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    Duet 2Wifi Board: 3 Z-Axis configuration create problem

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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      Please share your config.g and homing files as well as the output of sending M122 and M98 P"config.g" in the gcode console.

      Can you provide a photo of your wiring setup?

      Z-Bot CoreXY Build | Thingiverse Profile

      R006undefined Phaedruxundefined 2 Replies Last reply Reply Quote 0
      • R006undefined
        R006 @Phaedrux
        last edited by R006

        @Phaedrux

        Can you provide a photo of your wiring setup?
        Actually we have set table top setup for testing purpose.
        We have connect motor to board and display only.
        and still we get noise in Y axis motor.

        config

        M569 P0 S1                                           
        M569 P1 S1                                           
        M569 P2 S1                                           
        M569 P3 S1 
        M569 P4 S1 
        M569 P5 S1   
        M584 X0 Y1 Z2:3:4 E5                                    
        M350 X16 Y16 I0                                        
        M350 Z16 E16 I1                                      
        M92 X80.00 Y80.00 Z2133.33 E932.00                   
        M566 X600.00 Y600.00 Z300.00 E600.00                       
        M203 X8400.00 Y8400.00 Z1800.00 E6000.00          
        M201 X2500.00 Y2500.00 Z30.00 E250.00                
        M906 X2000 Y2000 Z1800 E800 I30                      
        M84 S30      
            
           ; Endstops
        M574 X1 S1 P"xstop"                                 
        M574 Y1 S1 P"ystop"                                
        M574 Z1 S1 P"zstop+e0_stop+e1_stop"         
        
        ; Bed Heater
        M308 S0 P"bedtemp" Y"thermistor" T100000 B4138       
        M950 H0 C"bedheat" T0                                
        M307 H0 B0 S1.00                                     
        M140 H0                                             
        M143 H0 S105                                         
        
        ; Extuder Heater
        M308 S1 P"e0temp" Y"pt1000"                          
        M950 H1 C"e0heat" T1                                 
        M307 H1 B0 S1.00                                      
        M143 H1 S320     
        

        homeall

        G91                  
        G1 H2 Z5 F6000       
        G1 H1 X-305 Y-305 F1800
        G1 H2 X5 Y5 F6000  
        G1 H1 X-305 Y-305 F600  
        G1 H1 Z305 F500
        G1 H2 Z-5 F500         
        G1 H1 Z305 F500 
        G90                   
        G92 Z300 
        

        homex

        G91              ; relative positioning
        G1 H2 Z5 F6000   ; lift Z relative to current position
        G1 H1 X-305 F1800 ; move quickly to X axis endstop and stop there (first pass)
        G1 H2 X5 F6000  ; go back a few mm
        G1 H1 X-305 F360  ; move slowly to X axis endstop once more (second pass)
        G1 H2 Z-5 F6000  ; lower Z again
        G90
        

        homey

        G91              ; relative positioning
        G1 H2 Z5 F6000   ; lift Z relative to current position
        G1 H1 Y-305 F1800 ; move quickly to Y axis endstop and stop there (first pass)
        G1 H2 Y5 F6000  ; go back a few mm
        G1 H1 Y-305 F360  ; move slowly to Y axis endstop once more (second pass)
        G1 H2 Z-5 F6000  ; lower Z again
        G90    
        

        homez

        G91              ; relative positioning
        G1 H2 Z5 F500   ; lift Z relative to current position
        G1 H1 Z305 F500 ; move Z up until the endstop is triggered
        G1 H2 Z-5 F500
        G1 H1 Z305 F500
        G90
        G92 Z305        ; set Z position to axis maximum (you may want to adjust this)
        
        
        T3P3Tonyundefined 1 Reply Last reply Reply Quote 0
        • Phaedruxundefined
          Phaedrux Moderator @Phaedrux
          last edited by

          @Phaedrux said in Duet 2Wifi Board: 3 Z-Axis configuration create problem:

          as well as the output of sending M122 and M98 P"config.g" in the gcode console.

