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    Missing Steps - Cant Print SpreadCycle StealthChop tuning help

    Scheduled Pinned Locked Moved Solved
    Tuning and tweaking
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    • carcamerarigundefined
      carcamerarig @dc42
      last edited by

      @dc42

      bang 1

      Date	Event	
      19/04/2021, 23:06:54	M569.2 P0.4 R111
      Register 0x6f value 0x40080000
      19/04/2021, 23:06:49	M569.2 P0.3 R111
      Register 0x6f value 0x40080000
      19/04/2021, 23:06:45	M569.2 P0.2 R111
      Register 0x6f value 0x40080000
      19/04/2021, 23:06:40	M569.2 P0.1 R111
      Register 0x6f value 0x00080000
      19/04/2021, 23:06:34	M569.2 P0.0 R111
      Register 0x6f value 0x80080000
      19/04/2021, 23:02:19	M32 "0:/gcodes/Sat1.gcode"
      File 0:/gcodes/Sat1.gcode selected for printing
      19/04/2021, 23:02:13	M569 P0.1 D2
      19/04/2021, 23:02:06	M569 P0.0 D2
      
      1 Reply Last reply Reply Quote 0
      • carcamerarigundefined
        carcamerarig @dc42
        last edited by

        @dc42

        So in spreadcycle its banging like a hooker on smack..... I let it run for a bit but something going to break again so ive quit it! The supposed switchover banging on infill is even more prominent but its not supposed to switching in D2 right??
        I'll upload the video of the infill bangs (mini bangs) but I didn't catch a travel move bang, too busy reporting M569.2 P# R111's...

        19/04/2021, 23:16:24	Printing paused at X186.4 Y40.6 Z3.0
        19/04/2021, 23:16:20	M25
        Resume state saved
        19/04/2021, 23:16:13	M569.2 P0.4 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:16:10	M569.2 P0.3 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:16:06	M569.2 P0.2 R111
        Register 0x6f value 0xc0080000
        19/04/2021, 23:16:01	M569.2 P0.1 R111
        Register 0x6f value 0x00080000
        19/04/2021, 23:15:56	M569.2 P0.0 R111
        Register 0x6f value 0x80080000
        19/04/2021, 23:14:30	M569.2 P0.0 R111
        Register 0x6f value 0x00080000
        19/04/2021, 23:14:26	M569.2 P0.1 R111
        Register 0x6f value 0x00080000
        19/04/2021, 23:14:22	M569.2 P0.2 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:14:16	M569.2 P0.3 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:14:13	M569.2 P0.4 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:13:39	M569.2 P0.4 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:13:35	M569.2 P0.3 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:13:32	M569.2 P0.2 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:13:29	M569.2 P0.1 R111
        Register 0x6f value 0x00080000
        19/04/2021, 23:13:26	M569.2 P0.0 R111
        Register 0x6f value 0x00080000
        19/04/2021, 23:11:35	M569.2 P0.0 R111
        Register 0x6f value 0x00080000
        19/04/2021, 23:11:33	M569.2 P0.1 R111
        Register 0x6f value 0x00080000
        19/04/2021, 23:11:29	M569.2 P0.2 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:11:24	M569.2 P0.3 R111
        Register 0x6f value 0x40080000
        19/04/2021, 23:11:19	M569.2 P0.4 R111
        Register 0x6f value 0x40080000
        
