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    Controlled arc problem

    Scheduled Pinned Locked Moved Solved
    CNC
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    • droftartsundefined
      droftarts administrators @neilo
      last edited by

      @neilo I think this is a mechanically issue. My best guess is that the X pulley is slipping on the motor shaft, because the first move of any change in direction in X causes the movement error, but subsequent ones do not. Probably the grub screw on the pulley is loose, allowing a limited range of movement.

      Ian

      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

      1 Reply Last reply Reply Quote 2
      • sonderzugundefined
        sonderzug
        last edited by

        I second @droftarts opinion; circles with horizontal and vertical flat spots (i.e. corresponding to the direction change of the x respectively the y axis) indicate mechanical backlash, quite noticable in your case.

        1 Reply Last reply Reply Quote 1
        • alankilianundefined
          alankilian
          last edited by

          One way to test this theory is to make a square, but rotated 90-degrees.

          That way, you get two reversals of each axis while the other axis is moving continuously in the same direction.

          You'll see the vertices get messed up if you've got a lot of backlash.

          AND you can do it with just G1 moves.

          SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

          droftartsundefined 1 Reply Last reply Reply Quote 0
          • droftartsundefined
            droftarts administrators @alankilian
            last edited by

            @alankilian said in Controlled arc problem:

            One way to test this theory is to make a square, but rotated 90-degrees.

            Don't you mean 45 degrees?!

            Ian

            Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

            alankilianundefined 1 Reply Last reply Reply Quote 1
            • neiloundefined
              neilo
              last edited by

              Thanks folks for the opinions really appreciate independent advice! I will focus on the mechanicals and re-test the square / diamond combo.
              Neil

              1 Reply Last reply Reply Quote 0
              • alankilianundefined
                alankilian @droftarts
                last edited by

                @droftarts said in Controlled arc problem:

                Don't you mean 45 degrees?!

                Ha ha.

                Yes. Thanks for catching my lack-of-coffee posting.

                SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

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                • cjmundefined
                  cjm
                  last edited by cjm

                  @neilo The behaviour does look odd.
                  It is interesting that some of the part (e.g. the upper left quadrant) is machined OK over multiple layers.
                  As mentioned by others, this implies something is loose, perhaps a drive block, so that when the axis is driven in one direction the slack is taken up and the movement is controlled, but when there is a change of direction, the slack needs to be taken up in the other direction before movement control is restored. i.e. backlash, but with much more movement (around 4-5mm by the looks of the part) than normal.
                  With the spindle/router powered down and unplugged for safety, if you send the machine to XY coordinates in the middle of its range and then manually try move the spindle/axes carriages in X and Y directions what do you feel?
                  Everything should be tight, with no knock or play.

                  I'm not sure it will help but as requested here's my config.sys file:
                  config.g

                  1 Reply Last reply Reply Quote 1
                  • alankilianundefined
                    alankilian
                    last edited by

                    This seems like a big enough error that you should be able to measure it with a ruler.

                    Try:

                    g0 x0 y0
                    (Mark the position)
                    g0 x100
                    (Check to see if it moved 100mm)
                    g0 x0
                    (Check to see if it moved 100mm back)

                    If there's a lot of backlash in the X mechanics, you'll see one or the other of those moves be less than 100mm

                    SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

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                    • neiloundefined
                      neilo
                      last edited by

                      Dear all, thanks so much for the advice, the loose grub screw was the root cause which was definitely in my blind spot! Learnt a lot and really appreciate the support, looking much better now with some tweaks.
                      Neil
                      WIN_20210109_13_55_44_Pro.jpg

                      cjmundefined 1 Reply Last reply Reply Quote 4
                      • whopping pochardundefined
                        whopping pochard
                        last edited by

                        Hooray!! Glad you solved it!

                        1 Reply Last reply Reply Quote 0
                        • cjmundefined
                          cjm @neilo
                          last edited by

                          @neilo great news!

                          1 Reply Last reply Reply Quote 0
                          • alankilianundefined
                            alankilian
                            last edited by

                            Wonderful!

                            I'm glad you kept at it. This is a good story for the next person struggling to solve a difficult issue.

                            SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

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