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    RRF can't "see" any of the stepper drivers, over night.

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    • Phaedruxundefined
      Phaedrux Moderator @Exerqtor
      last edited by Phaedrux

      @Exerqtor said in RRF can't "see" any of the stepper drivers, over night.:

      So it can only see the drivers if not powered by VIN.

      Can it see (and move) the drivers if powered by vin and usb at the same time? Be careful with USB ground loops.

      Z-Bot CoreXY Build | Thingiverse Profile

      Exerqtorundefined 2 Replies Last reply Reply Quote 0
      • Exerqtorundefined
        Exerqtor @Phaedrux
        last edited by

        @Phaedrux i haven't tried that since i thought that was a big no-no 🤣 i can try it this afternoon. What precautions should i take in regard to USB ground loops?

        gloomyandyundefined 1 Reply Last reply Reply Quote 0
        • gloomyandyundefined
          gloomyandy @Exerqtor
          last edited by

          @Exerqtor See https://docs.duet3d.com/User_manual/Overview/USB_ground_loops

          Exerqtorundefined 1 Reply Last reply Reply Quote 1
          • Exerqtorundefined
            Exerqtor @gloomyandy
            last edited by

            @gloomyandy said in RRF can't "see" any of the stepper drivers, over night.:

            @Exerqtor See https://docs.duet3d.com/User_manual/Overview/USB_ground_loops

            Of course it's covered in the docs, the "one" place i didn't look 🤦‍♂️

            Ok so running the usb to a laptop running on battery sounds like the safest and easiest way to go. I'll do that later and report how it turns out.

            1 Reply Last reply Reply Quote 0
            • Exerqtorundefined
              Exerqtor @Phaedrux
              last edited by

              @Phaedrux said in RRF can't "see" any of the stepper drivers, over night.:

              @Exerqtor said in RRF can't "see" any of the stepper drivers, over night.:

              So it can only see the drivers if not powered by VIN.

              Can it see (and move) the drivers if powered by vin and usb at the same time? Be careful with USB ground loops.

              I just hooked up both VIN & powered it from USB via a laptop running on the battery. No drivers visible.