          Z-Bot CoreXY Build | Thingiverse Profile

          R006undefined 1 Reply Last reply Reply Quote 0
          • T3P3Tonyundefined
            T3P3Tony administrators @R006
            last edited by

            @R006 are you using a Duex5?

            www.duet3d.com

            R006undefined 1 Reply Last reply Reply Quote 0
            • R006undefined
              R006 @T3P3Tony
              last edited by

              @T3P3Tony no

              T3P3Tonyundefined 1 Reply Last reply Reply Quote 0
              • R006undefined
                R006 @Phaedrux
                last edited by

                @Phaedrux
                M112

                2024-02-21 10:04:42 [debug] RepRapFirmware for Duet 2 WiFi/Ethernet MOD. By STPL version 3.4.0beta3 (2023-08-17 14:30:25) running on Duet WiFi 1.02 or later
                2024-02-21 10:04:42 [debug] Board ID: 08DLM-996RU-N8PS0-6J9F8-3SN6M-KVVMR
                2024-02-21 10:04:42 [debug] Used output buffers: 3 of 24 (24 max)
                2024-02-21 10:04:42 [debug] === RTOS ===
                2024-02-21 10:04:42 [debug] Static ram: 23940
                2024-02-21 10:04:42 [debug] Dynamic ram: 75676 of which 0 recycled
                2024-02-21 10:04:42 [debug] Never used RAM 9248, free system stack 100 words
                2024-02-21 10:04:42 [debug] Tasks:
                2024-02-21 10:04:42 [debug]  NETWORK(ready,14.0%,199)
                2024-02-21 10:04:42 [debug]  HEAT(notifyWait,0.0%,140)
                2024-02-21 10:04:42 [debug]  Move(notifyWait,1.0%,297)
                2024-02-21 10:04:42 [debug]  MAIN(running,84.9%,317)
                2024-02-21 10:04:42 [debug]  IDLE(ready,0.0%,29)
                2024-02-21 10:04:42 [debug] , total 100.0%
                Owned mutexes:
                2024-02-21 10:04:42 [debug]  Aux(MAIN)
                2024-02-21 10:04:42 [debug] === Platform ===
                2024-02-21 10:04:42 [debug] Last reset 22:16:10 ago, cause: power up
                2024-02-21 10:04:42 [debug] Last software reset time unknown, reason: User, GCodes spinning, available RAM 11928, slot 1
                2024-02-21 10:04:42 [debug] Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                2024-02-21 10:04:42 [debug] Error status: 0x0c
                2024-02-21 10:04:42 [debug] Aux0 errors 0,0,0
                2024-02-21 10:04:42 [debug] Step timer max interval 0
                2024-02-21 10:04:42 [debug] MCU temperature: min 30.0, current 30.3, max 30.7
                2024-02-21 10:04:42 [debug] Supply voltage: min 23.8, current 24.3, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                2024-02-21 10:04:42 [debug] Heap OK, handles allocated/used 99/1, heap memory allocated/used/recyclable 2048/14/0, gc cycles 0
                2024-02-21 10:04:42 [debug] Driver 0: position 42246, ok, SG min/max not available
                2024-02-21 10:04:42 [debug] Driver 1: position 38649, ok, SG min/max not available
                2024-02-21 10:04:42 [debug] Driver 2: position 14123, standstill, SG min/max not available
                2024-02-21 10:04:42 [debug] Driver 3: position 0, standstill, SG min/max not available
                2024-02-21 10:04:42 [debug] Driver 4: position 0, standstill, SG min/max not available
                2024-02-21 10:04:42 [debug] Driver 5: position 0
                2024-02-21 10:04:42 [debug] Driver 6: position 0
                2024-02-21 10:04:42 [debug] Driver 7: position 0
                2024-02-21 10:04:42 [debug] Driver 8: position 0
                2024-02-21 10:04:42 [debug] Driver 9: position 0
                2024-02-21 10:04:42 [debug] Driver 10: position 0
                2024-02-21 10:04:42 [debug] Driver 11: position 0
                2024-02-21 10:04:42 [debug] Date/time: 
                2024-02-21 10:04:42 [debug] 2024-02-21 10:04:42
                2024-02-21 10:04:42 [debug] Cache data hit count 4294967295
                2024-02-21 10:04:42 [debug] Slowest loop: 8.19ms; fastest: 0.18ms
                2024-02-21 10:04:42 [debug] I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                2024-02-21 10:04:42 [debug] === Storage ===
                Free file entries: 8
                2024-02-21 10:04:42 [debug] SD card 0 detected, interface speed: 20.0MBytes/sec