        m122
        === Diagnostics ===
        RepRapFirmware for Duet 3 Mini 5+ version 3.3beta2+2 (2021-04-15 16:55:30) running on Duet 3 Mini5plus WiFi (standalone mode)
        Board ID: Z9NZN-A296U-D65J0-40KM4-LY03Z-ZPQPD
        Used output buffers: 3 of 40 (30 max)
        === RTOS ===
        Static ram: 100104
        Dynamic ram: 106340 of which 32 recycled
        Never used RAM 34372, free system stack 134 words
        Tasks: NETWORK(ready,202) HEAT(delaying,294) CanReceiv(notifyWait,944) CanSender(notifyWait,357) CanClock(delaying,334) TMC(delaying,71) MAIN(running,337) IDLE(ready,20) AIN(notifyWait,266)
        Owned mutexes: WiFi(NETWORK)
        === Platform ===
        Last reset 00:15:48 ago, cause: power up
        Last software reset at 2021-04-18 12:27, reason: User, GCodes spinning, available RAM 34372, slot 2
        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
        Error status: 0x00
        Aux0 errors 0,0,0
        Aux1 errors 0,0,0
        MCU revision 3, ADC conversions started 1090996, completed 1090995, timed out 0, errs 0
        Step timer max interval 26927
        Supply voltage: min 23.4, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
        Heap OK, handles allocated/used 99/2, heap memory allocated/used/recyclable 2048/620/566, gc cycles 11
        Driver 0: position 35612, ok, SG min/max 0/400, read errors 0, write errors 0, ifcnt 21, reads 889, writes 0, timeouts 0, DMA errors 0
        Driver 1: position 10295, ok, SG min/max 0/504, read errors 0, write errors 0, ifcnt 20, reads 889, writes 0, timeouts 0, DMA errors 0
        Driver 2: position 1096, ok, SG min/max 0/206, read errors 0, write errors 0, ifcnt 17, reads 890, writes 0, timeouts 0, DMA errors 0
        Driver 3: position 0, ok, SG min/max 16/416, read errors 0, write errors 0, ifcnt 13, reads 890, writes 0, timeouts 0, DMA errors 0
        Driver 4: position 0, ok, SG min/max 0/112, read errors 0, write errors 0, ifcnt 18, reads 889, writes 0, timeouts 0, DMA errors 0
        Driver 5: position 0, assumed not present
        Driver 6: position 0, assumed not present
        Date/time: 2021-04-19 23:15:13
        Cache data hit count 1354624958
        Slowest loop: 87.00ms; fastest: 0.09ms
        === Storage ===
        Free file entries: 9
        SD card 0 detected, interface speed: 22.5MBytes/sec
        SD card longest read time 1.0ms, write time 5.0ms, max retries 0
        === Move ===
        DMs created 83, maxWait 0ms, bed compensation in use: mesh, comp offset 0.000
        === MainDDARing ===
        Scheduled moves 12869, completed moves 12829, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 17, 0], CDDA state 3
        === AuxDDARing ===
        Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
        === Heat ===
        Bed heaters = 0 -1, chamberHeaters = -1 -1
        Heater 0 is on, I-accum = 0.3
        Heater 1 is on, I-accum = 0.6
        === GCodes ===
        Segments left: 1
        Movement lock held by null
        HTTP is idle in state(s) 0
        Telnet is idle in state(s) 0
        File is doing "G1 X185.485 Y57.962 E0.01508" in state(s) 0
        USB is idle in state(s) 0
        Aux is idle in state(s) 0
        Trigger is idle in state(s) 0
        Queue is idle in state(s) 0
        LCD is idle in state(s) 0
        SBC is idle in state(s) 0
        Daemon is idle in state(s) 0
        Aux2 is idle in state(s) 0
        Autopause is idle in state(s) 0
        Code queue is empty.
        === Filament sensors ===
        Extruder 0 sensor: ok
        === CAN ===
        Messages queued 160, send timeouts 160, received 0, lost 0, longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 17 (min 17)
        Last cancelled message type 30 dest 127
        === Network ===
        Slowest loop: 216.27ms; fastest: 0.09ms
        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
        HTTP sessions: 1 of 8
        - WiFi -
        Network state is active
        WiFi module is connected to access point 
        Failed messages: pending 0, notready 0, noresp 1
        WiFi firmware version 1.25beta0
        WiFi MAC address f4:cf:a2:6f:e9:78
        WiFi Vcc 3.36, reset reason Power up
        WiFi flash size 2097152, free heap 21784
        WiFi IP address 192.168.1.226
        WiFi signal strength -41dBm, mode 802.11n, reconnections 0, sleep mode modem
        Clock register 00002002
        Socket states: 0 0 0 0 0 0 0 0
        
        19/04/2021, 23:23:46	M569 P0.4
        Drive 4 runs in reverse, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 0 (inf mm/sec), pwmScaleSum 64, pwmScaleAuto 9, pwmOfsAuto 255, pwmGradAuto 24, pos 168
        19/04/2021, 23:23:43	M569 P0.3
        Drive 3 runs in reverse, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 0 (inf mm/sec), pwmScaleSum 19, pwmScaleAuto 0, pwmOfsAuto 90, pwmGradAuto 18, pos 680
        19/04/2021, 23:23:40	M569 P0.2
        Drive 2 runs in reverse, active low enable, timing fast, mode stealthChop, ccr 0x00053, toff 3, tblank 0, tpwmthrs 0 (inf mm/sec), pwmScaleSum 60, pwmScaleAuto 5, pwmOfsAuto 255, pwmGradAuto 22, pos 72
        19/04/2021, 23:23:33	M569 P0.1
        Drive 1 runs in reverse, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 644
        19/04/2021, 23:23:27	M569 P0.0
        Drive 0 runs in reverse, active low enable, timing fast, mode spreadCycle, ccr 0x00053, toff 3, tblank 0, hstart/hend/hdec 5/0/0, pos 516
        
