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    Duet 3 SBC DCS has stopped

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • dhusoloundefined
      dhusolo
      last edited by

      More of a status update: I've started the same print again but I don't load any filament. I didn't want to waste the filament if it's going to cancel on me again.

      However I can now hear some strange jerky movements. I have a coreXY so it's hard to narrow down what stepper it's coming from especially since there's no filament going through it.

      Phaedruxundefined 1 Reply Last reply Reply Quote 0
      • oliofundefined
        oliof
        last edited by

        I think my recent post about issues with 3.2b3 are very similar to this issue.

        <>RatRig V-Minion Fly Super5Pro RRF<> V-Core 3.1 IDEX k*****r <> RatRig V-Minion SKR 2 Marlin<>

        1 Reply Last reply Reply Quote 2
        • Phaedruxundefined
          Phaedrux Moderator @dhusolo
          last edited by

          @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

          Z-Bot CoreXY Build | Thingiverse Profile

          A Former User? dhusoloundefined 2 Replies Last reply Reply Quote 0
          • A Former User?
            A Former User @Phaedrux
            last edited by

            @Phaedrux said in Duet 3 SBC DCS has stopped:

            @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

            Oh the irony.....

            Phaedruxundefined 1 Reply Last reply Reply Quote 0
            • dhusoloundefined
              dhusolo @Phaedrux
              last edited by

              @Phaedrux I'm going to attempt to go back to RRF 3.1.1 with RPI since issues with connecting are resolved. Doesn't make a lot of sense that it was working previously for 3 months without any issue.

              If that brings the same symptoms I'll run it in standalone until RRF 3.2 is stable. At least I know the board isn't bad

              1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator @A Former User
                last edited by

                @CaLviNx It's not irony because no one ever disagreed with you.

                Z-Bot CoreXY Build | Thingiverse Profile

                A Former User? 1 Reply Last reply Reply Quote 0
                • dhusoloundefined
                  dhusolo
                  last edited by

                  Can confirm going back to 3.1.1. the bug is still present. No idea why it appeared months after the original upload and weeks after any update to my config.

                  I did notice under Linux interface it shows a failed transfer, some bit loss and a SPI underrun

                  	M122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                  Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                  Used output buffers: 1 of 40 (12 max)
                  === RTOS ===
                  Static ram: 154604
                  Dynamic ram: 163392 of which 140 recycled
                  Exception stack ram used: 584
                  Never used ram: 74496
                  Tasks: NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1384) CanClock(blocked,1436) TMC(blocked,60) MAIN(running,2672) IDLE(ready,76)
                  Owned mutexes:
                  === Platform ===
                  Last reset 03:06:26 ago, cause: power up
                  Last software reset at 2020-11-09 16:57, reason: User, spinning module LinuxInterface, available RAM 77008 bytes (slot 1)
                  Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                  Error status: 0
                  MCU temperature: min 34.4, current 37.6, max 39.2
                  Supply voltage: min 24.2, current 24.5, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
                  Driver 0: standstill, reads 55804, writes 22 timeouts 0, SG min/max 0/193
                  Driver 1: standstill, reads 55797, writes 30 timeouts 0, SG min/max 0/1023
                  Driver 2: standstill, reads 55797, writes 30 timeouts 0, SG min/max 0/1023
                  Driver 3: standstill, reads 55794, writes 34 timeouts 0, SG min/max 0/1023
                  Driver 4: standstill, reads 55794, writes 34 timeouts 0, SG min/max 0/1023
                  Driver 5: standstill, reads 55795, writes 34 timeouts 0, SG min/max 0/1023
                  Date/time: 2020-11-09 20:05:07
                  Slowest loop: 9.46ms; fastest: 0.14ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  Hiccups: 0(0), FreeDm: 375, MinFreeDm: 317, MaxWait: 669637ms
                  Bed compensation in use: mesh, comp offset -0.024
                  === MainDDARing ===
                  Scheduled moves: 169139, completed moves: 169139, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                  === AuxDDARing ===
                  Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                  === Heat ===
                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is ready with "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File* is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger* is idle in state(s) 0
                  Queue* is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon* is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === Network ===
                  Slowest loop: 1.44ms; fastest: 0.01ms
                  Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                  HTTP sessions: 0 of 8
                  - Ethernet -
                  State: disabled
                  Error counts: 0 0 0 0 0
                  Socket states: 0 0 0 0 0 0 0 0
                  === Filament sensors ===
                  Extruder 0 sensor: ok
                  === CAN ===
                  Messages sent 44905, longest wait 0ms for type 0
                  === Linux interface ===
                  State: 0, failed transfers: 1
                  Last transfer: 17ms ago
                  RX/TX seq numbers: 36691/32296
                  SPI underruns 1, overruns 0
                  Number of disconnects: 0
                  Buffer RX/TX: 0/0-0
                  === Duet Control Server ===
                  Duet Control Server v3.1.1
                  Daemon:
                  Finishing macro daemon.g, started by system
                  > Next stack level
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 32.48
                  
