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    randomly reconnect of DWC on Duet2 Ethernet

    Scheduled Pinned Locked Moved Solved
    Duet Hardware and wiring
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    • AlexKidundefined
      AlexKid @Phaedrux
      last edited by

      @Phaedrux
      No this only happens when a message on printer display is shown (see first post).
      I searched the forum and found https://forum.duet3d.com/topic/36277/many-problems-with-3-5-2/18?_=1727095288513
      for me it is the same issue.

      chrishammundefined 1 Reply Last reply Reply Quote 0
      • chrishammundefined
        chrishamm administrators @AlexKid
        last edited by

        @AlexKid Can you please share your config file, too? You might find that increasing the number of AJAX retries in the DWC settings helps.

        Duet software engineer

        AlexKidundefined 1 Reply Last reply Reply Quote 0
        • AlexKidundefined
          AlexKid @chrishamm
          last edited by

          @chrishamm

          G90                                                          ; send absolute coordinates...
          M83                                                          ; ...but relative extruder moves
          M550 P"Muldex"                                               ; set printer name
          
          
          ; Network
          M552 S1 P192.168.200.100                                     ; enable network
          M586 P0 S1                                                   ; enable HTTP
          M586 P1 S1                                                   ; enable FTP
          M586 P2 S0                                                   ; disable Telnet
          
          ; Drives
          M569 P0 S0                                                   ; X physical drive 0 goes backwards
          M569 P1 S1                                                   ; Y right physical drive 1 goes forwards
          M569 P2 S0                                                   ; Y left physical drive 2 goes backwards
          M569 P3 S1                                                   ; U physical drive 3 goes forwords
          M569 P4 S0                                                   ; E1 physical drive 4 goes backwords
          M569 P5 S1                                                   ; Z left physical drive 5 goes backwards
          M569 P6 S1                                                   ; Z center physical drive 6 goes backwards
          M569 P7 S0                                                   ; Z right physical drive 7 goes forwards 
          M569 P8 S1                                                   ; E2 physical drive 8 goes backwords
          
          M584 X0 Y1:2 U3 Z5:6:7 E4:8                                  ; set drive mapping
          
          M350 X16 U16 Y16 Z16 E16:16 I1                               ; configure microstepping with interpolation
          M92 X100.00 U100.00 Y100.00 Z1120 E415.00:415.00             ; set steps per mm (1760nimble)
          M566 X1000.00 U1000.00 Y1000.00 Z100.00 E100.00:300.00       ; set maximum instantaneous speed changes (mm/min)(Nimble 40)
          M203 X12000.00 U12000.00 Y12000.00 Z2000.00 E4200.00:4200.00 ; set maximum speeds (mm/min)
          M201 X15000.00 U15000.00 Y15000.00 Z100.00 E2000.00:2000.00  ; set accelerations (mm/s^2)(500)(Nimble 120)
          M906 X1500 U1500 Y1500 Z1000 E800:800 I30                    ; set motor currents (mA) and motor idle factor in per cent(Nimble 500)
          M84 S30                                                      ; Set idle timeout
          
          ; Axis Limits
          M208 X-21.4:355 Y0:323 U41:419.3 Z0:300                      ; set axis min was (-18 BMG)16.7_X-14.4 Y0 U40 Z0 S1
          ;M208 X344 U413.75 Y334 Z300 S0                 ; set axis max Y WAS 339_X350 U422.7 Y334 Z300 S0(u414.75)
          
          M669 K0 Y1:1:0:1                                             ; select Markforged Kinematics Y to react with X and U
          
          ; Endstops 
          M574 X1 S1 P"xstop"                                          ; X axis active high endstop switch
          M574 Y2 S1 P"ystop+zstop"                                    ; Y Double max active high endstop switch
          M574 U2 S1 P"duex.e2stop"                                    ; U axis active high endstop switch
          M574 Z1 S2                                                   ; Define Z to use Probe. Home to Min.
          
