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    Duet 3 SBC DCS has stopped

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • dhusoloundefined
      dhusolo @jay_s_uk
      last edited by

      @jay_s_uk
      I had to start DCS and DWS manually but I was able to get to the web interface.

      M122 "DSF"
      === Duet Control Server ===
      Duet Control Server v3.2.0-beta3
      Code buffer space: 4096
      Configured SPI speed: 8000000 Hz
      Full transfers per second: 32.68
      11/8/2020, 2:58:59 PM```	
      
      M122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.2-beta3 running on Duet 3 MB6HC v1.01 or later (SBC mode)
      Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
      Used output buffers: 1 of 40 (10 max)
      === RTOS ===
      Static ram: 122124
      Dynamic ram: 137508 of which 0 recycled
      Never used RAM 132560, free system stack 185 words
      Tasks: Linux(ready,131) HEAT(blocked,362) CanReceiv(blocked,948) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,66) MAIN(running,1300) IDLE(ready,19)
      Owned mutexes: HTTP(MAIN)
      === Platform ===
      Last reset 00:09:17 ago, cause: software
      Last software reset details not available
      Error status: 0x00
      MCU temperature: min 25.3, current 26.2, max 26.4
      Supply voltage: min 0.3, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
      12V rail voltage: min 0.1, current 0.2, max 0.2, under voltage events: 0
      Driver 0: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
      Driver 1: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
      Driver 2: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
      Driver 3: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
      Driver 4: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
      Driver 5: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
      Date/time: 2020-11-08 14:58:59
      Slowest loop: 743.08ms; fastest: 0.16ms
      === Storage ===
      Free file entries: 10
      SD card 0 not detected, interface speed: 37.5MBytes/sec
      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
      === Move ===
      Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
      Bed compensation in use: none, comp offset 0.000
      === MainDDARing ===
      Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === AuxDDARing ===
      Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
      === GCodes ===
      Segments left: 0
      Movement lock held by null
      HTTP* is doing "M122" in state(s) 0
      Telnet is idle in state(s) 0
      File is idle in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger* is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon is idle in state(s) 0
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      Code queue is empty.
      === CAN ===
      Messages sent 0, send timeouts 0, longest wait 0ms for type 0, free CAN buffers 47
      === SBC interface ===
      State: 0, failed transfers: 1
      Last transfer: 14ms ago
      RX/TX seq numbers: 17902/17903
      SPI underruns 0, overruns 0
      Number of disconnects: 0, IAP RAM available 0x20aa0
      Buffer RX/TX: 0/0-0
      === Duet Control Server ===
      Duet Control Server v3.2.0-beta3
      Code buffer space: 4096
      Configured SPI speed: 8000000 Hz
      Full transfers per second: 32.56
      
      jay_s_ukundefined 1 Reply Last reply Reply Quote 0
      • jay_s_ukundefined
        jay_s_uk @dhusolo
        last edited by

        @dhusolo well at least you're back on the latest firmware.
        @chrishamm any comments on the error above whilst updating?

        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

        1 Reply Last reply Reply Quote 0
        • dhusoloundefined
          dhusolo
          last edited by

          More of a status update: I've started the same print again but I don't load any filament. I didn't want to waste the filament if it's going to cancel on me again.

          However I can now hear some strange jerky movements. I have a coreXY so it's hard to narrow down what stepper it's coming from especially since there's no filament going through it.

          Phaedruxundefined 1 Reply Last reply Reply Quote 0
          • oliofundefined
            oliof
            last edited by

            I think my recent post about issues with 3.2b3 are very similar to this issue.

            <>RatRig V-Minion Fly Super5Pro RRF<> V-Core 3.1 IDEX k*****r <> RatRig V-Minion SKR 2 Marlin<>

            1 Reply Last reply Reply Quote 2
            • Phaedruxundefined
              Phaedrux Moderator @dhusolo
              last edited by

              @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

              Z-Bot CoreXY Build | Thingiverse Profile

              A Former User? dhusoloundefined 2 Replies Last reply Reply Quote 0
              • A Former User?
                A Former User @Phaedrux
                last edited by

                @Phaedrux said in Duet 3 SBC DCS has stopped:

                @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                Oh the irony.....