                  1 Reply Last reply Reply Quote 0
                  • A Former User?
                    A Former User @Phaedrux
                    last edited by

                    @Phaedrux said in Duet 3 SBC DCS has stopped:

                    @CaLviNx It's not irony because no one ever disagreed with you.

                    The irony is that time and effort has been needlessly expended in a vain attempt to fix an issue that the reason for (at this point of time) is evidently unknown when, instead of trying to fix it, the smart approach would have been to just go standalone in the first place which would have resulted in getting the machine printing again, and printing is the whole point of the exercise.

                    Phaedruxundefined dhusoloundefined 2 Replies Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator @A Former User
                      last edited by

                      @CaLviNx It must be difficult going through life with such superior intellect. How do you manage to survive amongst us?

                      Z-Bot CoreXY Build | Thingiverse Profile

                      A Former User? 1 Reply Last reply Reply Quote 0
                      • dhusoloundefined
                        dhusolo @A Former User
                        last edited by

                        @CaLviNx seriously stop commenting. I do beta testing and bug fixing for a living. I took the steps I did for a reason. Everyone else has been trying to help while all you've been doing is throwing jabs in and out of this thread. I don't need you to tell me what the "smart approach" is because "the whole point of the exercise" is to figure out what happened and to see if I could fix it, not applying a band-aid.

                        1 Reply Last reply Reply Quote 2
                        • chrishammundefined
                          chrishamm administrators
                          last edited by

                          To get back to the topic: I think the previously reported problems should be fixed in 3.2.0-b3.2. Feel free to test this again.

                          Duet software engineer

                          dhusoloundefined 1 Reply Last reply Reply Quote 0
                          • A Former User?
                            A Former User @Phaedrux
                            last edited by

                            @Phaedrux said in Duet 3 SBC DCS has stopped:

                            @CaLviNx It must be difficult going through life with such superior intellect. How do you manage to survive amongst us?

                            Trust me dealing with such stupidity on a daily basis is tiresome.....

                            1 Reply Last reply Reply Quote 0
                            • dhusoloundefined
                              dhusolo @chrishamm
                              last edited by

                              @chrishamm That did fix the issue but after updating to 3.2.b3 I started to have jerky movements while printing that wasn't present before the update

                              chrishammundefined 1 Reply Last reply Reply Quote 0
                              • chrishammundefined
                                chrishamm administrators @dhusolo
                                last edited by

                                @dhusolo Please confirm that the installed RRF version is 3.2.0-beta3.2 and not 3.2.0-beta3.

                                Duet software engineer

                                dhusoloundefined 1 Reply Last reply Reply Quote 0
                                • dhusoloundefined
                                  dhusolo @chrishamm
                                  last edited by

