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    Controlled arc problem

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    • whopping pochardundefined
      whopping pochard
      last edited by

      Your 'squaretest' file has only G1 moves, right? Are you sure you aren't missing steps due to a mechanical or electrical problem?

      1 Reply Last reply Reply Quote 1
      • cjmundefined
        cjm @neilo
        last edited by

        @neilo

        I've used a Duet 2 board running RepRapFirmware for Duet 2 WiFi/Ethernet 3.2-beta1 (2020-09-15b1) with a homebrew CNC to machine a test piece containing diamond, circle and square sections:

        SquareDiamondCircle.jpg

        The g-code for this with a 5mm diameter end mill is as follows and contains both G2 and G3 commands that the Duet appears to have executed correctly:

        SquareDiamondCircle 42mm.g

        The finishing passes for the circular section are complete circles so one assumes should have shown up the same sort of error you're seeing if this was intrinsic to the Duet hardware/firmware?

        Perhaps trying this g-code file might help diagnose the problem?

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        • neiloundefined
          neilo
          last edited by

          @whopping-pochard that's right just trying to keep it simple with G1 commands in one file. I've added another test (fig 3)fig3.jpg
          and it appears to act erratically. Mechanically it looks fine, it's belt drive on X and Y NEMA 23 FYI .
          steps.g

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          • neiloundefined
            neilo
            last edited by

            @cjm just seen your post - many thanks I will try it out tomorrow.

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            • neiloundefined
              neilo
              last edited by

              @cjm here is the result: Still looks weird and clearly incorrect. I used a 1/4 inch bit so slight dimensional difference but does not explain for me the strange behaviour.
              Would you mind sharing your config.g file with me please?
              WIN_20210106_11_07_32_Pro.jpg
              Thanks,
              Neil

              droftartsundefined 1 Reply Last reply Reply Quote 0
              • droftartsundefined
                droftarts administrators @neilo
                last edited by

                @neilo I think this is a mechanically issue. My best guess is that the X pulley is slipping on the motor shaft, because the first move of any change in direction in X causes the movement error, but subsequent ones do not. Probably the grub screw on the pulley is loose, allowing a limited range of movement.

                Ian

                Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                1 Reply Last reply Reply Quote 2
                • sonderzugundefined
                  sonderzug
                  last edited by

                  I second @droftarts opinion; circles with horizontal and vertical flat spots (i.e. corresponding to the direction change of the x respectively the y axis) indicate mechanical backlash, quite noticable in your case.

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                  • alankilianundefined
                    alankilian
                    last edited by

                    One way to test this theory is to make a square, but rotated 90-degrees.

                    That way, you get two reversals of each axis while the other axis is moving continuously in the same direction.

                    You'll see the vertices get messed up if you've got a lot of backlash.

                    AND you can do it with just G1 moves.

                    SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

                    droftartsundefined 1 Reply Last reply Reply Quote 0
                    • droftartsundefined
                      droftarts administrators @alankilian
                      last edited by

                      @alankilian said in Controlled arc problem:

                      One way to test this theory is to make a square, but rotated 90-degrees.

                      Don't you mean 45 degrees?!

                      Ian

                      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                      alankilianundefined 1 Reply Last reply Reply Quote 1
                      • neiloundefined
                        neilo
                        last edited by

                        Thanks folks for the opinions really appreciate independent advice! I will focus on the mechanicals and re-test the square / diamond combo.
                        Neil

                        1 Reply Last reply Reply Quote 0
                        • alankilianundefined
                          alankilian @droftarts
                          last edited by

                          @droftarts said in Controlled arc problem:

                          Don't you mean 45 degrees?!

                          Ha ha.

                          Yes. Thanks for catching my lack-of-coffee posting.

                          SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

                          1 Reply Last reply Reply Quote 0
                          • cjmundefined
                            cjm
                            last edited by cjm

                            @neilo The behaviour does look odd.
                            It is interesting that some of the part (e.g. the upper left quadrant) is machined OK over multiple layers.
                            As mentioned by others, this implies something is loose, perhaps a drive block, so that when the axis is driven in one direction the slack is taken up and the movement is controlled, but when there is a change of direction, the slack needs to be taken up in the other direction before movement control is restored. i.e. backlash, but with much more movement (around 4-5mm by the looks of the part) than normal.
                            With the spindle/router powered down and unplugged for safety, if you send the machine to XY coordinates in the middle of its range and then manually try move the spindle/axes carriages in X and Y directions what do you feel?
                            Everything should be tight, with no knock or play.

                            I'm not sure it will help but as requested here's my config.sys file:
                            config.g

                            1 Reply Last reply Reply Quote 1
                            • alankilianundefined
                              alankilian
                              last edited by

                              This seems like a big enough error that you should be able to measure it with a ruler.

                              Try:

                              g0 x0 y0
                              (Mark the position)
                              g0 x100
                              (Check to see if it moved 100mm)
                              g0 x0
                              (Check to see if it moved 100mm back)

                              If there's a lot of backlash in the X mechanics, you'll see one or the other of those moves be less than 100mm

                              SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

                              1 Reply Last reply Reply Quote 0
                              • neiloundefined
                                neilo
                                last edited by

                                Dear all, thanks so much for the advice, the loose grub screw was the root cause which was definitely in my blind spot! Learnt a lot and really appreciate the support, looking much better now with some tweaks.
                                Neil
                                WIN_20210109_13_55_44_Pro.jpg

                                cjmundefined 1 Reply Last reply Reply Quote 4
                                • whopping pochardundefined
                                  whopping pochard
                                  last edited by

                                  Hooray!! Glad you solved it!

                                  1 Reply Last reply Reply Quote 0
                                  • cjmundefined
                                    cjm @neilo
                                    last edited by

                                    @neilo great news!

                                    1 Reply Last reply Reply Quote 0
                                    • alankilianundefined
                                      alankilian
                                      last edited by

                                      Wonderful!

                                      I'm glad you kept at it. This is a good story for the next person struggling to solve a difficult issue.

                                      SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

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