                Phaedruxundefined 1 Reply Last reply Reply Quote 0
                • dhusoloundefined
                  dhusolo @Phaedrux
                  last edited by

                  @Phaedrux I'm going to attempt to go back to RRF 3.1.1 with RPI since issues with connecting are resolved. Doesn't make a lot of sense that it was working previously for 3 months without any issue.

                  If that brings the same symptoms I'll run it in standalone until RRF 3.2 is stable. At least I know the board isn't bad

                  1 Reply Last reply Reply Quote 0
                  • Phaedruxundefined
                    Phaedrux Moderator @A Former User
                    last edited by

                    @CaLviNx It's not irony because no one ever disagreed with you.

                    Z-Bot CoreXY Build | Thingiverse Profile

                    A Former User? 1 Reply Last reply Reply Quote 0
                    • dhusoloundefined
                      dhusolo
                      last edited by

                      Can confirm going back to 3.1.1. the bug is still present. No idea why it appeared months after the original upload and weeks after any update to my config.

                      I did notice under Linux interface it shows a failed transfer, some bit loss and a SPI underrun

                      	M122
                      === Diagnostics ===
                      RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                      Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                      Used output buffers: 1 of 40 (12 max)
                      === RTOS ===
                      Static ram: 154604
                      Dynamic ram: 163392 of which 140 recycled
                      Exception stack ram used: 584
                      Never used ram: 74496
                      Tasks: NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1384) CanClock(blocked,1436) TMC(blocked,60) MAIN(running,2672) IDLE(ready,76)
                      Owned mutexes:
                      === Platform ===
                      Last reset 03:06:26 ago, cause: power up
                      Last software reset at 2020-11-09 16:57, reason: User, spinning module LinuxInterface, available RAM 77008 bytes (slot 1)
                      Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                      Error status: 0
                      MCU temperature: min 34.4, current 37.6, max 39.2
                      Supply voltage: min 24.2, current 24.5, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                      12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
                      Driver 0: standstill, reads 55804, writes 22 timeouts 0, SG min/max 0/193
                      Driver 1: standstill, reads 55797, writes 30 timeouts 0, SG min/max 0/1023
                      Driver 2: standstill, reads 55797, writes 30 timeouts 0, SG min/max 0/1023
                      Driver 3: standstill, reads 55794, writes 34 timeouts 0, SG min/max 0/1023
                      Driver 4: standstill, reads 55794, writes 34 timeouts 0, SG min/max 0/1023
                      Driver 5: standstill, reads 55795, writes 34 timeouts 0, SG min/max 0/1023
                      Date/time: 2020-11-09 20:05:07
                      Slowest loop: 9.46ms; fastest: 0.14ms
                      === Storage ===
                      Free file entries: 10
                      SD card 0 not detected, interface speed: 37.5MBytes/sec
                      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                      === Move ===
                      Hiccups: 0(0), FreeDm: 375, MinFreeDm: 317, MaxWait: 669637ms
                      Bed compensation in use: mesh, comp offset -0.024
                      === MainDDARing ===
                      Scheduled moves: 169139, completed moves: 169139, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                      === AuxDDARing ===
                      Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                      === Heat ===
                      Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                      === GCodes ===
                      Segments left: 0
                      Movement lock held by null
                      HTTP* is ready with "M122" in state(s) 0
                      Telnet is idle in state(s) 0
                      File* is idle in state(s) 0
                      USB is idle in state(s) 0
                      Aux is idle in state(s) 0
                      Trigger* is idle in state(s) 0
                      Queue* is idle in state(s) 0
                      LCD is idle in state(s) 0
                      SBC is idle in state(s) 0
                      Daemon* is idle in state(s) 0
                      Aux2 is idle in state(s) 0
                      Autopause is idle in state(s) 0
                      Code queue is empty.
                      === Network ===
                      Slowest loop: 1.44ms; fastest: 0.01ms
                      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                      HTTP sessions: 0 of 8
                      - Ethernet -
                      State: disabled
                      Error counts: 0 0 0 0 0
                      Socket states: 0 0 0 0 0 0 0 0
                      === Filament sensors ===
                      Extruder 0 sensor: ok
                      === CAN ===
                      Messages sent 44905, longest wait 0ms for type 0
                      === Linux interface ===
                      State: 0, failed transfers: 1
                      Last transfer: 17ms ago
                      RX/TX seq numbers: 36691/32296
                      SPI underruns 1, overruns 0
                      Number of disconnects: 0
                      Buffer RX/TX: 0/0-0
                      === Duet Control Server ===
                      Duet Control Server v3.1.1
                      Daemon:
                      Finishing macro daemon.g, started by system
                      > Next stack level
                      Code buffer space: 4096
                      Configured SPI speed: 8000000 Hz
                      Full transfers per second: 32.48
                      