                2024-02-21 10:04:42 [debug] SD card longest read time 2.0ms, write time 1.0ms, max retries 0
                2024-02-21 10:04:42 [debug] === Move ===
                DMs created 83, segments created 15, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                2024-02-21 10:04:42 [debug] === MainDDARing ===
                Scheduled moves 14329, completed moves 14324, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state 3
                2024-02-21 10:04:42 [debug] === AuxDDARing ===
                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                2024-02-21 10:04:42 [debug] === Heat ===
                Bed heaters =
                2024-02-21 10:04:42 [debug]  0
                2024-02-21 10:04:42 [debug]  -1
                2024-02-21 10:04:42 [debug]  -1
                2024-02-21 10:04:42 [debug]  -1
                2024-02-21 10:04:42 [debug] , chamberHeaters =
                2024-02-21 10:04:42 [debug]  -1
                2024-02-21 10:04:42 [debug]  -1
                2024-02-21 10:04:42 [debug]  -1
                2024-02-21 10:04:42 [debug]  -1
                2024-02-21 10:04:42 [debug] Heater 0 is on, I-accum = 0.2
                2024-02-21 10:04:42 [debug] Heater 1 is on, I-accum = 0.4
                2024-02-21 10:04:42 [debug] === GCodes ===
                2024-02-21 10:04:42 [debug] Segments left: 1
                2024-02-21 10:04:42 [debug] Movement lock held by null
                2024-02-21 10:04:42 [debug] HTTP is idle in state(s) 0
                2024-02-21 10:04:42 [debug] Telnet is idle in state(s) 0
                2024-02-21 10:04:42 [debug] File is doing "G1 X264.039 Y247.89 E1.1394" in state(s) 0
                2024-02-21 10:04:42 [debug] USB is idle in state(s) 0
                2024-02-21 10:04:42 [debug] Aux is ready with "M122" in state(s) 0
                2024-02-21 10:04:42 [debug] Trigger is idle in state(s) 0
                2024-02-21 10:04:42 [debug] Queue is idle in state(s) 0
                2024-02-21 10:04:42 [debug] LCD is idle in state(s) 0
                2024-02-21 10:04:42 [debug] Daemon is idle in state(s) 0
                2024-02-21 10:04:42 [debug] Autopause is idle in state(s) 0
                2024-02-21 10:04:42 [debug] Code queue is empty
                2024-02-21 10:04:42 [debug] === Filament sensors ===
                2024-02-21 10:04:42 [debug] Extruder 0 sensor: ok
                2024-02-21 10:04:42 [debug] === Network ===
                2024-02-21 10:04:42 [debug] Slowest loop: 201.09ms; fastest: 0.07ms
                2024-02-21 10:04:42 [debug] Responder states:
                2024-02-21 10:04:42 [debug]  HTTP(0)
                2024-02-21 10:04:42 [debug]  HTTP(0)
                2024-02-21 10:04:42 [debug]  HTTP(0)
                2024-02-21 10:04:42 [debug]  HTTP(0)
                2024-02-21 10:04:42 [debug]  FTP(0)
                2024-02-21 10:04:42 [debug]  Telnet(0), 0 sessions
                2024-02-21 10:04:42 [debug] HTTP sessions: 1 of 8
                2024-02-21 10:04:42 [debug] - WiFi -
                Network state is active
                2024-02-21 10:04:42 [debug] WiFi module is connected to access point 
                2024-02-21 10:04:42 [debug] Failed messages: pending 0, notready 0, noresp 1
                2024-02-21 10:04:42 [debug] WiFi firmware version 1.27
                2024-02-21 10:04:42 [debug] WiFi MAC address 48:3f:da:a6:ee:20
                2024-02-21 10:04:42 [debug] WiFi Vcc 3.42, reset reason Power up
                2024-02-21 10:04:42 [debug] WiFi flash size 2097152, free heap 26032
                2024-02-21 10:04:42 [debug] WiFi IP address 192.168.0.101
                2024-02-21 10:04:42 [debug] WiFi signal strength -69dBm, mode 802.11n, reconnections 0, sleep mode modem
                2024-02-21 10:04:42 [debug] Clock register 00002002
                2024-02-21 10:04:42 [debug] Socket states:
                2024-02-21 10:04:42 [debug]  0
                2024-02-21 10:04:42 [debug]  0
                2024-02-21 10:04:42 [debug]  0
                2024-02-21 10:04:42 [debug]  0
                2024-02-21 10:04:42 [debug]  0
                2024-02-21 10:04:42 [debug]  0
                2024-02-21 10:04:42 [debug]  0
                2024-02-21 10:04:42 [debug]  0
                

