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    Duet 3 Disconnects from SBC

    Scheduled Pinned Locked Moved Unsolved
    Firmware installation
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    • mrenz999undefined
      mrenz999 @mrenz999
      last edited by

      @Phaedrux
      Started the print again with same results. Then ran M122
      again
      9/3/2020, 9:23:58 PM Leadscrew adjustments made: 0.273 0.190 0.300, points used 3, (mean, deviation) before (0.254, 0.047) after (0.000, 0.000)
      9/3/2020, 9:23:46 PM m122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.01-RC9 running on Duet 3 MB6HC v1.01 or later
      Board ID: 08DJM-956L2-G43S8-6J1FA-3SJ6P-1B06GUsed output buffers: 1 of 40 (13 max)
      === RTOS ===
      Static ram: 154572
      Dynamic ram: 162708 of which 20 recycled
      Exception stack ram used: 424
      Never used ram: 75492
      Tasks: NETWORK(ready,2076) HEAT(blocked,1184) CanReceiv(suspended,3824) CanSender(suspended,1432) CanClock(blocked,1432) TMC(blocked,80) MAIN(running,4436) IDLE(ready,80)
      Owned mutexes:
      === Platform ===
      Last reset 00:24:07 ago, cause: software
      Last software reset at 2020-09-04 04:59, reason: User, spinning module LinuxInterface, available RAM 75604 bytes (slot 1)
      Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task 0x4e49414d
      Error status: 0
      Free file entries: 10
      SD card 0 not detected, interface speed: 37.5MBytes/sec
      SD card longest block write time: 0.0ms, max retries 0
      MCU temperature: min 42.3, current 42.8, max 42.9
      Supply voltage: min 23.0, current 23.7, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0
      Driver 0: ok, reads 62668, writes 3 timeouts 0, SG min/max 0/215
      Driver 1: ok, reads 62668, writes 3 timeouts 0, SG min/max 0/142
      Driver 2: standstill, reads 62668, writes 3 timeouts 0, SG min/max 0/88
      Driver 3: standstill, reads 62669, writes 3 timeouts 0, SG min/max 0/90
      Driver 4: standstill, reads 62668, writes 3 timeouts 0, SG min/max 0/93
      Driver 5: standstill, reads 62672, writes 0 timeouts 0, SG min/max not available
      Date/time: 2020-09-04 05:23:50
      Slowest loop: 4.72ms; fastest: 0.14ms
      === Move ===
      Hiccups: 0(0), FreeDm: 373, MinFreeDm: 373, MaxWait: 1426733ms
      Bed compensation in use: none, comp offset 0.000
      === MainDDARing ===
      Scheduled moves: 15, completed moves: 14, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: 3
      === AuxDDARing ===
      Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
      === Heat ===
      Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
      Heater 0 is on, I-accum = 0.4
      Heater 1 is on, I-accum = 0.6
      === GCodes ===
      Segments left: 0
      Movement lock held by File
      HTTP* is ready with "M122" in state(s) 0
      Telnet is idle in state(s) 0
      File* is idle in state(s) 40 0 0, running macro
      USB is idle in state(s) 0
      Aux is assembling a command in state(s) 0
      Trigger* is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon* is idle in state(s) 0
      Autopause is idle in state(s) 0
      Code queue is empty.
      === Network ===
      Slowest loop: 1.92ms; fastest: 0.01ms
      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
      HTTP sessions: 0 of 8

      • Ethernet -
        State: disabled
        Error counts: 0 0 0 0 0
        Socket states: 0 0 0 0 0 0 0 0
        === CAN ===
        Messages sent 1644, longest wait 0ms for type 0
        === Linux interface ===
        State: 0, failed transfers: 0
        Last transfer: 18ms ago
        RX/TX seq numbers: 13844/13846
        SPI underruns 0, overruns 0
        Number of disconnects: 1
        Buffer RX/TX: 0/0-0
        === Duet Control Server ===
        Duet Control Server v3.1.1
        File:
        Finishing macro deployprobe.g, started by G30 P1 X20 Y365 Z-99999 ; probe near an adjusting screw