                      1 Reply Last reply Reply Quote 0
                      • A Former User?
                        A Former User @Phaedrux
                        last edited by

                        @Phaedrux said in Duet 3 SBC DCS has stopped:

                        @CaLviNx It's not irony because no one ever disagreed with you.

                        The irony is that time and effort has been needlessly expended in a vain attempt to fix an issue that the reason for (at this point of time) is evidently unknown when, instead of trying to fix it, the smart approach would have been to just go standalone in the first place which would have resulted in getting the machine printing again, and printing is the whole point of the exercise.

                        Phaedruxundefined dhusoloundefined 2 Replies Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator @A Former User
                          last edited by

                          @CaLviNx It must be difficult going through life with such superior intellect. How do you manage to survive amongst us?

                          Z-Bot CoreXY Build | Thingiverse Profile

                          A Former User? 1 Reply Last reply Reply Quote 0
                          • dhusoloundefined
                            dhusolo @A Former User
                            last edited by

                            @CaLviNx seriously stop commenting. I do beta testing and bug fixing for a living. I took the steps I did for a reason. Everyone else has been trying to help while all you've been doing is throwing jabs in and out of this thread. I don't need you to tell me what the "smart approach" is because "the whole point of the exercise" is to figure out what happened and to see if I could fix it, not applying a band-aid.

                            1 Reply Last reply Reply Quote 2
                            • chrishammundefined
                              chrishamm administrators
                              last edited by

                              To get back to the topic: I think the previously reported problems should be fixed in 3.2.0-b3.2. Feel free to test this again.

                              Duet software engineer

                              dhusoloundefined 1 Reply Last reply Reply Quote 0
                              • A Former User?
                                A Former User @Phaedrux
                                last edited by

                                @Phaedrux said in Duet 3 SBC DCS has stopped:

                                @CaLviNx It must be difficult going through life with such superior intellect. How do you manage to survive amongst us?

                                Trust me dealing with such stupidity on a daily basis is tiresome.....

                                1 Reply Last reply Reply Quote 0
                                • dhusoloundefined
                                  dhusolo @chrishamm
                                  last edited by

                                  @chrishamm That did fix the issue but after updating to 3.2.b3 I started to have jerky movements while printing that wasn't present before the update

                                  chrishammundefined 1 Reply Last reply Reply Quote 0
                                  • chrishammundefined
                                    chrishamm administrators @dhusolo
                                    last edited by

                                    @dhusolo Please confirm that the installed RRF version is 3.2.0-beta3.2 and not 3.2.0-beta3.

                                    Duet software engineer

                                    dhusoloundefined 1 Reply Last reply Reply Quote 0
                                    • dhusoloundefined
                                      dhusolo @chrishamm
                                      last edited by