                M98 P"config.g"

                2024-02-21 10:07:14 [debug] WiFi module stopped
                2024-02-21 10:07:14 [debug] HTTP is enabled on port 80
                2024-02-21 10:07:14 [debug] FTP is disabled
                2024-02-21 10:07:14 [debug] TELNET is disabled
                2024-02-21 10:08:13 [debug] Done printing file
                2024-02-21 10:08:13 [debug] Done printing file
                2024-02-21 10:08:13 [warn] Cancelled printing file 1:/gcodes/new/20-2/300_50 cube_acc500_j5_ps_100.gcode, print time was 7h 47m
                2024-02-21 10:08:13 [warn] Error: G0/G1: insufficient axes homed
                2024-02-21 10:08:13 [info] G10 P0 X0 Y0 Z0                                      
                2024-02-21 10:08:13 [info] G10 P0 R0 S0                                         
                2024-02-21 10:08:13 [warn] Warning: Heater 1 appears to be over-powered. If left on at full power, its temperature is predicted to reach 767C
                2024-02-21 10:08:13 [info] G10 L2 P1 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] G10 L2 P2 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] G10 L2 P3 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] G10 L2 P4 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] G10 L2 P5 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] G10 L2 P6 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] G10 L2 P7 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] G10 L2 P8 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] G10 L2 P9 X0.00 Y0.00 Z0.00
                2024-02-21 10:08:13 [info] Event logging stopped
                2024-02-21 10:08:13 [info] Event logging started at level debug
                2024-02-21 10:08:13 [info] Running: Duet WiFi 1.02 or later: 3.4.0beta3 (2023-08-17 14:30:24)
                2024-02-21 10:08:13 [debug] STPL-INFD300 - Print your imagination!
                
                1 Reply Last reply Reply Quote 0
                • T3P3Tonyundefined
                  T3P3Tony administrators @R006
                  last edited by

                  @R006 so what external drivers are you using on the expansion header for the motors you are connecting there.

                  Also a note you are using custom RRF, have you tested with stock RRF?

                  www.duet3d.com

                  R006undefined 2 Replies Last reply Reply Quote 0
                  • R006undefined
                    R006 @T3P3Tony
                    last edited by

                    @T3P3Tony
                    external driver: Motion king stepper motor drive model no. 2L415B

                    yes we have tested with stock RRF.

                    droftartsundefined 1 Reply Last reply Reply Quote 0
                    • droftartsundefined
                      droftarts administrators @R006
                      last edited by

                      @R006 is it a genuine Duet3D board? Which version of RRF did you test with? Try 3.4.6 https://github.com/Duet3D/RepRapFirmware/releases/tag/3.4.6

                      Ian

                      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                      R006undefined 1 Reply Last reply Reply Quote 0
                      • R006undefined
                        R006 @droftarts
                        last edited by R006

                        @droftarts
                        yes it is.
                        i tried with 3.4.4 & 3.4.6 RRF version standard RRF.

                        I even tried to configure 2 motor in Z with same configuration, but again on Z movement, Y axis gets some random pulse.

                        Tried with 3 different duet 2 WIFI boards and observed this problem repeatedly, when the Z travel more then 5-10 mm then Y motor rotates intermittently, due to some random pulse signals on it,

                        Could you please try at your end, by configuring 3 different Z motors, oneY and one X, run 4 stepper motors with just the board? (temporarily just mark Z0, Y0 X0 using G92 & move Z axis by 5mm, then Y axis gets some pulse? IF you hold the motor shaft, you might feel it. You can also monitor the Y axis pins on DSO to see this.

                        NOTE: External driver was only used for Extruder. I was using onboard drivers for axes.

