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    Automatic Emergency Stop

    Scheduled Pinned Locked Moved
    Duet Hardware and wiring
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    • Sculpt Fabricatorundefined
      Sculpt Fabricator
      last edited by

      9/13/2022, 6:59:40 AM m122
      === Diagnostics ===
      RepRapFirmware for Duet 2 WiFi/Ethernet version 3.3 (2021-06-15 21:44:54) running on Duet WiFi 1.02 or later + DueX5
      Board ID: 08DLM-996RU-N85T0-6J1D4-3SJ6K-TAVZR
      Used output buffers: 3 of 24 (24 max)
      === RTOS ===
      Static ram: 23876
      Dynamic ram: 77308 of which 12 recycled
      Never used RAM 10364, free system stack 132 words
      Tasks: NETWORK(ready,14.2%,225) HEAT(delaying,0.0%,330) Move(notifyWait,0.1%,313) DUEX(notifyWait,0.0%,24) MAIN(running,85.7%,441) IDLE(ready,0.1%,29), total 100.0%
      Owned mutexes: WiFi(NETWORK)
      === Platform ===
      Last reset 00:30:38 ago, cause: software
      Last software reset at 2022-09-13 06:29, reason: User, GCodes spinning, available RAM 10364, slot 1
      Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
      Error status: 0x0c
      Aux0 errors 0,1,0
      Step timer max interval 0
      MCU temperature: min 34.6, current 35.0, max 36.9
      Supply voltage: min 22.7, current 23.9, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
      Heap OK, handles allocated/used 99/14, heap memory allocated/used/recyclable 2048/246/16, gc cycles 0
      Driver 0: position 0, standstill, SG min/max 0/0
      Driver 1: position 57500, standstill, SG min/max 0/71
      Driver 2: position 13866, standstill, SG min/max not available
      Driver 3: position 0, standstill, SG min/max not available
      Driver 4: position 0, standstill, SG min/max not available
      Driver 5: position 0, standstill, SG min/max 0/0
      Driver 6: position 0, standstill, SG min/max 0/278
      Driver 7: position 0, standstill, SG min/max 0/339
      Driver 8: position 0, standstill, SG min/max 0/321
      Driver 9: position 0, standstill, SG min/max 0/283
      Driver 10: position 0
      Driver 11: position 0
      Date/time: 2022-09-13 06:59:39
      Cache data hit count 4294967295
      Slowest loop: 10.52ms; fastest: 0.18ms
      I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
      === Storage ===
      Free file entries: 10
      SD card 0 detected, interface speed: 20.0MBytes/sec
      SD card longest read time 3.9ms, write time 0.0ms, max retries 0
      === Move ===
      DMs created 83, maxWait 3589ms, bed compensation in use: none, comp offset 0.000
      === MainDDARing ===
      Scheduled moves 7, completed moves 7, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === AuxDDARing ===
      Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters = -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
      Heater 0 is on, I-accum = 0.2
      === GCodes ===
      Segments left: 0
      Movement lock held by null
      HTTP is idle in state(s) 0
      Telnet is idle in state(s) 0
      File is idle in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      Daemon is idle in state(s) 0
      Autopause is idle in state(s) 0
      Code queue is empty.
      === Filament sensors ===
      Extruder 0 sensor: no data received
      Extruder 1 sensor: no data received
      === DueX ===
      Read count 1, 0.03 reads/min
      === Network ===
      Slowest loop: 82.42ms; fastest: 0.00ms
      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
      HTTP sessions: 2 of 8

      • WiFi -
        Network state is active
        WiFi module is connected to access point
        Failed messages: pending 0, notready 0, noresp 0
        WiFi firmware version 1.26
        WiFi MAC address ec:fa:bc:5b:41:b9
        WiFi Vcc 3.38, reset reason Turned on by main processor
        WiFi flash size 4194304, free heap 24504
        WiFi IP address 192.168.5.101
        WiFi signal strength -64dBm, mode 802.11n, reconnections 0, sleep mode modem
        Clock register 00002002
        Socket states: 0 0 0 0 0 0 0 0
      jay_s_ukundefined 1 Reply Last reply Reply Quote 0
      • jay_s_ukundefined
        jay_s_uk @Sculpt Fabricator
        last edited by

        @sculpt-fabricator i would suggest upgrading to 3.4.1 and seeing if it happens again

        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

        Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 0
        • Sculpt Fabricatorundefined
          Sculpt Fabricator @jay_s_uk
          last edited by