                                      @chrishamm can confirm it was 3.2.b3

                                      M122
                                      === Diagnostics ===
                                      RepRapFirmware for Duet 3 MB6HC version 3.2-beta3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                      Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                                      Used output buffers: 1 of 40 (10 max)
                                      === RTOS ===
                                      Static ram: 122236
                                      Dynamic ram: 139164 of which 24 recycled
                                      Never used RAM 130768, free system stack 200 words
                                      Tasks: Linux(ready,97) HEAT(blocked,296) CanReceiv(blocked,948) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,54) MAIN(running,1189) IDLE(ready,19)
                                      Owned mutexes: HTTP(MAIN)
                                      === Platform ===
                                      Last reset 00:00:20 ago, cause: software
                                      Last software reset at 2020-11-16 16:14, reason: User, GCodes spinning, available RAM 130768, slot 0
                                      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0xffffffff Task Linu
                                      Error status: 0x00
                                      MCU temperature: min 38.3, current 38.7, max 38.8
                                      Supply voltage: min 24.6, current 24.7, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                                      12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                      Driver 0: position 0, standstill, reads 35729, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 1: position 0, standstill, reads 35730, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 2: position 0, standstill, reads 35731, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 3: position 0, standstill, reads 35732, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 4: position 0, standstill, reads 35733, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 5: position 0, standstill, reads 35733, writes 14 timeouts 0, SG min/max 0/0
                                      Date/time: 2020-11-16 16:14:56
                                      Slowest loop: 1.42ms; fastest: 0.19ms
                                      === Storage ===
                                      Free file entries: 10
                                      SD card 0 not detected, interface speed: 37.5MBytes/sec
                                      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                      === Move ===
                                      Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                                      Bed compensation in use: none, comp offset 0.000
                                      === MainDDARing ===
                                      Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                      === AuxDDARing ===
                                      Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                      === Heat ===
                                      Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                      === GCodes ===
                                      Segments left: 0
                                      Movement lock held by null
                                      HTTP* is doing "M122" in state(s) 0
                                      Telnet is idle in state(s) 0
                                      File is idle in state(s) 0
                                      USB is idle in state(s) 0
                                      Aux is idle in state(s) 0
                                      Trigger* is idle in state(s) 0
                                      Queue is idle in state(s) 0
                                      LCD is idle in state(s) 0
                                      SBC is idle in state(s) 0
                                      Daemon is idle in state(s) 0
                                      Aux2 is idle in state(s) 0
                                      Autopause is idle in state(s) 0
                                      Code queue is empty.
                                      === Filament sensors ===
                                      Extruder 0 sensor: ok
                                      === CAN ===
                                      Messages sent 55, send timeouts 55, longest wait 0ms for type 0, free CAN buffers 47
                                      === SBC interface ===
                                      State: 0, failed transfers: 0
                                      Last transfer: 20ms ago
                                      RX/TX seq numbers: 440/442
                                      SPI underruns 0, overruns 0
                                      Number of disconnects: 0, IAP RAM available 0x20a30
                                      Buffer RX/TX: 0/0-0
                                      === Duet Control Server ===
                                      Duet Control Server v3.2.0-beta3
                                      Code buffer space: 4096
                                      Configured SPI speed: 8000000 Hz
                                      Full transfers per second: 30.36
                                      
                                      chrishammundefined 1 Reply Last reply Reply Quote 0
                                      • chrishammundefined
                                        chrishamm administrators @dhusolo
                                        last edited by

                                        @dhusolo What triggers are you using? Can you share the corresponding macro files?

                                        Duet software engineer

                                        dhusoloundefined 2 Replies Last reply Reply Quote 0
                                        • dhusoloundefined
                                          dhusolo @chrishamm
                                          last edited by

                                          @chrishamm Actually I'm not actively using the trigger anymore. That was originally configured for RRF2 as a shutdown button. trigger2.g might exist but it's not defined in config.g.

                                          I've tried printing with 3.2.b3 to see if the jerky movements come back. So far it hasn't. It's a different model and it's slower speeds so i'm wondering if the print speeds had been related to why it was doing it. I'm going to try that other file again to see if I can replicate it. If I can at my normal print speeds I'll slow it down to see if it happens again.

                                          1 Reply Last reply Reply Quote 0
                                          • dhusoloundefined
                                            dhusolo @chrishamm
                                            last edited by

                                            @chrishamm I ran the print that had the jerky movement after updating and it seemed like it printed normally.

                                            I made sure I followed the getting started link verbatim. Originally I didn't use Etcher or the Raspberry Pi Imager program to write the image. I used a program called USB Image Tool because i've been using it for years. This time I used the Raspberry Pi Imager. The only other thing I can think I did different was I don't remember changing the buffer size before

                                            echo "options spidev bufsiz=8192" | sudo tee /etc/modprobe.d/spidev.conf
                                            
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