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    Help: Temp Sensors and Homing Issues

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    • 94118undefined
      94118
      last edited by

      Request an update for recent message about the paneldue

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      • 94118undefined
        94118
        last edited by

        Duet 2 wifi seems to good with USB but not the paneldue

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        • Phaedruxundefined
          Phaedrux Moderator
          last edited by

          Please see the post from DC42 above. https://forum.duet3d.com/post/134957

          You need YAT connected via USB so that we can see if there is communication between the paneldue and the duet.

          Z-Bot CoreXY Build | Thingiverse Profile

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          • 94118undefined
            94118
            last edited by

            Direct from YAT: with Duet 2 plugged in to USB talking to Paneldue

            Debugging enabled for modules: GCodes(3)<LF>Debugging disabled for modules: Platform(0) Network(1) Webserver(2) Move(4) Heat(5) DDA(6) Roland(7) Scanner(8) PrintMonitor(9) Storage(10) PortControl(11) DuetExpansion(12) FilamentSensors(13) WiFi(14) Display(15) LinuxInterface(16)<LF>

            NO (aux: M408)

            What next

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            • Phaedruxundefined
              Phaedrux Moderator @dc42
              last edited by

              dc42 said in Help: Temp Sensors and Homing Issues:

              If you are using the ribbon cable, make sure it is plugged into the CONN_SD socket on the Duet. Not CONN_LCD.

              In your first picture it shows the PanelDue ribbon cable plugged into the wrong port. Are you still connected that way? Have you tried the 4 wire cabling option?

              https://duet3d.dozuki.com/Wiki/Duet_Wiring_Diagrams

              Z-Bot CoreXY Build | Thingiverse Profile

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              • 94118undefined
                94118
                last edited by

                disconnected ribbon cable now it shows Idle And Temps

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                • Phaedruxundefined
                  Phaedrux Moderator
                  last edited by

                  So it's working now? Your responses are so short it's hard to know what's actually going on, which makes it very challenging to help you out.

                  Z-Bot CoreXY Build | Thingiverse Profile

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                  • 94118undefined
                    94118
                    last edited by

                    I have and got it working by removing the ribbon cable. Now i think its my endstops conflicting with homing controls and commands (https://drive.google.com/open?id=1DxrsV36-5PN991DjbJJKdIKGP0n85crk) picture included status of endstops state Yes

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                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by Phaedrux

                      If the endstop state says that it' triggered when it's not, then it's likely been defined incorrectly for the switch type.

                      I don't know what type of switches you have, or how the endstops have been defined in config.g.

                      https://duet3d.dozuki.com/Wiki/Gcode#Section_M574_Set_endstop_configuration

                      It's likely a case of needing to change an S0 to S1 or vice versa.

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • 94118undefined
                        94118
                        last edited by

                        Mechanical ENdstops

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                        • 94118undefined
                          94118
                          last edited by

                          Homing still an issue Please review my config.g File i will Send config.g

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                          • Phaedruxundefined
                            Phaedrux Moderator @94118
                            last edited by Phaedrux

                            @94118 said in Help: Temp Sensors and Homing Issues:

                            Mechanical ENdstops

                            Yes, but what kind of switch is it? Normally open, or normally closed? Do you have a picture of the switch?

                            ; Endstops
                            M574 X1 S1 P"xstop"                            ; configure active-low endstop for low end on X via pin xstop
                            M574 Y2 S1 P"ystop"                            ; configure active-low endstop for high end on Y via pin ystop
                            M574 Z1 S1 P"zstop"                            ; configure active-low endstop for low end on Z via pin zstop
                            

                            As I mentioned above, you may need to change the S1 to S0.

                            With RRF3 you need to use a ! to invert the signal, so try

                            ; Endstops
                            M574 X1 S1 P"!xstop"                            ; configure active-low endstop for low end on X via pin xstop
                            M574 Y2 S1 P"!ystop"                            ; configure active-low endstop for high end on Y via pin ystop
                            M574 Z1 S1 P"!zstop"                            ; configure active-low endstop for low end on Z via pin zstop
                            

                            Z-Bot CoreXY Build | Thingiverse Profile

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                            • 94118undefined
                              94118
                              last edited by

                              Just replaced Hotend heater and Thermistor did Heater auto tune and it was successful with New 24v 40W Heater Cart. and an NTC 3950 Stud Thermistor

                              ![alt text](25bd99b3-f082-4f96-bf4f-d83736da1234-image.png image url)

                              Features:
                              Using 22AWG cable, the copper inside is very thick, it is resistant to current 2A, voltage 300V.
                              The nonconductor has a wide range of temperatures, up to 80 centigrade.
                              It is not easy to be snapped and convenient to be plugged in and unplugged.
                              For convenience, the plug on the other side is integrated , you can use the plug directly.

                              Connection description:

                              1. Bed wire connect VCC (+ of ramps)
                              2. Black wire connect GND (- of ramps)
                              3. Green wire connect SIGNAL (s of ramps)

                              One set includes:

                              1. 1x endstop switch
                              2. 1x 3-pin 27.5inch cable

                              What is in the package:
                              2 set endstop switches for RAMPS 1.4

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                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by

                                Yes those switches would likely need to be inverted. See my post above.

                                What firmware version are you running exactly? Send M115 and post the response.

                                Z-Bot CoreXY Build | Thingiverse Profile

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                                • 94118undefined
                                  94118
                                  last edited by

                                  console (2).txt Results posted Fixed my Z and Changed my endstops to inverted with the Exclamation Fix Thanks

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                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    M500: Warning: No M501 command was executed in config.g

                                    Don't forget to add M501 to the end of config.g or your tuned values won't be loaded at boot.

                                    Z-Bot CoreXY Build | Thingiverse Profile

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                                    • 94118undefined
                                      94118
                                      last edited by

                                      Ouickie: Is their a way to disable and enable motors so that i may level my bed with my Boro glass.

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                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        M84

                                        https://duet3d.dozuki.com/Wiki/Gcode#Section_M84_Stop_idle_hold

                                        Z-Bot CoreXY Build | Thingiverse Profile

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                                        • 94118undefined
                                          94118
                                          last edited by

                                          When homing Z at the end of run Command it is hitting my nozzle causing my bed to tilt a few degrees

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                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            Post your homing files.

                                            Is it using a probe, or an endstop?

                                            If the nozzle is hitting the bed before the endstop is triggered you'll need to move the endstop so that it gets triggered first. If it's hitting the endstop but not stopping you should test the endstop switch to see if it's triggering at all when pressed.

                                            Z-Bot CoreXY Build | Thingiverse Profile

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