                                  @chrishamm can confirm it was 3.2.b3

                                  M122
                                  === Diagnostics ===
                                  RepRapFirmware for Duet 3 MB6HC version 3.2-beta3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                  Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                                  Used output buffers: 1 of 40 (10 max)
                                  === RTOS ===
                                  Static ram: 122236
                                  Dynamic ram: 139164 of which 24 recycled
                                  Never used RAM 130768, free system stack 200 words
                                  Tasks: Linux(ready,97) HEAT(blocked,296) CanReceiv(blocked,948) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,54) MAIN(running,1189) IDLE(ready,19)
                                  Owned mutexes: HTTP(MAIN)
                                  === Platform ===
                                  Last reset 00:00:20 ago, cause: software
                                  Last software reset at 2020-11-16 16:14, reason: User, GCodes spinning, available RAM 130768, slot 0
                                  Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0xffffffff Task Linu
                                  Error status: 0x00
                                  MCU temperature: min 38.3, current 38.7, max 38.8
                                  Supply voltage: min 24.6, current 24.7, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                                  12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                  Driver 0: position 0, standstill, reads 35729, writes 14 timeouts 0, SG min/max 0/0
                                  Driver 1: position 0, standstill, reads 35730, writes 14 timeouts 0, SG min/max 0/0
                                  Driver 2: position 0, standstill, reads 35731, writes 14 timeouts 0, SG min/max 0/0
                                  Driver 3: position 0, standstill, reads 35732, writes 14 timeouts 0, SG min/max 0/0
                                  Driver 4: position 0, standstill, reads 35733, writes 14 timeouts 0, SG min/max 0/0
                                  Driver 5: position 0, standstill, reads 35733, writes 14 timeouts 0, SG min/max 0/0
                                  Date/time: 2020-11-16 16:14:56
                                  Slowest loop: 1.42ms; fastest: 0.19ms
                                  === Storage ===
                                  Free file entries: 10
                                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                  === Move ===
                                  Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                                  Bed compensation in use: none, comp offset 0.000
                                  === MainDDARing ===
                                  Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                  === AuxDDARing ===
                                  Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                  === Heat ===
                                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                  === GCodes ===
                                  Segments left: 0
                                  Movement lock held by null
                                  HTTP* is doing "M122" in state(s) 0
                                  Telnet is idle in state(s) 0
                                  File is idle in state(s) 0
                                  USB is idle in state(s) 0
                                  Aux is idle in state(s) 0
                                  Trigger* is idle in state(s) 0
                                  Queue is idle in state(s) 0
                                  LCD is idle in state(s) 0
                                  SBC is idle in state(s) 0
                                  Daemon is idle in state(s) 0
                                  Aux2 is idle in state(s) 0
                                  Autopause is idle in state(s) 0
                                  Code queue is empty.
                                  === Filament sensors ===
                                  Extruder 0 sensor: ok
                                  === CAN ===
                                  Messages sent 55, send timeouts 55, longest wait 0ms for type 0, free CAN buffers 47
                                  === SBC interface ===
                                  State: 0, failed transfers: 0
                                  Last transfer: 20ms ago
                                  RX/TX seq numbers: 440/442
                                  SPI underruns 0, overruns 0
                                  Number of disconnects: 0, IAP RAM available 0x20a30
                                  Buffer RX/TX: 0/0-0
                                  === Duet Control Server ===
                                  Duet Control Server v3.2.0-beta3
                                  Code buffer space: 4096
                                  Configured SPI speed: 8000000 Hz
                                  Full transfers per second: 30.36
                                  
                                  chrishammundefined 1 Reply Last reply Reply Quote 0
                                  • chrishammundefined
                                    chrishamm administrators @dhusolo
                                    last edited by

                                    @dhusolo What triggers are you using? Can you share the corresponding macro files?

                                    Duet software engineer

                                    dhusoloundefined 2 Replies Last reply Reply Quote 0
                                    • dhusoloundefined
                                      dhusolo @chrishamm
                                      last edited by

                                      @chrishamm Actually I'm not actively using the trigger anymore. That was originally configured for RRF2 as a shutdown button. trigger2.g might exist but it's not defined in config.g.

                                      I've tried printing with 3.2.b3 to see if the jerky movements come back. So far it hasn't. It's a different model and it's slower speeds so i'm wondering if the print speeds had been related to why it was doing it. I'm going to try that other file again to see if I can replicate it. If I can at my normal print speeds I'll slow it down to see if it happens again.

                                      1 Reply Last reply Reply Quote 0
                                      • dhusoloundefined
                                        dhusolo @chrishamm
                                        last edited by

                                        @chrishamm I ran the print that had the jerky movement after updating and it seemed like it printed normally.

                                        I made sure I followed the getting started link verbatim. Originally I didn't use Etcher or the Raspberry Pi Imager program to write the image. I used a program called USB Image Tool because i've been using it for years. This time I used the Raspberry Pi Imager. The only other thing I can think I did different was I don't remember changing the buffer size before

                                        echo "options spidev bufsiz=8192" | sudo tee /etc/modprobe.d/spidev.conf
                                        
                                        1 Reply Last reply Reply Quote 0
                                        • dhusoloundefined
                                          dhusolo
                                          last edited by

                                          Well it happened again while running 3.2.b3. It has been printing pretty good the last week. Over night the print cancelled but it just stopped printing. The heaters are still at temp and the head was in the same position on the print, it didn't run pause.g.

