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    Duet 3 SBC DCS has stopped

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • dhusoloundefined
      dhusolo
      last edited by

      but to your earlier question I tried updating to the beta following this and updating the source list to use unstable version

      1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        Would you be willing to test beta 3 once again?

        Z-Bot CoreXY Build | Thingiverse Profile

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        • dhusoloundefined
          dhusolo
          last edited by

          Sure. Should I use the getting started link or manually flash? I've tried compiling the firmware myself but with no success which is why I used the instructions in the link

          jay_s_ukundefined 1 Reply Last reply Reply Quote 0
          • jay_s_ukundefined
            jay_s_uk @dhusolo
            last edited by jay_s_uk

            @dhusolo that should be all you need to follow to move over to the unstable branch.
            There's no need to use the erase button to load the firmware as it will be updated as part of the upgrade process

            Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

            1 Reply Last reply Reply Quote 1
            • dhusoloundefined
              dhusolo
              last edited by

              I thought i did it correct but I got this error

              pi@duet3:~ $ sudo apt-get install duetsoftwareframework
              Reading package lists... Done
              Building dependency tree       
              Reading state information... Done
              The following additional packages will be installed:
                duetcontrolserver duetruntime duetsd duettools duetwebcontrol duetwebserver
                reprapfirmware
              The following packages will be upgraded:
                duetcontrolserver duetruntime duetsd duetsoftwareframework duettools
                duetwebcontrol duetwebserver reprapfirmware
              8 upgraded, 0 newly installed, 0 to remove and 118 not upgraded.
              Need to get 34.0 MB of archives.
              After this operation, 0 B of additional disk space will be used.
              Do you want to continue? [Y/n] y
              Get:1 https://pkg.duet3d.com unstable/armv7 armhf duetsoftwareframework armhf 3.2.0-beta3 [2,034 B]
              Get:2 https://pkg.duet3d.com unstable/armv7 armhf duetsd all 1.1.0 [2,102 B]
              Get:3 https://pkg.duet3d.com unstable/armv7 armhf duettools armhf 3.2.0-beta3 [62.2 kB]
              Get:4 https://pkg.duet3d.com unstable/armv7 armhf duetcontrolserver armhf 3.2.0-beta3 [226 kB]
              Get:5 https://pkg.duet3d.com unstable/armv7 armhf duetruntime armhf 3.2.0-beta3 [28.9 MB]
              Get:6 https://pkg.duet3d.com unstable/armv7 armhf duetwebserver armhf 3.2.0-beta3 [83.9 kB]
              Get:7 https://pkg.duet3d.com unstable/armv7 armhf duetwebcontrol all 3.2.0-beta3 [3,507 kB]
              Get:8 https://pkg.duet3d.com unstable/armv7 armhf reprapfirmware all 3.2.0-beta3-1 [1,260 kB]
              Fetched 34.0 MB in 19s (1,813 kB/s)                                           
              Reading changelogs... Done
              (Reading database ... 79179 files and directories currently installed.)
              Preparing to unpack .../0-duetsoftwareframework_3.2.0-beta3_armhf.deb ...
              Unpacking duetsoftwareframework (3.2.0-beta3) over (3.1.1) ...
              Preparing to unpack .../1-duetsd_1.1.0_all.deb ...
              Unpacking duetsd (1.1.0) over (1.0.6) ...
              Preparing to unpack .../2-duettools_3.2.0-beta3_armhf.deb ...
              Unpacking duettools (3.2.0-beta3) over (3.1.1) ...
              Preparing to unpack .../3-duetcontrolserver_3.2.0-beta3_armhf.deb ...
              Unpacking duetcontrolserver (3.2.0-beta3) over (3.1.1) ...
              Preparing to unpack .../4-duetruntime_3.2.0-beta3_armhf.deb ...
              Unpacking duetruntime (3.2.0-beta3) over (3.1.1) ...
              Preparing to unpack .../5-duetwebserver_3.2.0-beta3_armhf.deb ...
              Unpacking duetwebserver (3.2.0-beta3) over (3.1.0) ...
              Preparing to unpack .../6-duetwebcontrol_3.2.0-beta3_all.deb ...
              Unpacking duetwebcontrol (3.2.0-beta3) over (3.1.1) ...
              Preparing to unpack .../7-reprapfirmware_3.2.0-beta3-1_all.deb ...
              Unpacking reprapfirmware (3.2.0-beta3-1) over (3.1.1-1) ...
              Setting up duetruntime (3.2.0-beta3) ...
              Setting up duetcontrolserver (3.2.0-beta3) ...
              Installing new version of config file /opt/dsf/conf/config.json ...
              Creating group dsf with gid 995.
              Creating user dsf (n/a) with uid 995 and gid 995.
              Setting up duettools (3.2.0-beta3) ...
              Setting up duetwebserver (3.2.0-beta3) ...
              Setting up duetsoftwareframework (3.2.0-beta3) ...
              To modify config files consider adding yourself to the dsf groupd: # usermod -a -G dsf <username>
              Setting up duetwebcontrol (3.2.0-beta3) ...
              Setting up duetsd (1.1.0) ...
              Setting up reprapfirmware (3.2.0-beta3-1) ...
              Sending update request to DCS... Error: Failed to send update request
              Unhandled exception. System.Threading.Tasks.TaskCanceledException: A task was canceled.
                 at DuetAPIClient.BaseConnection.PerformCommand[T](BaseCommand command, CancellationToken cancellationToken) in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetAPIClient/BaseConnection.cs:line 188
                 at DuetControlServer.Program.CheckForAnotherInstance() in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetControlServer/Program.cs:line 305
                 at DuetControlServer.Program.Main(String[] args) in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetControlServer/Program.cs:line 84
                 at DuetControlServer.Program.<Main>(String[] args)
              