          @jay_s_uk

          Ok upgrades to 3.4.1
          started a print, it made it 22 min into the print and it Emergency stopped

             === Diagnostics ===
          RepRapFirmware for Duet 2 WiFi/Ethernet version 3.4.1 (2022-06-01 21:05:28) running on Duet WiFi 1.02 or later + DueX5
          Board ID: 08DLM-996RU-N85T0-6J1D4-3SJ6K-TAVZR
          Used output buffers: 10 of 26 (26 max)
          === RTOS ===
          Static ram: 23860
          Dynamic ram: 77116 of which 12 recycled
          Never used RAM 8236, free system stack 174 words
          Tasks: NETWORK(ready,13.2%,242) HEAT(notifyWait,0.0%,333) Move(notifyWait,0.0%,363) DUEX(notifyWait,0.0%,24) MAIN(running,86.3%,440) IDLE(ready,0.4%,30), total 100.0%
          Owned mutexes: WiFi(NETWORK)
          === Platform ===
          Last reset 00:03:14 ago, cause: software
          Last software reset at 2022-09-13 09:00, reason: User, GCodes spinning, available RAM 8236, slot 0
          Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
          Error status: 0x04
          Aux0 errors 0,0,0
          Step timer max interval 0
          MCU temperature: min 33.0, current 33.6, max 34.3
          Supply voltage: min 23.9, current 24.1, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
          Heap OK, handles allocated/used 99/14, heap memory allocated/used/recyclable 2048/230/0, gc cycles 0
          Events: 0 queued, 0 completed
          Driver 0: standstill, SG min n/a
          Driver 1: standstill, SG min n/a
          Driver 2: standstill, SG min n/a
          Driver 3: standstill, SG min n/a
          Driver 4: standstill, SG min n/a
          Driver 5: standstill, SG min n/a
          Driver 6: standstill, SG min n/a
          Driver 7: standstill, SG min n/a
          Driver 8: standstill, SG min n/a
          Driver 9: standstill, SG min n/a
          Driver 10: 
          Driver 11: 
          Date/time: 2022-09-13 09:03:54
          Cache data hit count 4294967295
          Slowest loop: 10.23ms; fastest: 0.20ms
          I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
          === Storage ===
          Free file entries: 10
          SD card 0 detected, interface speed: 20.0MBytes/sec
          SD card longest read time 3.5ms, write time 0.0ms, max retries 0
          === Move ===
          DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
          === MainDDARing ===
          Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
          === AuxDDARing ===
          Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
          === Heat ===
          Bed heaters -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
          === GCodes ===
          Segments left: 0
          Movement lock held by null
          HTTP is idle in state(s) 0
          Telnet is idle in state(s) 0
          File is idle in state(s) 0
          USB is idle in state(s) 0
          Aux is idle in state(s) 0
          Trigger is idle in state(s) 0
          Queue is idle in state(s) 0
          LCD is idle in state(s) 0
          Daemon is idle in state(s) 0
          Autopause is idle in state(s) 0
          Code queue is empty
          === Filament sensors ===
          Extruder 0 sensor: no data received
          Extruder 1 sensor: no data received
          === DueX ===
          Read count 1, 0.31 reads/min
          === Network ===
          Slowest loop: 79.94ms; fastest: 0.00ms
          Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
          HTTP sessions: 2 of 8
          - WiFi -
          Network state is active
          WiFi module is connected to access point 
          Failed messages: pending 0, notready 0, noresp 0
          WiFi firmware version 1.26
          WiFi MAC address ec:fa:bc:5b:41:b9
          WiFi Vcc 3.38, reset reason Turned on by main processor
          WiFi flash size 4194304, free heap 24944
          WiFi IP address 192.168.5.101
          WiFi signal strength -63dBm, mode 802.11n, reconnections 0, sleep mode modem
          Clock register 00002002
          Socket states: 0 0 0 0 0 0 0 0
          jay_s_ukundefined droftartsundefined 2 Replies Last reply Reply Quote 0
          • jay_s_ukundefined
            jay_s_uk @Sculpt Fabricator
            last edited by

            @sculpt-fabricator can you upload the print file?

            @dc42 any insight on the reset?

            Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

            Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 0
            • Sculpt Fabricatorundefined
              Sculpt Fabricator @jay_s_uk
              last edited by

              @jay_s_uk
              I have tried three different print files one of them we printed yesterday. The other two are new files we have not printed.

              jay_s_ukundefined 2 Replies Last reply Reply Quote 0
              • jay_s_ukundefined
                jay_s_uk @Sculpt Fabricator
                last edited by

                @sculpt-fabricator but can you upload a gcode file please

                Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 0
                • jay_s_ukundefined
                  jay_s_uk @Sculpt Fabricator
                  last edited by

                  @sculpt-fabricator oh, and also your config.g

                  Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                  Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 0
                  • Sculpt Fabricatorundefined
                    Sculpt Fabricator @jay_s_uk
                    last edited by

                    @jay_s_uk
                    I can get you the step file If you want

                    @dc24 I can reset it from the panel with the M999, rehome etc. and it back
                    to normal

                    jay_s_ukundefined 2 Replies Last reply Reply Quote 0
                    • jay_s_ukundefined
                      jay_s_uk @Sculpt Fabricator
                      last edited by

                      @sculpt-fabricator the step file is no use, which is why i have asked for the gcode

                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                      1 Reply Last reply Reply Quote 0
                      • Sculpt Fabricatorundefined
                        Sculpt Fabricator @jay_s_uk
                        last edited by

                        @jay_s_uk

                        Config G -

                        ; General preferences_________________________________________________________
                        G21 														; dimentions in mm
                        G90                                             			; for X,Y,Z     use absolute coordinate values
                        M83                                             			; for E0,E1,etc use relative coordinate values
                        M111 S0 													; Debug off
                        M555 P2 													; Set output to look like Marlin
                        M575 P0 B57600 S2              								; communication parameters for USB serial
                        M575 P1 B57600 S1											; Set auxiliary serial port baud rate and require checksum (for PanelDue)
                        
                        ; Network_____________________________________________________________________
                        M550 P"Big 60"                         						; set printer name
                        M552 S1                                        				; enable (S1) networking (WiFi)
                        M586 S1 P1 ;T0                 								; enable (S1) FTP    (P1) Disable TLS (T0)
                        M586 S1 P2 ;T0                								; enable (S1) Telnet (P2) Disable TLS (T0)
                        
                        ; mode control variables _____________________________________________________
                        global g_probe_z_trigger = 1.752                            ; default - set as appropriate for the Z probe 
                        global g_z_home            = 5                  ; can be used to always move Z to known height
                        global g_z_datum_set       = false              ; can be used to prevent unneeded setting of Z=0 datum
                         
                        global g_map_mode          = "300 point"        ; determines which kind of height map is created/loaded
                        global g_probe_mode        = "two consecutive"  ; determines if z proving used consecutive or averaging
                        global g_level_mode        = "4 point"          ; determines if 3 or 4 points are used for leveling
                         
                        global g_print_beg_prime   = 10                 ; default - set desired in filament config.g
                        global g_print_beg_retract = 0                  ; default - set desired in filament config.g
                         
                        global g_print_end_retract = 0                  ; default - set desired in filament config.g
                        global g_print_end_mode    = "heat off"         ; determines if heaters are turned off when print is done
                         
                        
                        ; Drives_________________________________________________________________________
                        
                        ;Main board______________________________________________________________________
                        M569 P0 S0                                                          ; Physical drive 0 . X1
                        M569 P1 S1                                                          ; Physical drive 1 . X2
                        M569 P3 S0                                                       	; Physical drive 3 . Main Extruder
                        M569 P4 S0                                                       	; Physical drive 4 . Secondary Extruder									
                        ;Duex5 board_____________________________________________________________________
                        M569 P5 S0                                                       	; Physical drive 5 . Y
                        M569 P6 S0                                                       	; Physical drive 6 . Z1 (-188 , 656.5) 
                        M569 P7 S0                                                       	; Physical drive 7 . Z2 (-188, -35.5) 
                        M569 P8 S0                                                       	; Physical drive 8 . Z3 (658.6 , -35.5) 
                        M569 P9 S0                                                       	; Physical drive 9 . Z4 (658.6, 656.5) 
                        
                        ;Settings_________________________________________________________
                        M584 X0:1 Y5 Z6:7:8:9  E3:4 P3								   	    ; Driver mapping                                                 
                        
                        
                        ;___________________________________________________________________
                        M350 X16 Y16 I1  		                            				; Configure microstepping with interpolation                     
                        M350 Z16 E16:16 I0              		                			; Configure microstepping without interpolation
                        