        1 Reply Last reply Reply Quote 0
        • carcamerarigundefined
          carcamerarig @dc42
          last edited by

          @dc42

          For clarity

          ; General preferences
          G90                                         ; Send absolute coordinates...
          M83                                         ; ...but relative extruder moves
          
          ; Network
          M550 P"Duet Caribou 420"                        	; Set machine name
          M552 S1                                     	; Enable network
          ;*** Access point is configured manually via M587
          ;M586 P0 S1                                  ; Enable HTTP
          ;M586 P1 S0                                  ; Disable FTP
          ;M586 P2 S0                                  ; Disable Telnet
          M575 P1 S1 B57600							; Panel Due
          
          ; Drive Mappings
          M569 P0.0 S0 D3 V0                             ; Drive 0: X Axis
          M569 P0.1 S0 D3 V0                             ; Drive 1: Y Axis
          M569 P0.2 S0 D3 V0                             ; Drive 2:  Z Axis
          M569 P0.3 S0 D3 V0                             ; Drive 3: E Axis
          M569 P0.4 S0 D3 V0                             ; Drive 4: E1 used for Z1
          
          ; Motor remapping for dual Z and axis Limits
          M584 X0 Y1 Z2:4 E3				; two Z motors connected to driver outputs Z and E1
          M671 X-37:287 Y0:0 S4			; leadscrews at left (connected to Z) and right (connected to E1) of X axis
          
          ; Micrpstepping and Speed
          M350 X32 Y32 E16 Z16 I1                     ; Configure microstepping with interpolation
          M92 X200.00 Y200.00 Z400.00 E830.00         ; Set steps per mm
          
          ; Speeds, Acceleration and Jerk
          M566 X900 Y900 Z25.00 E600.00 P1      ; Set maximum instantaneous speed changes (mm/min)
          M203 X18000.00 Y18000.00 Z720.00 E1200.00     ; Set maximum speeds (mm/min)
          M201 X1500.00 Y1500.00 Z1200.00 E4000.00     ; Set accelerations (mm/s^2)
          
          ; Motor currents
          M906 X700.00 Y700.00 Z700.00 E700.00 I20    ; Set motor currents (mA) and motor idle factor in percent X,Y,Z=1000/1.414 E=1400/1.414
          M84 S30                                     ; Set idle timeout
          
          ; Printer geometry
          M208 X0:250 Y-4:215 Z-0.5:410               ; Axis Limits
          M564 H0							            ; allow unhomed movement
          
          ; Endstops for each Axis
          M574 X1 S3								 	; Set endstops controlled by motor load detection
          M574 Y1 S3                               	; Set endstops controlled by motor load detection
          
          ; Stallgaurd Sensitivy
          ;M915 X S-2 F0 H200 R0		                ; Set X axis Sensitivity  MOVED TO HOMEALL.G
          ;M915 Y S15 F0 H200 R0		                ; Set y axis Sensitivity 
          
          ; Input Shaper
          ;M593 F58.5 P4 S0.2  ; Input Shaping 3.3/3.4
          ;M593 F54.26
          
          ; Z-Probe Super PINDA
          M574 Z1 S0 ; Set endstops controlled by probe
          M558 P5 C"^io3.in" I1 H1 F500 T4800 A30 S0.004
          
          ; Mesh Grid 
          M557 X24:221 Y10:195 P8	                         ; Define mesh grid for probing
          
          ; Sheets
          ;G31 P1000 X23 Y5 Z1.730 	                    ; Satin Sheet
          G31 P1000 X23 Y5 Z1.95 	  	                  ; Textured Sheet 
          ;G31 P1000 X23 Y5 Z1.445 					    ; PEI Sheet
          ;G31 P1000 X23 Y5 Z1.445 					    ; PEI Sheet 0.6 nozzle -10 offset
          
          
          ; Heatbed Heaters and Thermistor Bed 
          M308 S0 P"temp0" Y"thermistor" T100000 B4725 C7.060000e-8       ; Set thermistor + ADC parameters for heater 0 Bed
          M950 H0 C"out0" T0 Q10					                        ; Creates Bed Heater Qnn PWM frequency in Hz. Valid range: 0-65535, default: 500. (optional) 10hz stopped clicking
          M307 H0 R0.273 C345.3 D10.89 S1.00 V23.8 B0						; PID 3.2
          M140 H0										                    ; Bed uses Heater 0
          M143 H0 S120                                                    ; Set temperature limit for heater 0 to 120C Bed
          