                        1 Reply Last reply Reply Quote 0
                        • R006undefined
                          R006 @T3P3Tony
                          last edited by

                          @T3P3Tony @Phaedrux @dc42
                          I am waiting for your response.

                          gloomyandyundefined 1 Reply Last reply Reply Quote 0
                          • gloomyandyundefined
                            gloomyandy @R006
                            last edited by

                            @R006 It might help if you post a picture of the board showing how you have the motors connected.

                            R006undefined 1 Reply Last reply Reply Quote 0
                            • R006undefined
                              R006 @gloomyandy
                              last edited by

                              @gloomyandy
                              1.png

                              gloomyandyundefined droftartsundefined 2 Replies Last reply Reply Quote 0
                              • gloomyandyundefined
                                gloomyandy @R006
                                last edited by

                                @R006 Di you have a higher resolution version, it is hard to see what you have connected to the board in that picture.

                                R006undefined 1 Reply Last reply Reply Quote 0
                                • droftartsundefined
                                  droftarts administrators @R006
                                  last edited by

                                  @R006 in your config.g, you haven’t specified any timing for your external drivers, set by M569 Txx:xx:xx:xx parameter. I think this may be causing a problem, as it will be using the default timing of ‘fast’, which is only suitable for the on-board drivers. The high frequency of these steps, and the high step rate you have set for Z (M92 Z2133.33) may be causing the interference. Try:

                                  M569 P5 S1 T5:5:10:10
                                  

                                  And similar for any other external driver.

                                  Ian

                                  Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                  R006undefined 1 Reply Last reply Reply Quote 0
                                  • R006undefined
                                    R006 @droftarts
                                    last edited by R006

                                    @droftarts , @dc42 , @T3P3Tony
                                    hey,
                                    i tried as per your suggestion but problem remains same. Please find detailed observations as per trials:

                                    with onboard drivers connected for all axes:

                                    1. I have 4 boards, and all of them with latest or old software have same behaviour.
                                    2. Somehow on while moving Z, Y axis gets some pulse.
                                    3. If i interchange the driver of X& Y, from P0 , P1 respectively to P1, P0, even then the noise appears only on the Y channel.
                                    4. The problem is some intermittent pulse that generates only on Y channel when declared. If i make P0 & P1 as X, then noise does not appear.
                                    5. It appears only if the Zmove is > 5mm .
                                    6. This noise does not generate when we HOME Z, but move Z at the same homing speed, the problem appears.

                                    with XY via external driver:
                                    7) When we use SPI-> external driver-> with suggested timing parameters, the probelms still exists.

                                    I have tried many things, Can you please check this once in the boards with you ? Somewhere a pulse is generated for the Y axis only when z moves.

                                    Is there anywhere in code where i can look for the problem ?

                                    ***What can be the possible causes for such behaviour?***bolded text

                                    1 Reply Last reply Reply Quote 0
                                    • R006undefined
                                      R006 @gloomyandy
                                      last edited by

                                      @gloomyandy

                                      can't upload original file because the original file size is more and giving error while upload it

                                      droftartsundefined 1 Reply Last reply Reply Quote 0
                                      • droftartsundefined
                                        droftarts administrators @R006
                                        last edited by

                                        @R006 please post your current config.g.

                                        Ian

                                        Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

                                        R006undefined 2 Replies Last reply Reply Quote 0
                                        • R006undefined
                                          R006 @droftarts
                                          last edited by R006

                                          @droftarts
                                          config

                                          
                                          G90                                                  
                                          M83                                                 
                                          M550 P"INFD300s"                                     
                                          M551 P"INFD300"                                      
                                          
                                          ; Network
                                          ;M552 S1                                                                                          
                                          M552 S-1
                                          M586 P0 S1                                           
                                          M586 P1 S0                                          
                                          M586 P2 S0                                           
                                          