                        M92 X100.00 Y100.00 Z2000.00 E425:300       				        ; Set steps per mm                                                
                        
                        M566 X300 Y500 Z100.00 E120.00:120.00  P1               		    ; Set maximum instantaneous speed changes (mm/min)                
                        M203 X18000.00 Y18000.00 Z300.00 E1200.00:1200.00           		; Set maximum speeds (mm/min)                                     
                        M201 X1000 Y1000 Z120.00 E250.00:250.00                  			; Set accelerations (mm/s^2)                                      
                        M204 P500                                     			            ; Set print and travel accelerations  (mm/s^2)
                        M906 X1800 Y1800.00 E1000:1000  I40 					        	; Set motor currents (mA) and motor idle factor in per cent (E1270 per dyze)   
                        M906 Z1800.00 I50 													; Set motor currents (mA) and motor idle factor in per cent
                        M84 S100                                          					; Set idle timeout - 100 seconds
                        
                        ; Axis Limits
                        
                        M208 X0 Y0 Z-0.5 S1                               			 	    ; set axis minima
                        M208 X585 Y575 Z630 S0                          					; set axis maxima 580;580
                        
                        ; Endstops
                        
                        M574 X1 S1 P"xstop + e0stop"                            	; configure switch-type (e.g. microswitch) endstop for low end on X via pin xstop
                        M574 Y2 S1 P"ystop"                            				; configure switch-type (e.g. microswitch) endstop for low end on Y via pin ystop
                        
                        
                        ; Z-Probe
                        
                        
                        ;M558 P9 C"^zprobe.in" H5 F120 T6000 A1 R1  				; set Z probe type to bltouch and the dive height + speeds
                        ;M950 S0 C"duex.pwm5"										; set probe pin
                        M98 P"config_probe.g"
                        M556 S50 X0 Y0 Z0		                               		; set orthogonal axis compensation parameters woher kommt der test wie wurde der Winkel bestimmt Unklar!
                        M376 H20													; stop z-leveling after 10 layers
                        
                        ; Heaters___________________________________________________________
                        M140 H-1                                       				; disable heated bed (overrides default heater mapping)
                        
                        
                        ;E0_________________________________________________________________
                        M308 S0 P"spi.cs1" Y"rtd-max31865" A"Main Extruder"         ; create sensor number 1 as a PT100 sensor in first position daughterboard 
                        M950 H0 C"e0heat"   T0                       		        ; create nozzle heater output on e0heat and map it to sensor 0
                        M307 H0 B0 R2.059 C461.5:461.5 D8.35 S1.00 V23.5            ; PID calibration
                        ;M307 H0 B0 R6.167 C268.6:268.6 D4.07 S1.00 V23.5
                        M143 H0 S1400                                    			; set temperature limit for heater 0 to 450C
                        
                        ;E1_________________________________________________________________
                        M308 S1 P"spi.cs2" Y"rtd-max31865" A"Support Extruder"    	; create sensor number 2 as a PT100 sensor in sec position daughterboard 
                        
                        
                        ;E4_________________________________________________________________
                        M308 S1 P"duex.e4temp" Y"thermistor" T100000 B4267   		; configure sensor 1 as thermistor on pin e1temp
                        M950 H5 C"duex.e4heat" T1                            		; create nozzle heater output on e4heat and map it to sensor 4											
                        M143 H5 S120                                  			    ; set temperature limit for heater 1 to 120C
                        
                        ; Fans & LED___________________________________________________________
                        M950 F0 C"fan0" Q500                            			; create fan 0 on pin fan0 and set its frequency
                        M106 P0 S0 H-1                                  			; set fan 0 value. Thermostatic control is turned on
                        
                        M950 F1 C"fan1" Q500                            			; create fan 1 on pin fan1 and set its frequency
                        M106 P1 S0 H-1                                  			; set fan 1 value. Thermostatic control is turned on
                        
                        M950 F2 C"fan2" Q500                            			; create air filter fan on fan 2 on pin fan2 and set its frequency
                        M106 P2 S0 H-1                                  			; set fan 2 value. Thermostatic control is turned on
                        
                        M950 F7 C"!duex.fan7" Q500                            		; create LED on pin fan7 and set its frequency
                        M106 P7 S0 H-1                               				; Disable fan channel for LED
                        M106 P7 S255							                    ; remove ";" to set the LED to full brightness by default
                        
                        M950 F3 C"duex.fan3" Q500                       			; create fan 3 on pin fan3 and set its frequency
                        M106 P3 S1 H-1                           					; set fan 3 value. Thermostatic control is turned on Bed relay to on
                        
                        ; Tools______________________________________________________________
                        
                        ;T0_________________________________________________________________
                        M563 P0 S"E0 Main" D0 H0 F0                  				; define tool 0
                        G10 P0 X0 Y0 Z0                                 			; set tool 0 axis offsets
                        G10 P0 R0 S265                                  			; set initial tool 0 active and standby temperatures to 0C
                        