      Next stack level
      Executing macro bed.g, started by G32 ; bed compensation
      Suspended code: G30 P2 X430 Y240 Z-99999 S3 ; probe near an adjusting screw and calibrate 3 motors
      Suspended code: ;G29
      Suspended code: ;M402 ; retract probe
      Next stack level
      Executing macro start.g, started by system
      Suspended code: G28 ; home XYZ
      Suspended code: ;G29 S1 ; load heightmap
      Suspended code: ;M400
      Suspended code: ;G10 P0 R80 S235 ; Set extruder to 180 and release
      Suspended code: ;M98 P"0:/sys/ZSpeedsPrint.g" ; Load Z speeds for printing
      Suspended code: ;M98 P"0:/sys/CurrentsPrint.g" ; Load print motor currents
      Suspended code: ; Slicer Start Gcode begins.
      Next stack level
      Suspended code: T0
      Suspended code: M190 S70
      Suspended code: M104 S245
      Suspended code: M109 S245
      Suspended code: M82 ;absolute extrusion mode
      Suspended code: M83 ;relative extrusion mode
      Suspended code: G1 F1500 E-6.5
      Suspended code: ;LAYER_COUNT:51
      Suspended code: ;LAYER:0
      Suspended code: M107
      Suspended code: G0 F3600 X86.205 Y144.27 Z0.3
      Suspended code: ;TYPE:SKIRT
      Suspended code: G1 F1500 E6.5
      Suspended code: G1 F1800 X86.965 Y143.845 E0.03139
      Suspended code: G1 X88.334 Y143.116 E0.05591
      Suspended code: G1 X88.714 Y142.922 E0.01538
      Suspended code: G1 X89.867 Y142.356 E0.0463
      Suspended code: G1 X90.079 Y142.272 E0.00822
      Suspended code: G1 X91.185 Y141.751 E0.04407
      Suspended code: G1 X91.433 Y141.647 E0.00969
      Suspended code: G1 X92.556 Y141.229 E0.04319
      Suspended code: G1 X93.411 Y140.916 E0.03282
      Suspended code: G1 X94.083 Y140.698 E0.02547
      Suspended code: G1 X94.905 Y140.451 E0.03094
      Suspended code: G1 X95.523 Y140.28 E0.02311
      Suspended code: G1 X96.059 Y140.127 E0.02009
      Suspended code: G1 X96.74 Y139.945 E0.02541
      Suspended code: G1 X97.539 Y139.75 E0.02965
      Suspended code: G1 X97.766 Y139.701 E0.00837
      Suspended code: G1 X98.593 Y139.536 E0.0304
      Suspended code: G1 X98.654 Y139.529 E0.00221
      Suspended code: G1 X99.964 Y139.278 E0.04808
      Trigger:
      Finishing macro config.g, started by system
      Next stack level
      Code buffer space: 4096
      Configured SPI speed: 8000000 Hz
      Full transfers per second: 32.69
      File /opt/dsf/sd/gcodes/petgtriple-moon.gcode is selected, processing
      9/3/2020, 9:23:36 PM Connection to Duet established
      9/3/2020, 9:23:36 PM Warning: Lost connection to Duet (Board is not available (no data response))

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      • mrenz999undefined
        mrenz999
        last edited by