          ; HotEnd Heaters and Thermistor HotEnd      
          M308 S1 P"temp1" Y"thermistor" T500000 B4725 C1.19622e-7	       	; define E0 temperature sensor e3d
          M950 H1 C"out1" T1 						                            ; Create HotEnd Heater
          M307 H1 R2.383 C178.5:130.6 D5.32 S1.00 V23.9 B0						; PID
          M143 H1 S285                                                    	; Set temperature limit for heater 1 to 285C HotEnd
          M302 S185 R185
          
          ; Fans
          M950 F1 C"out5" Q250				; Creates HOTEND Fan
          M106 P1 T45 S235 H1                 ; HOTEND Fan Settings
          M950 F0 C"out6" Q100				; Creates PARTS COOLING FAN
          M106 P0 H-1                         ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned off PARTS COOLING FAN
          
          ; Tools
          M563 P0 D0 H1 F0                            ; Define tool 0
          G10 P0 X0 Y0 Z0                             ; Set tool 0 axis offsets
          G10 P0 R0 S0                                ; Set initial tool 0 active and standby temperatures to 0C
          
          ; StealthCop calibration - MOVED TO HOMEALL.G
          ; M17
          ; G4 P150
          ; G1 X2 Y2 Z2 F2000 	
          ; G4 S2
          ; M84 ; disable motors
          
          ; Filament Sensor Logic
          M98 P"0:/macros/02_Functions/StartupFilamentSensorCheck"  ; Runout Sensor Logic: Startup with filament = runout sensor active   Startup without filament = autoload active
          

          Spreadcycle Video

          1 Reply Last reply Reply Quote 0
          • droftartsundefined
            droftarts administrators
            last edited by

            Seems like we might, finally, have nailed this one. After testing all day today, @dc42 noticed the longest loop time in @carcamerarig's M122 reports was very long, often over 100ms. Looking through the M122 reports taken during printing in this thread, he noticed the SD card read times were very long, too, eg:

            SD card longest read time 91.0ms, write time 5.2ms, max retries 0
            

            By comparison, my loop time and SD card longest read, running the same code:

            Slowest loop: 12.28ms; fastest: 0.10ms
            ...
            SD card longest read time 7.9ms, write time 0.0ms, max retries 0
            

            dc's current theory is that either the SD card is faulty, or the SD card interface is faulty. We're waiting for @carcamerarig to let us know if replacing the SD card helps.

            Ian

            Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

            dc42undefined 1 Reply Last reply Reply Quote 4
            • dc42undefined
              dc42 administrators @droftarts
              last edited by

              To add to that, we also now have a firmware build that doesn't have these problems despite the excessively slow SD card read performance.

              Duet WiFi hardware designer and firmware engineer
              Please do not ask me for Duet support via PM or email, use the forum
              http://www.escher3d.com, https://miscsolutions.wordpress.com

              1 Reply Last reply Reply Quote 3
              • droftartsundefined
                droftarts administrators
                last edited by droftarts

                All testing I was doing was with 0.9° motors (48mm long NEMA 17 motors, one from E3D, one from Wantai) with similar specs to LDO motors, running at x32 micro stepping with interpolation. These were quiet in stealthchop, and noisier in spreadcycle, but not noticeably noisier than 1.8° motors.

                I kept jerk settings high at 900mm/m (15mm/s) with Marlin jerk policy, acceleration at 2000mm/s^2, speeds up to 18,000mm/m (300mm/s). Motor current was 1000mA on X and Y, though these are 1.7A motors.

                With these setting (which are probably close to the limit my poor old machine can cope with!) I didn’t have any banging problems, though as noted in previous posts, we think these are actually related to an SD card problem.

                I also didn’t have problems in hybrid mode, so long as changeover speed was low, but could replicate the “micro banging” @carcamerarig experienced in gyroid fill if set around 35mm/s, which is to be expected as this is the speed gyroid fill was being printed at, so X and Y axes speed up and slow down through the changeover speed on each gyroid curve.

                One caveat is that I was using endstops for homing, not sensorless homing. We did get that working on @carcamerarig’s machine, I think reliably, though with 1.8 motors. I’ll test sensorless homing my setup when I can.

                I’ll update the documentation with best practices for all of that we’ve learnt in this process!