                                          ; Drives
                                          M569 P0 S1                                           
                                          M569 P1 S1                                           
                                          M569 P2 S1                                           
                                          M569 P3 S1 
                                          M569 P4 S1 
                                          M569 P5 S1   
                                          M584 X0 Y1 Z2:3:4 E5                                    
                                          M350 X32 Y32 I0                                        
                                          M350 Z16 E16 I1                                      
                                          M92 X160.00 Y160.00 Z2133.33 E932.00 
                                          ;change as per machine                   
                                          M566 X720.00 Y720.00 Z300.00 E600.00                       
                                          M203 X8400.00 Y8400.00 Z420.00 E8400.00          
                                          M201 X3000.00 Y3000.00 Z30.00 E250.00                
                                          ;M-curr 
                                          M906 X2200 Y2200 Z1600 E800 I30                      
                                          M84 S30                                              
                                          
                                          ; Axis Limits
                                          M208 X0 Y0 Z0 S1                                     
                                          M208 X280 Y280 Z291 S0                               
                                          
                                          ; filament Sensor                           
                                          M591 D0 P7 C"exp.e3stop" R15:300 L7 E17 S1            
                                          
                                          ; Endstops
                                          M574 X1 S1 P"xstop"                                 
                                          M574 Y1 S1 P"ystop"                                
                                          M574 Z1 S1 P"zstop+e0_stop+e1_stop"                                 
                                          
                                          ; Z-Probe
                                          M950 S0 C"exp.heater3"                               
                                          M558 P9 C"^zprobe.in" H5 F120 T6000  
                                                         
                                          ;G31 P500 X-35 Y-30 Z2.199    
                                          G31 P500 X0 Y0 Z1.0
                                          
                                          ; Auto level, coordinates as per motor order in M584 
                                          M671 X-17.66:297.34:140.00 Y-5.00:-5.00:327.61 S5.0  ;points position with left right &center
                                          
                                          ; define mesh grid                           
                                          M557 X30:270 Y30:270 S20   
                                          M376 H5                        
                                             					   
                                          ; End Limits 
                                          ;M950 J1 C"!exp.e4stop"  				   	 
                                          ;M581 P1 T2 R0 S1                                     			     
                                          ;M582 T2							     
                                          ;M581 P-1 T2	                                         				     
                                          ;M581 P1 T0 R0 S1                                    
                                          
                                          ;PA
                                          M572 D0 S0.050	
                                          
                                          ;SKEW
                                          M556 Y1.1 S50.0		                             
                                          
                                          ; Bed Heater
                                          M308 S0 P"bedtemp" Y"thermistor" T100000 B4138       
                                          M950 H0 C"bedheat" T0                                
                                          M307 H0 B0 S1.00                                     
                                          M140 H0                                             
                                          M143 H0 S105                                         
                                          
                                          ; Extuder Heater
                                          M308 S1 P"e0temp" Y"pt1000"                          
                                          M950 H1 C"e0heat" T1                                 
                                          M307 H1 B0 S1.00                                      
                                          M143 H1 S320                                         
                                          
                                          ; cooling Fans
                                          M950 F0 C"fan0" Q500                                 
                                          M106 P0 S0 H-1                                       
                                          M950 F1 C"fan1" Q500                                 
                                          M106 P1 S0 H-1                                       
                                          
                                          ; Tools
                                          M563 P0 D0 H1 F0                                    
                                          G10 P0 X0 Y0 Z0                                      
                                          G10 P0 R0 S0                                         
                                          
                                          ; Custom settings are not defined
                                          
                                          ; Miscellaneous
                                          M575 P1 S1 B57600                                   
                                          M501                                                
                                          M911 S21 R22.5 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000"   
                                          M929 S3 P"/macros/SERVICE/log/STPL_DEBUG.txt"       
                                          M17
                                          
                                          

                                          i have tested with 4 more boards with me all the 8 boards show same problem of noise on Y drive whenever Z moves irrespective of Z speed.

                                          here is my invoice conforming on my original board purchase.

                                          kindly tell me how to proceed, as none of the board is working well & I am confident about the config declaration of motors.
                                          I have also observed that whenever Yaxis gets this extra pulses due to Z move, after that on homing Y axis, its displays values like -0.6 or -0.0 depending upon its position.

                                          Please respond at the earliest here, as I have a customer to respond to & I am stuck with the board isssue.

                                          INVOICE-2.pdf

                                          droftartsundefined 2 Replies Last reply Reply Quote 0
                                          • R006undefined
                                            R006 @droftarts
                                            last edited by

                                            @droftarts @T3P3Tony @Phaedrux @dc42
                                            I am waiting for your response.

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