              
              jay_s_ukundefined 1 Reply Last reply Reply Quote 0
              • jay_s_ukundefined
                jay_s_uk @dhusolo
                last edited by jay_s_uk

                @dhusolo
                Are you still able to connect to the board via DWC?
                If you can confirm the firmware version using 3.1.1
                If it's still 3.1.1, send M997 B0
                I would be interested to see if you get any errors reported

                Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                dhusoloundefined 1 Reply Last reply Reply Quote 0
                • dhusoloundefined
                  dhusolo @jay_s_uk
                  last edited by

                  @jay_s_uk
                  I had to start DCS and DWS manually but I was able to get to the web interface.

                  M122 "DSF"
                  === Duet Control Server ===
                  Duet Control Server v3.2.0-beta3
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 32.68
                  11/8/2020, 2:58:59 PM```	
                  
                  M122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.2-beta3 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                  Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                  Used output buffers: 1 of 40 (10 max)
                  === RTOS ===
                  Static ram: 122124
                  Dynamic ram: 137508 of which 0 recycled
                  Never used RAM 132560, free system stack 185 words
                  Tasks: Linux(ready,131) HEAT(blocked,362) CanReceiv(blocked,948) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,66) MAIN(running,1300) IDLE(ready,19)
                  Owned mutexes: HTTP(MAIN)
                  === Platform ===
                  Last reset 00:09:17 ago, cause: software
                  Last software reset details not available
                  Error status: 0x00
                  MCU temperature: min 25.3, current 26.2, max 26.4
                  Supply voltage: min 0.3, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
                  12V rail voltage: min 0.1, current 0.2, max 0.2, under voltage events: 0
                  Driver 0: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                  Driver 1: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                  Driver 2: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                  Driver 3: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                  Driver 4: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                  Driver 5: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                  Date/time: 2020-11-08 14:58:59
                  Slowest loop: 743.08ms; fastest: 0.16ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                  Bed compensation in use: none, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === AuxDDARing ===
                  Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === Heat ===
                  Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is doing "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger* is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === CAN ===
                  Messages sent 0, send timeouts 0, longest wait 0ms for type 0, free CAN buffers 47
                  === SBC interface ===
                  State: 0, failed transfers: 1
                  Last transfer: 14ms ago
                  RX/TX seq numbers: 17902/17903
                  SPI underruns 0, overruns 0
                  Number of disconnects: 0, IAP RAM available 0x20aa0
                  Buffer RX/TX: 0/0-0
                  === Duet Control Server ===
                  Duet Control Server v3.2.0-beta3
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 32.56
                  
                  jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                  • jay_s_ukundefined
                    jay_s_uk @dhusolo
                    last edited by

                    @dhusolo well at least you're back on the latest firmware.
                    @chrishamm any comments on the error above whilst updating?