        9/3/2020, 10:36:20 PM m122
        === Diagnostics ===
        RepRapFirmware for Duet 3 MB6HC version 3.01-RC9 running on Duet 3 MB6HC v1.01 or later
        Board ID: 08DJM-956L2-G43S8-6J1FA-3SJ6P-1B06GUsed output buffers: 1 of 40 (10 max)
        === RTOS ===
        Static ram: 154572
        Dynamic ram: 162500 of which 20 recycled
        Exception stack ram used: 528
        Never used ram: 75596
        Tasks: NETWORK(ready,2076) HEAT(blocked,1184) CanReceiv(suspended,3824) CanSender(suspended,1432) CanClock(blocked,1432) TMC(blocked,80) MAIN(running,2808) IDLE(ready,80)
        Owned mutexes:
        === Platform ===
        Last reset 00:57:28 ago, cause: software
        Last software reset at 2020-09-04 05:38, reason: User, spinning module LinuxInterface, available RAM 75388 bytes (slot 2)
        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task 0x4e49414d
        Error status: 0
        Free file entries: 10
        SD card 0 not detected, interface speed: 37.5MBytes/sec
        SD card longest block write time: 0.0ms, max retries 0
        MCU temperature: min 43.7, current 43.8, max 46.6
        Supply voltage: min 23.1, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
        12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0
        Driver 0: standstill, reads 55532, writes 19 timeouts 0, SG min/max 0/216
        Driver 1: standstill, reads 55533, writes 19 timeouts 0, SG min/max 0/182
        Driver 2: standstill, reads 55533, writes 19 timeouts 0, SG min/max 0/117
        Driver 3: standstill, reads 55533, writes 19 timeouts 0, SG min/max 0/867
        Driver 4: standstill, reads 55534, writes 19 timeouts 0, SG min/max 0/107
        Driver 5: standstill, reads 55534, writes 19 timeouts 0, SG min/max 0/202
        Date/time: 2020-09-04 06:36:24
        Slowest loop: 4.66ms; fastest: 0.14ms
        === Move ===
        Hiccups: 0(0), FreeDm: 375, MinFreeDm: 330, MaxWait: 29338ms
        Bed compensation in use: none, comp offset 0.000
        === MainDDARing ===
        Scheduled moves: 0, completed moves: 3, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
        === AuxDDARing ===
        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
        === Heat ===
        Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
        === GCodes ===
        Segments left: 0
        Movement lock held by null
        HTTP* is ready with "M122" in state(s) 0
        Telnet is idle in state(s) 0
        File* is idle in state(s) 0
        USB is idle in state(s) 0
        Aux is assembling a command in state(s) 0
        Trigger* is idle in state(s) 0
        Queue* is idle in state(s) 0
        LCD is idle in state(s) 0
        SBC is idle in state(s) 0
        Daemon* is idle in state(s) 0
        Autopause is idle in state(s) 0
        Code queue is empty.
        === Network ===
        Slowest loop: 1.92ms; fastest: 0.01ms
        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
        HTTP sessions: 0 of 8

        • Ethernet -
          State: disabled
          Error counts: 0 0 0 0 0
          Socket states: 0 0 0 0 0 0 0 0
          === CAN ===
          Messages sent 13776, longest wait 0ms for type 0
          === Linux interface ===
          State: 0, failed transfers: 96
          Last transfer: 19ms ago
          RX/TX seq numbers: 46307/46300
          SPI underruns 40, overruns 40
          Number of disconnects: 1
          Buffer RX/TX: 0/0-0
          === Duet Control Server ===
          Duet Control Server v3.1.1
          Code buffer space: 4096
          Configured SPI speed: 8000000 Hz
          Full transfers per second: 32.49
        1 Reply Last reply Reply Quote 0
        • jay_s_ukundefined
          jay_s_uk
          last edited by

          I would first suggest updating your firmware. You're still running 3.01-RC9

          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            You're still on an old release candidate firmware. Please update to 3.1.1 your issue may already be solved.

            Z-Bot CoreXY Build | Thingiverse Profile

            mrenz999undefined 1 Reply Last reply Reply Quote 0
            • mrenz999undefined
              mrenz999 @Phaedrux
              last edited by

              @Phaedrux So it should just require a sudo apt-get update ?

              1 Reply Last reply Reply Quote 0
              • A Former User?
                A Former User
                last edited by

                as of 3.0.0 apt should just-work(tm) for upgrades (but expansion- or tool-boards needs to be upgraded by M997 until the scripts from the reprapfirmware package takes care of that)

                mrenz999undefined 1 Reply Last reply Reply Quote 0
                • mrenz999undefined
                  mrenz999 @A Former User
                  last edited by

                  @bearer Hmmm. Well it updated the Pi but not the Duet 3. Is there something else I should be doing ?

                  A Former User? 1 Reply Last reply Reply Quote 0
                  • mrenz999undefined
                    mrenz999
                    last edited by

                    Is there something else to do other than that sudo apt-get update and upgrade that needs to be done?

                    1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Some of the older firmware didn't update properly with the normal apr-get update method. In these cases you'd need to update the board firmware separately. Once you're at 3.1.1 it should "just work" going forward.

                      You should be able to update the board firmware by uploading the firmware zip file to the /sys folder in DWC just as you would normally with any other Duet.

                      https://github.com/Duet3D/RepRapFirmware/releases/download/3.1.1/Duet2and3Firmware-3.1.1.zip

                      If that doesn't work, then you have the option of using Bossa to flash the firmware to the board over USB with a PC.

                      https://duet3d.dozuki.com/Wiki/Getting_Started_With_Duet_3#Section_Updating_Duet_3_main_board_firmware

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • A Former User?
                        A Former User @mrenz999
                        last edited by A Former User

                        @mrenz999 said in Duet 3 Disconnects from SBC:

                        @bearer Hmmm. Well it updated the Pi but not the Duet 3. Is there something else I should be doing ?