                Ian

                Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                dc42undefined 1 Reply Last reply Reply Quote 4
                • dc42undefined
                  dc42 administrators @droftarts
                  last edited by dc42

                  All, we have tracked down this issue. It affects Duet 3 Mini boards running all released firmware versions when a heater output is configured to a low PWM frequency - for example, when the bed heater is set to run at 10Hz because it is driven via a SSR. Unfortunately, there is a synchronisation delay between the heater management task and the PWM port, which causes the heater task to hog the CPU for up to one cycle at the PWM frequency, and that occasionally causes the movement system to fail to finalise moves before they are due to be executed.

                  We already have Duet 3 Mini firmware with improved motion planning that works around this, and I expect to fix the underlying issue shortly. The fix will be in the 3.3beta3 release, which I hope to make available within the next few days. Meanwhile, for anyone not using SSRs to drive heaters, the workaround is to use a higher PWM frequency, e.g. 100Hz or 500Hz.

                  Special thanks to @carcamerarig, who has worked closely with us over the last few days to help us get to the bottom of this.

                  Duet WiFi hardware designer and firmware engineer
                  Please do not ask me for Duet support via PM or email, use the forum
                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                  oc_geekundefined ctilley79undefined Argoundefined 3 Replies Last reply Reply Quote 7
                  • oc_geekundefined
                    oc_geek @dc42
                    last edited by

                    @dc42 good catch !

                    that might also be the issue behind slicer output .g files not completing the upload when the heater is turned on. They reach 100% but then start over again and again...
                    thanks

                    dc42undefined 1 Reply Last reply Reply Quote 1
                    • carcamerarigundefined
                      carcamerarig
                      last edited by

                      Thanks to everyone involved in this, there are a few of you LOL made especially testing for some with my lack of knowledge of RRF, Gcode and 3d printing in general. I've learned a lot in a short space of time and glad I didn't quit on the mini, I'm especially impressed with the level of support from the Duet team to find the cause and then produce a number fixed fw / workarounds until resolved.
                      Looking forward to 3.3b3 in few days 🙂

                      Phaedruxundefined 1 Reply Last reply Reply Quote 3
                      • ctilley79undefined
                        ctilley79 @dc42
                        last edited by

                        @dc42 You owe @carcamerarig a bottle of Macallan lol.

                        1 Reply Last reply Reply Quote 1
                        • Phaedruxundefined
                          Phaedrux Moderator @carcamerarig
                          last edited by

                          @carcamerarig Thanks for sticking with it.

                          Z-Bot CoreXY Build | Thingiverse Profile

                          1 Reply Last reply Reply Quote 2
                          • Argoundefined
                            Argo @dc42
                            last edited by Argo

                            @dc42

                            Oh that explains why I had trouble with slow downs at 10Hz and swiftly switched back to 100Hz because the slow downs were already obvious during the probing procedure.

                            https://forum.duet3d.com/topic/22142/slowdowns-pauses-pid-algorithm-and-pwm-freq?_=1619033412104

                            I already suspected it had something to do with internal cycles as Prusa explained that they also had issues with that.
                            https://blog.prusaprinters.org/dev-diary-2-how-we-made-the-heatbed-silent_30946/

                            1 Reply Last reply Reply Quote 0
                            • dc42undefined
                              dc42 administrators @oc_geek
                              last edited by

                              @oc_geek said in Missing Steps - Cant Print SpreadCycle StealthChop tuning help:

                              @dc42 good catch !

                              that might also be the issue behind slicer output .g files not completing the upload when the heater is turned on. They reach 100% but then start over again and again...
                              thanks

                              Yes. I did some tests on the old firmware with 5Hz PWM frequency and found that it completely disrupted file uploading. Anyway, a 1-line change has fixed the underlying issue, so we're hoping to release 3.3beta3 tomorrow.

                              Duet WiFi hardware designer and firmware engineer
                              Please do not ask me for Duet support via PM or email, use the forum
                              http://www.escher3d.com, https://miscsolutions.wordpress.com

                              fulgundefined 1 Reply Last reply Reply Quote 4
                              • fulgundefined
                                fulg @dc42
                                last edited by

                                I was unable to contribute to the troubleshooting efforts due to a missing board, but now that I have one again I just wanted to confirm that 3.3b3 has also completely solved this issue for me.

                                Thank you @dc42 for sticking with the thread, which often wandered outside of the subject at hand 🙂

                                Cheers,
                                Ben.