                                          When I started DWC on my PC the print status was still printing. I pressed pause and that's when it ran pause.g. I tried to resume the print and it said cannot print no file selected

                                          m122
                                          === Diagnostics ===
                                          RepRapFirmware for Duet 3 MB6HC version 3.2-beta3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                          Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                                          Used output buffers: 1 of 40 (12 max)
                                          === RTOS ===
                                          Static ram: 122236
                                          Dynamic ram: 139788 of which 64 recycled
                                          Never used RAM 130104, free system stack 118 words
                                          Tasks: Linux(ready,67) HEAT(blocked,295) CanReceiv(blocked,948) CanSender(blocked,343) CanClock(blocked,352) TMC(blocked,18) MAIN(running,669) IDLE(ready,19)
                                          Owned mutexes: HTTP(MAIN)
                                          === Platform ===
                                          Last reset 14:24:35 ago, cause: software
                                          Last software reset at 2020-11-22 19:53, reason: User, GCodes spinning, available RAM 130104, slot 2
                                          Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0xffffffff Task Linu
                                          Error status: 0x00
                                          MCU temperature: min 35.4, current 37.2, max 38.3
                                          Supply voltage: min 24.2, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
                                          12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
                                          Driver 0: position 200, standstill, reads 25360, writes 21 timeouts 0, SG min/max 0/202
                                          Driver 1: position -200, standstill, reads 25349, writes 33 timeouts 0, SG min/max 0/1023
                                          Driver 2: position 5843, standstill, reads 25350, writes 33 timeouts 0, SG min/max 0/1023
                                          Driver 3: position 0, standstill, reads 25350, writes 33 timeouts 0, SG min/max 0/1023
                                          Driver 4: position 0, standstill, reads 25351, writes 33 timeouts 0, SG min/max 0/1023
                                          Driver 5: position 0, standstill, reads 25352, writes 33 timeouts 0, SG min/max 0/1023
                                          Date/time: 2020-11-23 10:17:46
                                          Slowest loop: 278.17ms; fastest: 0.09ms
                                          === Storage ===
                                          Free file entries: 10
                                          SD card 0 not detected, interface speed: 37.5MBytes/sec
                                          SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                          === Move ===
                                          Hiccups: 0(0), FreeDm: 375, MinFreeDm: 354, MaxWait: 10418300ms
                                          Bed compensation in use: mesh, comp offset 0.000
                                          === MainDDARing ===
                                          Scheduled moves 480277, completed moves 480277, StepErrors 0, LaErrors 0, Underruns [0, 0, 3], CDDA state -1
                                          === AuxDDARing ===
                                          Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                          === Heat ===
                                          Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                          === GCodes ===
                                          Segments left: 0
                                          Movement lock held by null
                                          HTTP* is doing "M122" in state(s) 0
                                          Telnet is idle in state(s) 0
                                          File* is idle in state(s) 0
                                          USB is idle in state(s) 0
                                          Aux is idle in state(s) 0
                                          Trigger* is idle in state(s) 0
                                          Queue* is idle in state(s) 0
                                          LCD is idle in state(s) 0
                                          SBC is idle in state(s) 0
                                          Daemon is idle in state(s) 0
                                          Aux2 is idle in state(s) 0
                                          Autopause is idle in state(s) 0
                                          Code queue is empty.
                                          === Filament sensors ===
                                          Extruder 0 sensor: ok
                                          === CAN ===
                                          Messages sent 207659, send timeouts 207659, longest wait 0ms for type 0, free CAN buffers 47
                                          === SBC interface ===
                                          State: 0, failed transfers: 1
                                          Last transfer: 19ms ago
                                          RX/TX seq numbers: 27088/26081
                                          SPI underruns 3, overruns 0
                                          Number of disconnects: 0, IAP RAM available 0x20a30
                                          Buffer RX/TX: 0/0-0
                                          === Duet Control Server ===
                                          Duet Control Server v3.2.0-beta3
                                          Code buffer space: 4096
                                          Configured SPI speed: 8000000 Hz
                                          Full transfers per second: 32.32
                                          
                                          chrishammundefined 1 Reply Last reply Reply Quote 0
                                          • chrishammundefined
                                            chrishamm administrators @dhusolo
                                            last edited by

                                            @dhusolo Please upgrade to 3.2-b4, it should be fixed in the latest builds.

                                            Duet software engineer

                                            1 Reply Last reply Reply Quote 0
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