Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    RRF can't "see" any of the stepper drivers, over night.

    Scheduled Pinned Locked Moved
    General Discussion
    5
    28
    1.2k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • Exerqtorundefined
      Exerqtor @Phaedrux
      last edited by Exerqtor

      @Phaedrux Yeah i can, and it's the same exact behaviour.

      So it can only see the drivers if not powered by VIN.

      Regarding how it's mounted, it's mounted with the stock Voron board mounts and click-on DIN rail mounts. Both printed in ABS, with ABS washers between the PCB and screws on the front side.

      Nothing shorting it while inside the printer either.

      When i had the board out of the machine it was still screwed on to the mounts, so twisting/pressure ain't the issue.

      Phaedruxundefined 1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator @Exerqtor
        last edited by Phaedrux

        @Exerqtor said in RRF can't "see" any of the stepper drivers, over night.:

        So it can only see the drivers if not powered by VIN.

        Can it see (and move) the drivers if powered by vin and usb at the same time? Be careful with USB ground loops.

        Z-Bot CoreXY Build | Thingiverse Profile

        Exerqtorundefined 2 Replies Last reply Reply Quote 0
        • Exerqtorundefined
          Exerqtor @Phaedrux
          last edited by

          @Phaedrux i haven't tried that since i thought that was a big no-no 🤣 i can try it this afternoon. What precautions should i take in regard to USB ground loops?

          gloomyandyundefined 1 Reply Last reply Reply Quote 0
          • gloomyandyundefined
            gloomyandy @Exerqtor
            last edited by

            @Exerqtor See https://docs.duet3d.com/User_manual/Overview/USB_ground_loops

            Exerqtorundefined 1 Reply Last reply Reply Quote 1
            • Exerqtorundefined
              Exerqtor @gloomyandy
              last edited by

              @gloomyandy said in RRF can't "see" any of the stepper drivers, over night.:

              @Exerqtor See https://docs.duet3d.com/User_manual/Overview/USB_ground_loops

              Of course it's covered in the docs, the "one" place i didn't look 🤦‍♂️

              Ok so running the usb to a laptop running on battery sounds like the safest and easiest way to go. I'll do that later and report how it turns out.

              1 Reply Last reply Reply Quote 0
              • Exerqtorundefined
                Exerqtor @Phaedrux
                last edited by

                @Phaedrux said in RRF can't "see" any of the stepper drivers, over night.:

                @Exerqtor said in RRF can't "see" any of the stepper drivers, over night.:

                So it can only see the drivers if not powered by VIN.

                Can it see (and move) the drivers if powered by vin and usb at the same time? Be careful with USB ground loops.

                I just hooked up both VIN & powered it from USB via a laptop running on the battery. No drivers visible.