                                VORON V2 CoreXY + Duet3 Mini5+ Ethernet v1.0 with Mini2+ expansion, VORON V0 CoreXY + Duet2 Maestro

                                1 Reply Last reply Reply Quote 0
                                • carcamerarigundefined
                                  carcamerarig
                                  last edited by

                                  @fulg Well done, I think most issues have been resolved in this release which pretty cool eh. Not had a spare moment to print anything yet, hoping I will later tonight. 🤞🏼

                                  1 Reply Last reply Reply Quote 0
                                  • MartinNYHCundefined
                                    MartinNYHC
                                    last edited by MartinNYHC

                                    Just replaced a Duet 2 Wifi with a Mini 5 and upgraded to 3.3-rc1. Nothin else changed on the printer. Unfortunately it looks like i still have this issue. As described above after a "bang" there's a layer shift. Any ideas please?

                                    ; General preferences
                                    G90                                                    ; send absolute coordinates...
                                    M83                                                    ; ...but relative extruder moves
                                    M550 P"Voron0"                                         ; set printer name
                                    M669 K1                                                ; select CoreXY mode
                                    
                                    ; Drives
                                    M569 P0.0 S1 D3 V0	                                   ; physical drive 0 goes forwards
                                    M569 P0.1 S1 D3 V0
                                    M569 P0.2 S0	                                      ; physical drive 2 goes forwards
                                    M569 P0.3 S0                                            ; physical drive 3 goes forwards
                                    M584 X0.0 Y0.1 Z0.2 E0.3                                       ; set drive mapping
                                    M350 X16 Y16 Z16 E16 I1    	                           ; configure microstepping with interpolation
                                    
                                    M92 X80.00 Y80.00 Z320.00 E711.97  		               ; set steps per mm
                                    M566 X600.00 Y600.00 Z50.00 E2000.00    		       ; set maximum instantaneous speed changes (mm/min)
                                    M203 X20000.00 Y20000.00 Z1000.00 E5000.00      	   ; set maximum speeds (mm/min)
                                    M201 X2000.00 Y2000.00 Z200.00 E1000.00	               ; set accelerations (mm/s^2)
                                    M906 X400 Y400 Z600 E400 I75	                       ; set motor currents (mA) and motor idle factor in per cent
                                    M84 S120                                               ; Set idle timeout
                                    M572 D0 S0.061										   ; Pressure advance
                                    
                                    
                                    ; Axis Limits
                                    M208 X3 Y3 Z0 S1                                       ; set axis minima
                                    M208 X118 Y118 Z110 S0                                 ; set axis maxima
                                    
                                    ; Endstops
                                    M574 X2 S1 P"io1.in"                    				; configure active-high endstop for high end on X via pin io1.in
                                    M574 Y2 S1 P"io2.in"                    				; configure active-high endstop for high end on Y via pin io2.in
                                    M574 Z1 S1 P"io3.in"                    				; configure active-high endstop for high end on Z via pin io3.in
                                    
                                    ; Heaters
                                    M308 S0 P"temp0" Y"thermistor" T100000 B4092       		; configure sensor 0 as PT1000 on pin temp0
                                    M950 H0 C"out1" T0                      				; create bed heater output on out0 and map it to sensor 0
                                    M307 H0 B0 S1.00                        				; disable bang-bang mode for the bed heater and set PWM limit
                                    M140 H0                                 				; map heated bed to heater 0
                                    M143 H0 S120                            				; set temperature limit for heater 0 to 120C
                                    M308 S1 P"temp1" Y"thermistor" T100000 B3950        	; configure sensor 1 as PT1000 on pin temp1
                                    M950 H1 C"out2" T1                      				; create nozzle heater output on out1 and map it to sensor 1
                                    M307 H1 B0 S1.00                        				; disable bang-bang mode for heater  and set PWM limit
                                    M143 H1 S280                            				; set temperature limit for heater 1
                                    M308 S2 P"temp2" A"Chamber" Y"thermistor" T100000 B3950
                                    
                                    ; Fans
                                    M950 F0 C"out3" Q500                    				; create fan 0 on pin out3 and set its frequency
                                    M106 P0 C"Bed" S0 H-1                          				; set fan 0 value. Thermostatic control is turned off
                                    M950 F1 C"out4" Q2000                    				; create fan 1 on pin out4 and set its frequency
                                    M106 P1 C"Hotend" L0.70 X0.70 H1 T70 S0.70 B5           ; set fan 1 value. Thermostatic control is turned on
                                    M950 F2 C"out5"							 			   ; create fan 2 on pin fan2
                                    M106 P2 C"Chamber" S0 H-1								   ; set fan 2 name and values
                                    M950 F3 C"out6"							 			   ; create fan 2 on pin fan2
                                    M106 P3 C"Light" S1 H-1								   ; set fan 2 name and values
                                    
                                    ; Tools
                                    M563 P0 D0 H1 F0                                       ; define tool 0
                                    G10 P0 X0 Y0 Z0                                        ; set tool 0 axis offsets
                                    G10 P0 R0 S0                                           ; set initial tool 0 active and standby temperatures to 0C
                                    