                    Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                    1 Reply Last reply Reply Quote 0
                    • dhusoloundefined
                      dhusolo
                      last edited by

                      More of a status update: I've started the same print again but I don't load any filament. I didn't want to waste the filament if it's going to cancel on me again.

                      However I can now hear some strange jerky movements. I have a coreXY so it's hard to narrow down what stepper it's coming from especially since there's no filament going through it.

                      Phaedruxundefined 1 Reply Last reply Reply Quote 0
                      • oliofundefined
                        oliof
                        last edited by

                        I think my recent post about issues with 3.2b3 are very similar to this issue.

                        <>RatRig V-Minion Fly Super5Pro RRF<> V-Core 3.1 IDEX k*****r <> RatRig V-Minion SKR 2 Marlin<>

                        1 Reply Last reply Reply Quote 2
                        • Phaedruxundefined
                          Phaedrux Moderator @dhusolo
                          last edited by

                          @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                          Z-Bot CoreXY Build | Thingiverse Profile

                          A Former User? dhusoloundefined 2 Replies Last reply Reply Quote 0
                          • A Former User?
                            A Former User @Phaedrux
                            last edited by

                            @Phaedrux said in Duet 3 SBC DCS has stopped:

                            @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                            Oh the irony.....

                            Phaedruxundefined 1 Reply Last reply Reply Quote 0
                            • dhusoloundefined
                              dhusolo @Phaedrux
                              last edited by

                              @Phaedrux I'm going to attempt to go back to RRF 3.1.1 with RPI since issues with connecting are resolved. Doesn't make a lot of sense that it was working previously for 3 months without any issue.

                              If that brings the same symptoms I'll run it in standalone until RRF 3.2 is stable. At least I know the board isn't bad

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                              • Phaedruxundefined
                                Phaedrux Moderator @A Former User
                                last edited by

                                @CaLviNx It's not irony because no one ever disagreed with you.

                                Z-Bot CoreXY Build | Thingiverse Profile

                                A Former User? 1 Reply Last reply Reply Quote 0
                                • dhusoloundefined
                                  dhusolo
                                  last edited by

                                  Can confirm going back to 3.1.1. the bug is still present. No idea why it appeared months after the original upload and weeks after any update to my config.

                                  I did notice under Linux interface it shows a failed transfer, some bit loss and a SPI underrun