                        not really, but it'd be helpfull to see the output from apt as it would allude to why the firmware failed.

                        should be as simple as doing echo S997 | sudo /opt/dsf/bin/CodeConsole from ssh if the duet is communicating with the pi (if its not then thats why the upgrade failed, but afaik not been an issue after 3.0)

                        mrenz999undefined 1 Reply Last reply Reply Quote 0
                        • mrenz999undefined
                          mrenz999 @A Former User
                          last edited by mrenz999

                          @bearer pi@duet3:~ $ echo S997 | sudo /opt/dsf/bin/CodeConsole
                          Unhandled exception. System.Net.Internals.SocketExceptionFactory+ExtendedSocketException (99): Cannot assign requested address /var/run/dsf/dcs.sock
                          at System.Net.Sockets.Socket.DoConnect(EndPoint endPointSnapshot, SocketAddress socketAddress)
                          at System.Net.Sockets.Socket.Connect(EndPoint remoteEP)
                          at DuetAPIClient.BaseConnection.Connect(ClientInitMessage initMessage, String socketPath, CancellationToken cancellationToken) in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetAPIClient/BaseConnection.cs:line 98
                          at CodeConsole.Program.Main(String[] args) in /home/christian/Duet3D/DuetSoftwareFramework/src/CodeConsole/Program.cs:line 44
                          at CodeConsole.Program.<Main>(String[] args)
                          Aborted
                          This is the result of it.

                          A Former User? 1 Reply Last reply Reply Quote 0
                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            Did you try uploading the Zip in DWC?

                            Z-Bot CoreXY Build | Thingiverse Profile

                            mrenz999undefined 2 Replies Last reply Reply Quote 0
                            • mrenz999undefined
                              mrenz999 @Phaedrux
                              last edited by mrenz999

                              @Phaedrux I did download it. However, I am unable to connect to DWC now for some reason. It says Failed to connect to Duet3.local DCS not started. I hard power reset both, unplugged and left off for a few mins and replugged them in. Is there a way to do it through the pi ?

                              1 Reply Last reply Reply Quote 0
                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by

                                If the pi is connected to the duet via usb you can use bossa to flash the duet. That may be a better option if it's too much hassle getting everything disconnected to get it to a PC to flash. But if you have a laptop or PC nearby that might be easier if you're not comfortable with the pi environment.

                                Z-Bot CoreXY Build | Thingiverse Profile

                                mrenz999undefined 2 Replies Last reply Reply Quote 0
                                • mrenz999undefined
                                  mrenz999 @Phaedrux
                                  last edited by

                                  @Phaedrux I have a laptop. Do I need to disconnect everything from the board or just plug in and do it ?

                                  1 Reply Last reply Reply Quote 0
                                  • mrenz999undefined
                                    mrenz999 @Phaedrux
                                    last edited by

                                    @Phaedrux Verify failed
                                    Page errors: 1115
                                    Byte errors: 564485
                                    This was the response when I used BOSSA through the pi

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                                    • A Former User?
                                      A Former User @mrenz999
                                      last edited by

                                      @mrenz999 said in Duet 3 Disconnects from SBC:

                                      Unhandled exception. System.Net.Internals.SocketExceptionFactory+ExtendedSocketException (99): Cannot assign requested address /var/run/dsf/dcs.sock
                                      ...
                                      Aborted
                                      This is the result of it.

                                      so that could be why it didn't upgrade with apt, as pi and duet aren't communicating over the spi link and that also prevent duet web control working.

                                      seeing as bossac failed, maybe try different usb cable or from a computer instead (or disconnect any power hungry peripherals to eliminate usb power supply issues)

                                      1 Reply Last reply Reply Quote 0
                                      • mrenz999undefined
                                        mrenz999 @Phaedrux
                                        last edited by

                                        @Phaedrux Ok I got it updated using BOSSA through the pi. 2 failed prints later.