          ; Filament Sensor
          ;M591 D0 P3 C"e0stop" S0 R70:130 L24.8 E3.0 ; Duet3D rotating magnet sensor for extruder drive 0 is connected to E0 endstop input, enabled, sensitivity 24.8mm.rev, 70% to 130% tolerance, 3mm detection length
          ;M591 D1 P3 C"e1stop" S0 R70:130 L24.8 E3.0 ; Duet3D rotating magnet sensor for extruder drive 0 is connected to E0 endstop input, enabled, sensitivity 24.8mm.rev, 70% to 130% tolerance, 3mm detection length
          
          ;M591 D0 ; display filament sensor parameters for extruder drive 0
          ;M591 D1 ; display filament sensor parameters for extruder drive 0
          
          ; Z-Probe
          ;M307 H7 A-1 C-1 D-1                                          ; Disable the 6th Heater to free up PWM channel 5 on the Duex board.
          M671 X-20.6:200:420.6 Y14.3:333.3:14.3 S5                    ; Locations left, center, right 
          M950 S0 C"duex.e6heat"                                       ; create servo pin 0 for BLTouch
          M558 K0 P9 C"^zprobe.in" H5 F120 T6000 R0.005                ; set Z probe type to bltouch and the dive height + speeds (WAS 9000)
          ;M558 P9 C"^zprobe.in H5 F120 T6000 R0.5 A10
          G31 P500 X-29 Y0 Z2.61                                       ; set Z probe trigger value, offset and trigger height(lower number farther away)1.55glass 1.62 Build
          M557 X10:326 Y10:290 S20                                     ; probe from X=10 to 390, Y=10 to 290mm with a mesh spacing of 20mm
          
          ; Heaters
          M308 S0 P"bedtemp" Y"thermistor" T100000 B4725 C7.06e-8      ; configure sensor 0 as thermistor on pin bedtemp
          M950 H0 C"bedheat" T0                                        ; create bed heater output on bedheat and map it to sensor 0
          M143 H0 S120                                                 ; set temperature limit for heater 0 to 120C
          M307 H0 B0 S1.00                                             ; disable bang-bang mode for the bed heater and set PWM limit
          M140 H0                                                      ; map heated bed to heater 0
          M308 S1 P"e0temp" Y"thermistor" T100000 B4725 C7.06e-8       ; configure sensor 1 as thermistor on pin e0temp
          M950 H1 C"e0heat" T1                                         ; create nozzle heater output on e0heat and map it to sensor 1
          M143 H1 S280                                                 ; set temperature limit for heater 1 to 280C
          M307 H1 B0 S1.00                                             ; disable bang-bang mode for heater  and set PWM limit
          M308 S2 P"e1temp" Y"thermistor" T100000 B4725 C7.06e-8       ; configure sensor 2 as thermistor on pin e1temp
          M950 H2 C"e1heat" T2                                         ; create nozzle heater output on e1heat and map it to sensor 2
          M143 H2 S280                                                 ; set temperature limit for heater 2 to 280C
          M307 H2 B0 S1.00                                             ; disable bang-bang mode for heater  and set PWM limit
          
          ; Fans
          M950 F0 C"fan0" Q500                                         ; create fan 0 on pin fan0 and set its frequency
          M106 P0 S0 H-1                                               ; set fan 0 value. Thermostatic control is turned off
          M950 F1 C"fan1" Q500                                         ; create fan 1 on pin fan1 and set its frequency
          M106 P1 S1 H1 T45                                            ; set fan 1 value. Thermostatic control is turned on
          M950 F2 C"fan2" Q500                                         ; create fan 2 on pin fan2 and set its frequency
          M106 P2 S0 H-1                                               ; set fan 2 value. Thermostatic control is turned off
          M950 F3 C"duex.fan8" Q500                                    ; create fan 3 on pin duex.fan8 and set its frequency
          M106 P3 S1 H2 T45                                            ; set fan 3 value. Thermostatic control is turned on
          
          ; LEDs
          M950 F4 C"duex.fan6"                                         ;Q500                       ; create LED 4 on pin duex.fan6 and set its frequency
          M106 P4 S0 H-1                                               ; set LED 4 value. Thermostatic control is turned OFF
          M950 F5 C"duex.fan7"                                         ;Q500                       ; create LED 5 on pin duex.fan7 and set its frequency
          M106 P5 S0 H-1                                               ; set LED 5 value. Thermostatic control is turned OFF
          