                M122
                === Diagnostics ===
                RepRapFirmware for Duet 3 Mini 5+ version 3.5.0-beta.4 (2023-06-08 23:40:14) running on Duet 3 Mini5plus WiFi (standalone mode)
                Board ID: DXGUZ-U196U-D65J0-40KMN-1Y03Z-RKST9
                Used output buffers: 10 of 40 (24 max)
                === RTOS ===
                Static ram: 102996
                Dynamic ram: 124276 of which 16 recycled
                Never used RAM 11912, free system stack 156 words
                Tasks: NETWORK(2,nWait,17.1%,215) HEAT(3,nWait,0.0%,352) Move(4,nWait,0.0%,358) CanReceiv(6,nWait,0.0%,672) CanSender(5,nWait,0.0%,337) CanClock(7,delaying,0.0%,351) TMC(4,nWait,0.3%,110) MAIN(1,running,81.5%,704) IDLE(0,ready,0.2%,29) AIN(4,delaying,0.8%,266), total 100.0%
                Owned mutexes:
                === Platform ===
                Last reset 00:02:32 ago, cause: software
                Last software reset at 2023-08-24 17:31, reason: User, Gcodes spinning, available RAM 12404, slot 0
                Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                Error status: 0x00
                Aux0 errors 0,0,0
                MCU revision 3, ADC conversions started 152189, completed 152189, timed out 0, errs 0
                MCU temperature: min 24.4, current 27.0, max 27.0
                Supply voltage: min 24.0, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                Heap OK, handles allocated/used 99/29, heap memory allocated/used/recyclable 2048/588/192, gc cycles 2
                Events: 0 queued, 0 completed
                Driver 0: not present
                Driver 1: not present
                Driver 2: not present
                Driver 3: not present
                Driver 4: not present
                Driver 5: not present
                Driver 6: not present
                Date/time: 2023-08-24 17:34:05
                Cache data hit count 252956637
                Slowest loop: 11.79ms; fastest: 0.14ms
                === Storage ===
                Free file entries: 18
                SD card 0 detected, interface speed: 22.5MBytes/sec
                SD card longest read time 4.5ms, write time 4.4ms, max retries 0
                === Move ===
                DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, height map offset 0.000, ebfmin 0.00, ebfmax 0.00
                no step interrupt scheduled
                === DDARing 0 ===
                Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                === DDARing 1 ===
                Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                === Heat ===
                Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                Heater 1 is on, I-accum = 0.0
                === GCodes ===
                Movement locks held by null, null
                HTTP is idle in state(s) 0
                Telnet is idle in state(s) 0
                File is idle in state(s) 0
                USB is idle in state(s) 0
                Aux is idle in state(s) 0
                Trigger is idle in state(s) 0
                Queue is idle in state(s) 0
                LCD is idle in state(s) 0
                SBC is idle in state(s) 0
                Daemon is doing "G4 S1                                                                        " in state(s) 0 0, running macro
                Aux2 is idle in state(s) 0
                Autopause is idle in state(s) 0
                File2 is idle in state(s) 0
                Queue2 is idle in state(s) 0
                Q0 segments left 0, axes/extruders owned 0x0000803
                Code queue 0 is empty
                Q1 segments left 0, axes/extruders owned 0x0000000
                Code queue 1 is empty
                === Filament sensors ===
                Extruder 0 sensor: no filament
                === CAN ===
                Messages queued 1145, received 2609, lost 0, boc 0
                Longest wait 0ms for reply type 0, peak Tx sync delay 6, free buffers 18 (min 18), ts 636/636/0
                Tx timeouts 0,0,0,0,0,0
                === Network ===
                Slowest loop: 25.23ms; fastest: 0.06ms
                Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
                HTTP sessions: 1 of 8
                = WiFi =
                Interface state: active
                Module is connected to access point 
                Failed messages: pending 0, notready 0, noresp 0
                Firmware version 2.1beta4
                MAC address d8:bf:c0:14:e6:36
                Module reset reason: Power up, Vcc 3.31, flash size 2097152, free heap 43132
                WiFi IP address 192.168.10.50
                Signal strength -49dBm, channel 1, mode 802.11n, reconnections 0
                Clock register 00002001
                Socket states: 0 0 0 0 0 0 0 0
                
                1 Reply Last reply Reply Quote 0
                • Phaedruxundefined
                  Phaedrux Moderator
                  last edited by

                  Quite strange. When and where was the board purchased?

                  Z-Bot CoreXY Build | Thingiverse Profile

                  Exerqtorundefined 1 Reply Last reply Reply Quote 0
                  • Exerqtorundefined
                    Exerqtor @Phaedrux
                    last edited by Exerqtor

                    @Phaedrux Yeah it's pretty weird, especially since it worked perfectly one evening, then this just happens while standing idle over night.

                    I just bought the board second hand from a dude here in Norway. He purchased the board from E3D in november 2022 (i have a printout of the order confirmation mail he got, with order number).

                    1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Please send an email to warranty@duet3d.com and CC your reseller. Include a link to this forum thread and the details of your original purchase. You'll receive a reply with a form to fill out.

                      Z-Bot CoreXY Build | Thingiverse Profile

                      Exerqtorundefined 1 Reply Last reply Reply Quote 1
                      • Exerqtorundefined
                        Exerqtor @Phaedrux
                        last edited by

                        Thanks @Phaedrux, mail sent ✌

                        1 Reply Last reply Reply Quote 0
                        • jonasr75undefined
                          jonasr75
                          last edited by

                          @Exerqtor said in RRF can't "see" any of the stepper drivers, over night.:

                          G1: G0/G1: insufficient axes homed

                          I follow the topic.
                          I have a similar problem, but not quite this one. I also get the following error message: "G1: G0/G1: insufficient axes homed". Could this not be an endstop problem? I have a DueX5 extension board as I drive 3 pcs Z nema17 stepper motors. However, on the DueX5 board, I see a small "crater" on the first chip of the TMC2660 stepper. Could this chip be broken and cause the homing process to fail? I haven't run the M122 command yet.

                          Phaedruxundefined 1 Reply Last reply Reply Quote 0
                          • Phaedruxundefined
                            Phaedrux Moderator @jonasr75
                            last edited by

                            @jonasr75 Best to start a new thread. Provide all the details including your config.g and a photo of your driver.

                            Z-Bot CoreXY Build | Thingiverse Profile

                            jonasr75undefined 1 Reply Last reply Reply Quote 1
                            • jonasr75undefined
                              jonasr75 @Phaedrux
                              last edited by

                              @Phaedrux ok, i have started a new thread:
                              https://forum.duet3d.com/topic/33921/homing-error-in-x-y-axes

                              1 Reply Last reply Reply Quote 0
                              • Exerqtorundefined Exerqtor referenced this topic
                              • First post
                                Last post
                              Unless otherwise noted, all forum content is licensed under CC-BY-SA