                                  	M122
                                  === Diagnostics ===
                                  RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                  Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                                  Used output buffers: 1 of 40 (12 max)
                                  === RTOS ===
                                  Static ram: 154604
                                  Dynamic ram: 163392 of which 140 recycled
                                  Exception stack ram used: 584
                                  Never used ram: 74496
                                  Tasks: NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1384) CanClock(blocked,1436) TMC(blocked,60) MAIN(running,2672) IDLE(ready,76)
                                  Owned mutexes:
                                  === Platform ===
                                  Last reset 03:06:26 ago, cause: power up
                                  Last software reset at 2020-11-09 16:57, reason: User, spinning module LinuxInterface, available RAM 77008 bytes (slot 1)
                                  Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                  Error status: 0
                                  MCU temperature: min 34.4, current 37.6, max 39.2
                                  Supply voltage: min 24.2, current 24.5, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                                  12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
                                  Driver 0: standstill, reads 55804, writes 22 timeouts 0, SG min/max 0/193
                                  Driver 1: standstill, reads 55797, writes 30 timeouts 0, SG min/max 0/1023
                                  Driver 2: standstill, reads 55797, writes 30 timeouts 0, SG min/max 0/1023
                                  Driver 3: standstill, reads 55794, writes 34 timeouts 0, SG min/max 0/1023
                                  Driver 4: standstill, reads 55794, writes 34 timeouts 0, SG min/max 0/1023
                                  Driver 5: standstill, reads 55795, writes 34 timeouts 0, SG min/max 0/1023
                                  Date/time: 2020-11-09 20:05:07
                                  Slowest loop: 9.46ms; fastest: 0.14ms
                                  === Storage ===
                                  Free file entries: 10
                                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                  === Move ===
                                  Hiccups: 0(0), FreeDm: 375, MinFreeDm: 317, MaxWait: 669637ms
                                  Bed compensation in use: mesh, comp offset -0.024
                                  === MainDDARing ===
                                  Scheduled moves: 169139, completed moves: 169139, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                                  === AuxDDARing ===
                                  Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                                  === Heat ===
                                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                  === GCodes ===
                                  Segments left: 0
                                  Movement lock held by null
                                  HTTP* is ready with "M122" in state(s) 0
                                  Telnet is idle in state(s) 0
                                  File* is idle in state(s) 0
                                  USB is idle in state(s) 0
                                  Aux is idle in state(s) 0
                                  Trigger* is idle in state(s) 0
                                  Queue* is idle in state(s) 0
                                  LCD is idle in state(s) 0
                                  SBC is idle in state(s) 0
                                  Daemon* is idle in state(s) 0
                                  Aux2 is idle in state(s) 0
                                  Autopause is idle in state(s) 0
                                  Code queue is empty.
                                  === Network ===
                                  Slowest loop: 1.44ms; fastest: 0.01ms
                                  Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                                  HTTP sessions: 0 of 8
                                  - Ethernet -
                                  State: disabled
                                  Error counts: 0 0 0 0 0
                                  Socket states: 0 0 0 0 0 0 0 0
                                  === Filament sensors ===
                                  Extruder 0 sensor: ok
                                  === CAN ===
                                  Messages sent 44905, longest wait 0ms for type 0
                                  === Linux interface ===
                                  State: 0, failed transfers: 1
                                  Last transfer: 17ms ago
                                  RX/TX seq numbers: 36691/32296
                                  SPI underruns 1, overruns 0
                                  Number of disconnects: 0
                                  Buffer RX/TX: 0/0-0
                                  === Duet Control Server ===
                                  Duet Control Server v3.1.1
                                  Daemon:
                                  Finishing macro daemon.g, started by system
                                  > Next stack level
                                  Code buffer space: 4096
                                  Configured SPI speed: 8000000 Hz
                                  Full transfers per second: 32.48
                                  
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                                  • A Former User?
                                    A Former User @Phaedrux
                                    last edited by

                                    @Phaedrux said in Duet 3 SBC DCS has stopped:

                                    @CaLviNx It's not irony because no one ever disagreed with you.

                                    The irony is that time and effort has been needlessly expended in a vain attempt to fix an issue that the reason for (at this point of time) is evidently unknown when, instead of trying to fix it, the smart approach would have been to just go standalone in the first place which would have resulted in getting the machine printing again, and printing is the whole point of the exercise.

                                    Phaedruxundefined dhusoloundefined 2 Replies Last reply Reply Quote 0
                                    • Phaedruxundefined
                                      Phaedrux Moderator @A Former User
                                      last edited by

                                      @CaLviNx It must be difficult going through life with such superior intellect. How do you manage to survive amongst us?

                                      Z-Bot CoreXY Build | Thingiverse Profile

                                      A Former User? 1 Reply Last reply Reply Quote 0
                                      • dhusoloundefined
                                        dhusolo @A Former User
                                        last edited by

                                        @CaLviNx seriously stop commenting. I do beta testing and bug fixing for a living. I took the steps I did for a reason. Everyone else has been trying to help while all you've been doing is throwing jabs in and out of this thread. I don't need you to tell me what the "smart approach" is because "the whole point of the exercise" is to figure out what happened and to see if I could fix it, not applying a band-aid.

                                        1 Reply Last reply Reply Quote 2
                                        • chrishammundefined
                                          chrishamm administrators
                                          last edited by

                                          To get back to the topic: I think the previously reported problems should be fixed in 3.2.0-b3.2. Feel free to test this again.

                                          Duet software engineer

                                          dhusoloundefined 1 Reply Last reply Reply Quote 0
                                          • A Former User?
                                            A Former User @Phaedrux
                                            last edited by

                                            @Phaedrux said in Duet 3 SBC DCS has stopped:

                                            @CaLviNx It must be difficult going through life with such superior intellect. How do you manage to survive amongst us?

                                            Trust me dealing with such stupidity on a daily basis is tiresome.....

                                            1 Reply Last reply Reply Quote 0
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