              M122
              === Diagnostics ===
              RepRapFirmware for Duet 3 Mini 5+ version 3.5.0-beta.4 (2023-06-08 23:40:14) running on Duet 3 Mini5plus WiFi (standalone mode)
              Board ID: DXGUZ-U196U-D65J0-40KMN-1Y03Z-RKST9
              Used output buffers: 10 of 40 (24 max)
              === RTOS ===
              Static ram: 102996
              Dynamic ram: 124276 of which 16 recycled
              Never used RAM 11912, free system stack 156 words
              Tasks: NETWORK(2,nWait,17.1%,215) HEAT(3,nWait,0.0%,352) Move(4,nWait,0.0%,358) CanReceiv(6,nWait,0.0%,672) CanSender(5,nWait,0.0%,337) CanClock(7,delaying,0.0%,351) TMC(4,nWait,0.3%,110) MAIN(1,running,81.5%,704) IDLE(0,ready,0.2%,29) AIN(4,delaying,0.8%,266), total 100.0%
              Owned mutexes:
              === Platform ===
              Last reset 00:02:32 ago, cause: software
              Last software reset at 2023-08-24 17:31, reason: User, Gcodes spinning, available RAM 12404, slot 0
              Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
              Error status: 0x00
              Aux0 errors 0,0,0
              MCU revision 3, ADC conversions started 152189, completed 152189, timed out 0, errs 0
              MCU temperature: min 24.4, current 27.0, max 27.0
              Supply voltage: min 24.0, current 24.1, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
              Heap OK, handles allocated/used 99/29, heap memory allocated/used/recyclable 2048/588/192, gc cycles 2
              Events: 0 queued, 0 completed
              Driver 0: not present
              Driver 1: not present
              Driver 2: not present
              Driver 3: not present
              Driver 4: not present
              Driver 5: not present
              Driver 6: not present
              Date/time: 2023-08-24 17:34:05
              Cache data hit count 252956637
              Slowest loop: 11.79ms; fastest: 0.14ms
              === Storage ===
              Free file entries: 18
              SD card 0 detected, interface speed: 22.5MBytes/sec
              SD card longest read time 4.5ms, write time 4.4ms, max retries 0
              === Move ===
              DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, height map offset 0.000, ebfmin 0.00, ebfmax 0.00
              no step interrupt scheduled
              === DDARing 0 ===
              Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === DDARing 1 ===
              Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === Heat ===
              Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
              Heater 1 is on, I-accum = 0.0
              === GCodes ===
              Movement locks held by null, null
              HTTP is idle in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon is doing "G4 S1                                                                        " in state(s) 0 0, running macro
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              File2 is idle in state(s) 0
              Queue2 is idle in state(s) 0
              Q0 segments left 0, axes/extruders owned 0x0000803
              Code queue 0 is empty
              Q1 segments left 0, axes/extruders owned 0x0000000
              Code queue 1 is empty
              === Filament sensors ===
              Extruder 0 sensor: no filament
              === CAN ===
              Messages queued 1145, received 2609, lost 0, boc 0
              Longest wait 0ms for reply type 0, peak Tx sync delay 6, free buffers 18 (min 18), ts 636/636/0
              Tx timeouts 0,0,0,0,0,0
              === Network ===
              Slowest loop: 25.23ms; fastest: 0.06ms
              Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
              HTTP sessions: 1 of 8
              = WiFi =
              Interface state: active
              Module is connected to access point 
              Failed messages: pending 0, notready 0, noresp 0
              Firmware version 2.1beta4
              MAC address d8:bf:c0:14:e6:36
              Module reset reason: Power up, Vcc 3.31, flash size 2097152, free heap 43132
              WiFi IP address 192.168.10.50
              Signal strength -49dBm, channel 1, mode 802.11n, reconnections 0
              Clock register 00002001
              Socket states: 0 0 0 0 0 0 0 0
              
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              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                Quite strange. When and where was the board purchased?

                Z-Bot CoreXY Build | Thingiverse Profile

                Exerqtorundefined 1 Reply Last reply Reply Quote 0
                • Exerqtorundefined
                  Exerqtor @Phaedrux
                  last edited by Exerqtor

                  @Phaedrux Yeah it's pretty weird, especially since it worked perfectly one evening, then this just happens while standing idle over night.

                  I just bought the board second hand from a dude here in Norway. He purchased the board from E3D in november 2022 (i have a printout of the order confirmation mail he got, with order number).

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                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    Please send an email to warranty@duet3d.com and CC your reseller. Include a link to this forum thread and the details of your original purchase. You'll receive a reply with a form to fill out.

                    Z-Bot CoreXY Build | Thingiverse Profile

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                    • Exerqtorundefined
                      Exerqtor @Phaedrux
                      last edited by

                      Thanks @Phaedrux, mail sent ✌

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                      • jonasr75undefined
                        jonasr75
                        last edited by

                        @Exerqtor said in RRF can't "see" any of the stepper drivers, over night.:

                        G1: G0/G1: insufficient axes homed

                        I follow the topic.
                        I have a similar problem, but not quite this one. I also get the following error message: "G1: G0/G1: insufficient axes homed". Could this not be an endstop problem? I have a DueX5 extension board as I drive 3 pcs Z nema17 stepper motors. However, on the DueX5 board, I see a small "crater" on the first chip of the TMC2660 stepper. Could this chip be broken and cause the homing process to fail? I haven't run the M122 command yet.

                        Phaedruxundefined 1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator @jonasr75
                          last edited by

                          @jonasr75 Best to start a new thread. Provide all the details including your config.g and a photo of your driver.

                          Z-Bot CoreXY Build | Thingiverse Profile

                          jonasr75undefined 1 Reply Last reply Reply Quote 1
                          • jonasr75undefined
                            jonasr75 @Phaedrux
                            last edited by

                            @Phaedrux ok, i have started a new thread:
                            https://forum.duet3d.com/topic/33921/homing-error-in-x-y-axes

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