                        ;T1_________________________________________________________________
                        M563 P1 S"E1 Support" D1 H1 F1                				; define tool 1
                        G10 P1 X0 Y65 Z0                                			; set tool 1 axis offsets  Y-2 moves filament 2mm to back of machine     X-1 moves filament 1mm to the right
                        G10 P1 R0 S265                                    			; set initial tool 1 active and standby temperatures to 0C
                        
                        ;T2____________________________________________________________________
                        
                        ;T3___________________________________________________________________
                        M563 P3 S"CHAMBER TEMP" H5
                        G10 P3 R0 S40
                        
                        ; Custom settings__________________________________________________
                        M950 J0 C"exp.e2stop" 
                        M581 T1 P0 S0 R1 
                        M591 D0 P7 C"e1stop" S1 L4.2 E10 R10:1000
                        
                        M950 J1 C"exp.e3stop" 
                        M581 T1 P1 S0 R1 
                        M591 D1 P7 C"zstop" S1 L4.2 E10 R10:1000
                        ;M591 D0 P1 C"duex.e2stop" S1								; Regular filament sensor for E0
                        ;M591 D1 P1 C"duex.e3stop" S1								; Regular filament sensor for E1
                        
                        M950 J2 C"duex.e4stop"                                      ; create Input Pin 2 on Zstop for the M581 command.
                        M581 P2 T0 S0 R0                                            ; Crash Detector  [Add-On]
                        
                        M42 P2 S255 												; Start up air filter 
                        
                        ; Automatic power saving____________________________________________
                        M911 S21 R29.0 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000"              ; Set voltage thresholds and actions to run on power loss. Power Failure Pause
                        
                        jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                        • jay_s_ukundefined
                          jay_s_uk @Sculpt Fabricator
                          last edited by

                          @sculpt-fabricator also, does it reset if you simulate the job?

                          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                          Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 0
                          • jay_s_ukundefined
                            jay_s_uk @Sculpt Fabricator
                            last edited by

                            @sculpt-fabricator and have you always used global variables or have you only recently started to use them?

                            Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                            Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 0
                            • Sculpt Fabricatorundefined
                              Sculpt Fabricator @jay_s_uk
                              last edited by

                              @jay_s_uk I have never run a job simulate. I don't know how to do that ?

                              jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                              • jay_s_ukundefined
                                jay_s_uk @Sculpt Fabricator
                                last edited by

                                @sculpt-fabricator right click on the job and simulate

                                Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 0
                                • Sculpt Fabricatorundefined
                                  Sculpt Fabricator @jay_s_uk
                                  last edited by

                                  @jay_s_uk

                                  I haven't changed any g-code or any setting in 4 months, printer was working
                                  perfectly sense 3.3 update and getting all the code dialed in. Machine has been
                                  running 24/7 for 4 weeks

                                  1 Reply Last reply Reply Quote 0
                                  • Sculpt Fabricatorundefined
                                    Sculpt Fabricator @jay_s_uk
                                    last edited by

                                    @jay_s_uk
                                    It made it 100% thought simulation.

                                    jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                                    • jay_s_ukundefined
                                      jay_s_uk @Sculpt Fabricator
                                      last edited by

                                      @sculpt-fabricator not much we can do now until the reset map is looked at.

                                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                      1 Reply Last reply Reply Quote 0
                                      • droftartsundefined
                                        droftarts administrators @Sculpt Fabricator
                                        last edited by

                                        @sculpt-fabricator said in Automatic Emergency Stop:

                                        Error status: 0x04

                                        Error 0x04 = Output buffer starvation, I think. I'd guess that your SD card is either full or damaged. Please check your SD card by running the commands here: https://docs.duet3d.com/en/User_manual/RepRapFirmware/SD_card#troubleshooting-sd-card-issues

                                        Ian

                                        Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                        Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 1
                                        • Sculpt Fabricatorundefined
                                          Sculpt Fabricator @droftarts
                                          last edited by

                                          @droftarts
                                          The SD card was really full we deleted everything out of it. I will look into
                                          that more

                                          1 Reply Last reply Reply Quote 1
                                          • droftartsundefined
                                            droftarts administrators
                                            last edited by

                                            @sculpt-fabricator probably file fragmentation on the SD card slowing down read time, then.

                                            Ian

                                            Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                            Sculpt Fabricatorundefined 1 Reply Last reply Reply Quote 0
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