                                        m122
                                        === Diagnostics ===
                                        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                        Board ID: 08DJM-956L2-G43S8-6J1FA-3SJ6P-1B06G
                                        Used output buffers: 1 of 40 (13 max)
                                        === RTOS ===
                                        Static ram: 154604
                                        Dynamic ram: 163364 of which 20 recycled
                                        Exception stack ram used: 536
                                        Never used ram: 74692
                                        Tasks: NETWORK(ready,1972) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1420) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,2868) IDLE(ready,76)
                                        Owned mutexes:
                                        === Platform ===
                                        Last reset 10:16:20 ago, cause: software
                                        Last software reset at 2020-09-05 05:11, reason: User, spinning module LinuxInterface, available RAM 75124 bytes (slot 3)
                                        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                        Error status: 0
                                        MCU temperature: min 40.5, current 40.8, max 43.9
                                        Supply voltage: min 23.9, current 24.1, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
                                        12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0
                                        Driver 0: standstill, reads 56301, writes 8 timeouts 0, SG min/max 0/591
                                        Driver 1: standstill, reads 56300, writes 8 timeouts 0, SG min/max 0/646
                                        Driver 2: standstill, reads 56301, writes 8 timeouts 0, SG min/max 0/99
                                        Driver 3: standstill, reads 56300, writes 8 timeouts 0, SG min/max 0/97
                                        Driver 4: standstill, reads 56300, writes 8 timeouts 0, SG min/max 0/78
                                        Driver 5: standstill, reads 56304, writes 4 timeouts 0, SG min/max 0/847
                                        Date/time: 2020-09-05 15:27:29
                                        Slowest loop: 5.84ms; fastest: 0.15ms
                                        === Storage ===
                                        Free file entries: 10
                                        SD card 0 not detected, interface speed: 37.5MBytes/sec
                                        SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                        === Move ===
                                        Hiccups: 0(0), FreeDm: 375, MinFreeDm: 292, MaxWait: 9557402ms
                                        Bed compensation in use: none, comp offset 0.000
                                        === MainDDARing ===
                                        Scheduled moves: 41108, completed moves: 41108, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                                        === AuxDDARing ===
                                        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                                        === Heat ===
                                        Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                        === GCodes ===
                                        Segments left: 0
                                        Movement lock held by null
                                        HTTP* is ready with "M122" in state(s) 0
                                        Telnet is idle in state(s) 0
                                        File* is idle in state(s) 0
                                        USB is idle in state(s) 0
                                        Aux is assembling a command in state(s) 0
                                        Trigger* is idle in state(s) 0
                                        Queue* is idle in state(s) 0
                                        LCD is idle in state(s) 0
                                        SBC is idle in state(s) 0
                                        Daemon* is idle in state(s) 0 0, running macro
                                        Aux2 is idle in state(s) 0
                                        Autopause is idle in state(s) 0
                                        Code queue is empty.
                                        === Network ===
                                        Slowest loop: 2.13ms; fastest: 0.01ms
                                        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                                        HTTP sessions: 0 of 8

                                        • Ethernet -
                                          State: disabled
                                          Error counts: 0 0 0 0 0
                                          Socket states: 0 0 0 0 0 0 0 0
                                          === CAN ===
                                          Messages sent 91415, longest wait 0ms for type 0
                                          === Linux interface ===
                                          State: 0, failed transfers: 309
                                          Last transfer: 16ms ago
                                          RX/TX seq numbers: 20337/20313
                                          SPI underruns 118, overruns 118
                                          Number of disconnects: 0
                                          Buffer RX/TX: 0/0-0
                                          === Duet Control Server ===
                                          Duet Control Server v3.1.1
                                          Code buffer space: 4096
                                          Configured SPI speed: 8000000 Hz
                                          Full transfers per second: 32.45
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                                        • Phaedruxundefined
                                          Phaedrux Moderator
                                          last edited by

                                          Does it fail on every print now?

                                          Can you share the gcode file you're printing?

                                          Can you setup debugging info?

                                          https://duet3d.dozuki.com/Wiki/Getting_Started_With_Duet_3#Section_Monitoring_optional

                                          Z-Bot CoreXY Build | Thingiverse Profile

                                          mrenz999undefined 3 Replies Last reply Reply Quote 0
                                          • mrenz999undefined
                                            mrenz999 @Phaedrux
                                            last edited by

                                            @Phaedrux Yes every print. I have tried mulitple prints. I will setup debugging and share the Gcode this evening when I get back from work. Every print it just stops about 10% or so in. It has rebooted but on the status page it says it has completed the print.

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