                                    ; Miscellaneous
                                    M575 P1 S0 B57600                                      ; enable support for PanelDue
                                    M501
                                    T0                                                     ; select first tool
                                    
                                    
                                    05/05/2021, 11:22:32 	M122
                                    === Diagnostics ===
                                    RepRapFirmware for Duet 3 Mini 5+ version 3.3RC1 (2021-05-01 09:59:28) running on Duet 3 Mini5plus Ethernet (SBC mode)
                                    Board ID: J4FFG-A196U-D65J0-40KM4-MG03Z-HG970
                                    Used output buffers: 1 of 40 (40 max)
                                    === RTOS ===
                                    Static ram: 102476
                                    Dynamic ram: 92820 of which 0 recycled
                                    Never used RAM 45552, free system stack 114 words
                                    Tasks: SBC(resourceWait:,4.2%,294) HEAT(delaying,0.0%,320) Move(notifyWait,0.4%,276) CanReceiv(notifyWait,0.0%,943) CanSender(notifyWait,0.0%,357) CanClock(delaying,0.0%,341) TMC(notifyWait,0.7%,114) MAIN(running,93.9%,497) IDLE(ready,0.0%,29) AIN(delaying,0.8%,264), total 100.0%
                                    Owned mutexes: HTTP(MAIN)
                                    === Platform ===
                                    Last reset 00:39:02 ago, cause: power up
                                    Last software reset at 2021-05-05 09:54, reason: User, none spinning, available RAM 51896, slot 1
                                    Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0400f000 BFAR 0xe000ed38 SP 0x00000000 Task Linu Freestk 0 n/a
                                    Error status: 0x04
                                    Aux0 errors 0,0,0
                                    Aux1 errors 0,0,0
                                    MCU revision 3, ADC conversions started 2342835, completed 2342835, timed out 0, errs 0
                                    Step timer max interval 1490
                                    MCU temperature: min 37.7, current 43.2, max 43.7
                                    Supply voltage: min 23.7, current 24.3, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
                                    Heap OK, handles allocated/used 99/0, heap memory allocated/used/recyclable 2048/8/8, gc cycles 0
                                    Driver 0: position 8800, standstill, SG min/max 0/436, read errors 0, write errors 0, ifcnt 20, reads 57528, writes 20, timeouts 0, DMA errors 0
                                    Driver 1: position -7200, standstill, SG min/max 0/434, read errors 0, write errors 0, ifcnt 20, reads 57528, writes 20, timeouts 0, DMA errors 0
                                    Driver 2: position 4224, standstill, SG min/max 0/10, read errors 0, write errors 0, ifcnt 18, reads 57530, writes 18, timeouts 0, DMA errors 0
                                    Driver 3: position 0, standstill, SG min/max 0/44, read errors 0, write errors 0, ifcnt 16, reads 57531, writes 16, timeouts 0, DMA errors 0
                                    Driver 4: position 0, standstill, SG min/max 0/0, read errors 0, write errors 0, ifcnt 9, reads 57539, writes 9, timeouts 0, DMA errors 0
                                    Driver 5: position 0, assumed not present
                                    Driver 6: position 0, assumed not present
                                    Date/time: 2021-05-05 11:22:31
                                    Cache data hit count 3725941281
                                    Slowest loop: 158.94ms; fastest: 0.10ms
                                    === Storage ===
                                    Free file entries: 10
                                    SD card 0 not detected, interface speed: 0.0MBytes/sec
                                    SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                    === Move ===
                                    DMs created 83, maxWait 139363ms, bed compensation in use: none, comp offset 0.000
                                    === MainDDARing ===
                                    Scheduled moves 26047, completed moves 26047, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 33], CDDA state -1
                                    === AuxDDARing ===
                                    Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                    === Heat ===
                                    Bed heaters = 0 -1, chamberHeaters = -1 -1
                                    === GCodes ===
                                    Segments left: 0
                                    Movement lock held by null
                                    HTTP* is doing "M122" in state(s) 0
                                    Telnet is idle in state(s) 0
                                    File* is idle in state(s) 0
                                    USB is idle in state(s) 0
                                    Aux is idle in state(s) 0
                                    Trigger* is idle in state(s) 0
                                    Queue* is idle in state(s) 0
                                    LCD is idle in state(s) 0
                                    SBC is idle in state(s) 0
                                    Daemon is idle in state(s) 0
                                    Aux2 is idle in state(s) 0
                                    Autopause is idle in state(s) 0
                                    Code queue is empty.
                                    === CAN ===
                                    Messages queued 20985, send timeouts 20982, received 0, lost 0, longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 17 (min 17)
                                    Last cancelled message type 4514 dest 127
                                    === SBC interface ===
                                    State: 4, failed transfers: 0
                                    Last transfer: 4ms ago
                                    RX/TX seq numbers: 36438/36438
                                    SPI underruns 0, overruns 0
                                    Number of disconnects: 0, IAP RAM available 0x10c34
                                    Buffer RX/TX: 0/0-0
                                    === Duet Control Server ===
                                    Duet Control Server v3.3-rc1
                                    Code buffer space: 4096
                                    Configured SPI speed: 8000000 Hz
                                    Full transfers per second: 44.04
                                    Codes per second: 19.47
                                    Maximum length of RX/TX data transfers: 3460/1300
                                    