          ; Tools
          M563 P0 D0 H1 F0 S"Left"                                     ; define tool 0 Left 
          G10 P0 X0 Y0 Z0                                              ; set tool 0 axis offsets y was .45
          G10 P0 R0 S0                                                 ; set initial tool 0 active and standby temperatures to 0C
          M207 S10.0 F400                                              ; set Firmware Retraction
          
          M563 P1 D1 H2 X3 F2 S"Right"                                 ; define tool 1 Right
          G10 P1 X0 Y0 Z0                                              ; set tool 1 axis offsets (.5BMG) (-1.45)
          G10 P1 R0 S0                                                 ; set initial tool 1 active and standby temperatures to 0C
          M207 S10.0 F400                                              ; set Firmware Retraction
          
          M563 P2 D0:1 H1:2 X0:3 F0:2 S"Copy"                          ; define tool 2 Copy
          G10 P2 X95 Y0 U-95 S0 R0                                     ; set tool 2 axis offsets (WAS 105)
          M567 P2 E1:1         
          M568 P2 S1                                                   ; turn on mixing for tool 2           ; set mix ratio 100% on both extruders
          
          M501                                                         ; Record
          
          M575 P1 S1 B57600                                            ;Panel due
          
          chrishammundefined 1 Reply Last reply Reply Quote 0
          • chrishammundefined
            chrishamm administrators @AlexKid
            last edited by chrishamm

            @AlexKid Thanks for your config file, I could reproduce it here and I believe I found DWC settings that prevent this problem. Can you please try to change the following values on the Settings -> Machine-Specific page and check if DWC remains stable then?

            • Communication -> Maximum number of AJAX retries: 3
            • Communication -> Time to wait between AJAX retries (in ms): 250

            If that fixes it for you, too, I will change the default DWC settings in the next version.

            PS: You could also try to increase the PanelDue BAUD rate from 57600 to 115200. That way, data can be sent to PanelDue quicker which could result in better network performance, too.

            Duet software engineer

            AlexKidundefined 1 Reply Last reply Reply Quote 2
            • AlexKidundefined
              AlexKid @chrishamm
              last edited by

              @chrishamm
              unfortunately this does not help.
              lots of reconnects with active DWC and performing homing of all axis via Panel Due
              also increased Baudrate to 115200

              AlexKidundefined 1 Reply Last reply Reply Quote 0
              • AlexKidundefined
                AlexKid @AlexKid
                last edited by

                @chrishamm I'm running RRF 3.5.4 now for several weeks. The issue is no longer present. I also updated PanelDue today to 3.5.1 and it still seams to be stable.
                I would suggeset to close this topic.

                T3P3Tonyundefined 1 Reply Last reply Reply Quote 2
                • jay_s_ukundefined jay_s_uk marked this topic as a question
                • jay_s_ukundefined jay_s_uk has marked this topic as solved
                • T3P3Tonyundefined
                  T3P3Tony administrators @AlexKid
                  last edited by

                  @AlexKid Please would you test this with 3.6beta3 RRF and 3.5.1 Paneldue firmware:

                  https://forum.duet3d.com/topic/37289/software-version-3-6-0-beta-3-now-available
                  https://forum.duet3d.com/topic/37179/paneldue-firmware-3-5-1-released

                  to confirm its now fixed with your original settings.

                  www.duet3d.com

                  AlexKidundefined 1 Reply Last reply Reply Quote 0
                  • AlexKidundefined
                    AlexKid @T3P3Tony
                    last edited by

                    @T3P3Tony
                    I will install the beta and provide feedback

                    1 Reply Last reply Reply Quote 2
                    • AlexKidundefined
                      AlexKid
                      last edited by AlexKid

                      Hi @T3P3Tony,

                      installed 3.6.0 Beta 3.
                      I can no longer access the webinterface.
                      Paneldue is very slow
                      It was not a good idea to install the beta version 😖

                      jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                      • jay_s_ukundefined
                        jay_s_uk @AlexKid
                        last edited by

                        @AlexKid theres a bug fix version already for the duet 2 ethernet. see here https://forum.duet3d.com/post/349876

                        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                        1 Reply Last reply Reply Quote 0
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