                        Last software reset at 2022-03-21 15:37, reason: User, GCodes spinning, available RAM 13092, slot 1
                                        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                                        Error status: 0x00
                                        Aux0 errors 0,0,0
                                        Step timer max interval 0
                                        MCU temperature: min 29.3, current 30.0, max 30.3
                                        Supply voltage: min 25.6, current 25.7, max 25.8, under voltage events: 0, over voltage events: 0, power good: yes
                                        Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                                        Driver 0: position 0, standstill, SG min/max not available
                                        Driver 1: position 0, standstill, SG min/max not available
                                        Driver 2: position 0, standstill, SG min/max not available
                                        Driver 3: position 0, standstill, SG min/max not available
                                        Driver 4: position 0, standstill, SG min/max not available
                                        Driver 5: position 0, standstill, SG min/max not available
                                        Driver 6: position 0, standstill, SG min/max not available
                                        Driver 7: position 0, temperature-shutdown! short-to-ground, standstill, SG min/max not available
                                        Driver 8: position 0, temperature-shutdown! short-to-ground, standstill, SG min/max not available
                                        Driver 9: position 0, standstill, SG min/max not available
                                        Driver 10: position 0
                                        Driver 11: position 0
                                        Date/time: 2022-03-21 15:37:49
                                        Cache data hit count 981081507
                                        Slowest loop: 6.48ms; fastest: 0.19ms
                                        I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                                        === Storage ===
                                        Free file entries: 10
                                        SD card 0 detected, interface speed: 20.0MBytes/sec
                                        SD card longest read time 1.0ms, write time 0.0ms, max retries 0
                                        === Move ===
                                        DMs created 83, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                                        === MainDDARing ===
                                        Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                        === AuxDDARing ===
                                        Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                        === Heat ===
                                        Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                        Heater 1 is on, I-accum = 0.0
                                        === GCodes ===
                                        Segments left: 0
                                        Movement lock held by null
                                        HTTP is idle in state(s) 0
                                        Telnet is idle in state(s) 0
                                        File is idle in state(s) 0
                                        USB is idle in state(s) 0
                                        Aux is idle in state(s) 0
                                        Trigger is idle in state(s) 0
                                        Queue is idle in state(s) 0
                                        LCD is idle in state(s) 0
                                        Daemon is idle in state(s) 0
                                        Autopause is idle in state(s) 0
                                        Code queue is empty.
                                        === Filament sensors ===
                                        Extruder 0 sensor: no filament
                                        Extruder 1 sensor: ok
                                        Extruder 2 sensor: no filament
                                        Extruder 3 sensor: ok
                                        === DueX ===
                                        Read count 1, 2.36 reads/min
                                        === Network ===
                                        Slowest loop: 39.88ms; fastest: 0.00ms
                                        Responder states: HTTP(2) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                                        HTTP sessions: 1 of 8

                                        • WiFi -
                                          Network state is active
                                          WiFi module is connected to access point
                                          Failed messages: pending 0, notready 0, noresp 0
                                          WiFi firmware version 1.26
                                          WiFi MAC address 40:f5:20:0d:6b:49
                                          WiFi Vcc 3.37, reset reason Turned on by main processor
                                          WiFi flash size 4194304, free heap 20888
                                          WiFi IP address 192.168.1.5
                                          WiFi signal strength -64dBm, mode 802.11n, reconnections 0, sleep mode modem
                                          Clock register 00002002
                                          Socket states: 0 4 0 0 0 0 0 0
                                          21/3/2022, 15:37:46 Error: short-to-ground reported by driver(s) 7 8
                                          Error: over temperature shutdown reported by driver(s) 7 8
                                          21/3/2022, 15:37:41 Error: short-to-ground reported by driver(s) 7 8
                                          Error: over temperature shutdown reported by driver(s) 7 8
                                          21/3/2022, 15:37:39 Connected to 192.168.1.5
                                          config (18).g
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                                        • droftartsundefined
                                          droftarts administrators @paolozampini1973
                                          last edited by

                                          @paolozampini1973 said in DUEX 5 V0.8 TO DUEX 5 V0.11:

                                          I did as you told me but the axes move by themselves without command Both X and Y

                                          Is that in both DueX2 mode and DueX5 mode?

                                          Ian

                                          Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                          paolozampini1973undefined 4 Replies Last reply Reply Quote 0
                                          • paolozampini1973undefined
                                            paolozampini1973 @droftarts
                                            last edited by

                                            @droftarts As you can see the errors alone are only when AND IN DUEX MODE 5 DRIVER 7+ DRIVER 8 ARE OFF IN DUEX 2 MODE IT DOESN'T GIVE SHORT-CIRCUIT ERRORS SO IT IS NOT NORMAL IN MY MEETING

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