                                    IMG_0433.png

                                    dc42undefined 1 Reply Last reply Reply Quote 0
                                    • dc42undefined
                                      dc42 administrators @MartinNYHC
                                      last edited by

                                      @martinnyhc I suspect that your high maximum speeds (20000 mm/min in M203) are not compatible with running permanently in stealthChop mode. stealthChop doesn't work when the driver supply voltage is too low to overcome the inductive and rotational back emf of the motor. You can use the back EMF calculator at https://www.reprapfirmware.org/ to get an estimate of the speed at which this will occur.

                                      Duet WiFi hardware designer and firmware engineer
                                      Please do not ask me for Duet support via PM or email, use the forum
                                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                                      MartinNYHCundefined 1 Reply Last reply Reply Quote 0
                                      • MartinNYHCundefined
                                        MartinNYHC @dc42
                                        last edited by MartinNYHC

                                        @dc42 Used the calculator and used some conserative settings:

                                        M92 X80.00 Y80.00 Z320.00 E711.97  		               ; set steps per mm
                                        M566 X600.00 Y600.00 Z50.00 E2000.00    		       ; set maximum instantaneous speed changes (mm/min)
                                        M203 X8000.00 Y8000.00 Z1000.00 E5000.00 	     	   ; set maximum speeds (mm/min)
                                        M201 X2000.00 Y2000.00 Z200.00 E1000.00	               ; set accelerations (mm/s^2)
                                        M906 X400 Y400 Z600 E400 I75	                       ; set motor currents (mA) and motor idle factor in per cent
                                        M84 S120                                               ; Set idle timeout
                                        M572 D0 S0.061										   ; Pressure advance
                                        

                                        The result is better in terms of the amount of layer shifts. But it still happened two times during the print. With the Duet 2 Wifi I never configured any Stealthchop/Spreadcycle settings but due to the other drivers on the Mini 5 I had to because steppers sounded terrible.

                                        Is there anything else I can try? Thanks for your help in advance.

                                        IMG_0435.png

                                        droftartsundefined 1 Reply Last reply Reply Quote 0
                                        • droftartsundefined
                                          droftarts administrators @MartinNYHC
                                          last edited by

                                          @martinnyhc said in Missing Steps - Cant Print SpreadCycle StealthChop tuning help:

                                          With the Duet 2 Wifi I never configured any Stealthchop/Spreadcycle settings

                                          That's because the TMC2660 driver chips on Duet 2 WiFi only have spreadcycle.

                                          Most noticeable for noise is spreadcycle at standstill. To test if your missed steps are an issue with stealthchop, you can set the drivers to spreadcycle only when moving, and stealthchop when the are stationary. To do this, set the V parameter in M569 for X and Y to a relatively high number, something like V2000, then send M569 P0 and check the 'tpwmthrs' response. When I do this, I get 'tpwmthrs 2000 (2.3 mm/sec)', but it depends on your microstepping and steps per mm. Adjust the V parameter until it is somewhere between 5 and 10mm/s. Use this speed as it's below your M566 instantaneous speed setting of X600 Y600 (which is 10mm/s).

                                          Alternatively, switch it to spreadcycle for a test with M569 P# D2 (where # is the driver number).

                                          Ian

                                          Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                          MartinNYHCundefined 1 Reply Last reply Reply Quote 0
                                          • MartinNYHCundefined
                                            MartinNYHC @droftarts
                                            last edited by

                                            @droftarts Already tried D2. The problem is that as soon as I use D2 or D3 without a V value or V higher than 0 both steppers are sound like they are going to explode in a few seconds. And beside of that i cannot get rid of the layer shifts completely.

                                            droftartsundefined 1 Reply Last reply Reply Quote 0
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