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    Solved Duet 3 SBC DCS has stopped

    Beta Firmware
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    • jay_s_uk
      jay_s_uk @dhusolo last edited by jay_s_uk

      @dhusolo
      Are you still able to connect to the board via DWC?
      If you can confirm the firmware version using 3.1.1
      If it's still 3.1.1, send M997 B0
      I would be interested to see if you get any errors reported

      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

      dhusolo 1 Reply Last reply Reply Quote 0
      • dhusolo
        dhusolo @jay_s_uk last edited by

        @jay_s_uk
        I had to start DCS and DWS manually but I was able to get to the web interface.

        M122 "DSF"
        === Duet Control Server ===
        Duet Control Server v3.2.0-beta3
        Code buffer space: 4096
        Configured SPI speed: 8000000 Hz
        Full transfers per second: 32.68
        11/8/2020, 2:58:59 PM```	
        
        M122
        === Diagnostics ===
        RepRapFirmware for Duet 3 MB6HC version 3.2-beta3 running on Duet 3 MB6HC v1.01 or later (SBC mode)
        Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
        Used output buffers: 1 of 40 (10 max)
        === RTOS ===
        Static ram: 122124
        Dynamic ram: 137508 of which 0 recycled
        Never used RAM 132560, free system stack 185 words
        Tasks: Linux(ready,131) HEAT(blocked,362) CanReceiv(blocked,948) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,66) MAIN(running,1300) IDLE(ready,19)
        Owned mutexes: HTTP(MAIN)
        === Platform ===
        Last reset 00:09:17 ago, cause: software
        Last software reset details not available
        Error status: 0x00
        MCU temperature: min 25.3, current 26.2, max 26.4
        Supply voltage: min 0.3, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
        12V rail voltage: min 0.1, current 0.2, max 0.2, under voltage events: 0
        Driver 0: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
        Driver 1: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
        Driver 2: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
        Driver 3: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
        Driver 4: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
        Driver 5: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
        Date/time: 2020-11-08 14:58:59
        Slowest loop: 743.08ms; fastest: 0.16ms
        === Storage ===
        Free file entries: 10
        SD card 0 not detected, interface speed: 37.5MBytes/sec
        SD card longest read time 0.0ms, write time 0.0ms, max retries 0
        === Move ===
        Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
        Bed compensation in use: none, comp offset 0.000
        === MainDDARing ===
        Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
        === AuxDDARing ===
        Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
        === Heat ===
        Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
        === GCodes ===
        Segments left: 0
        Movement lock held by null
        HTTP* is doing "M122" in state(s) 0
        Telnet is idle in state(s) 0
        File is idle in state(s) 0
        USB is idle in state(s) 0
        Aux is idle in state(s) 0
        Trigger* is idle in state(s) 0
        Queue is idle in state(s) 0
        LCD is idle in state(s) 0
        SBC is idle in state(s) 0
        Daemon is idle in state(s) 0
        Aux2 is idle in state(s) 0
        Autopause is idle in state(s) 0
        Code queue is empty.
        === CAN ===
        Messages sent 0, send timeouts 0, longest wait 0ms for type 0, free CAN buffers 47
        === SBC interface ===
        State: 0, failed transfers: 1
        Last transfer: 14ms ago
        RX/TX seq numbers: 17902/17903
        SPI underruns 0, overruns 0
        Number of disconnects: 0, IAP RAM available 0x20aa0
        Buffer RX/TX: 0/0-0
        === Duet Control Server ===
        Duet Control Server v3.2.0-beta3
        Code buffer space: 4096
        Configured SPI speed: 8000000 Hz
        Full transfers per second: 32.56
        
        jay_s_uk 1 Reply Last reply Reply Quote 0
        • jay_s_uk
          jay_s_uk @dhusolo last edited by

          @dhusolo well at least you're back on the latest firmware.
          @chrishamm any comments on the error above whilst updating?

          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

          1 Reply Last reply Reply Quote 0
          • dhusolo
            dhusolo last edited by

            More of a status update: I've started the same print again but I don't load any filament. I didn't want to waste the filament if it's going to cancel on me again.

            However I can now hear some strange jerky movements. I have a coreXY so it's hard to narrow down what stepper it's coming from especially since there's no filament going through it.

            Phaedrux 1 Reply Last reply Reply Quote 0
            • oliof
              oliof last edited by

              I think my recent post about issues with 3.2b3 are very similar to this issue.

              <>Creality CR-20 IDEX Duet3 mini 5+<>RatRig V-Minion SKR RRF 1.1<>

              1 Reply Last reply Reply Quote 2
              • Phaedrux
                Phaedrux Moderator @dhusolo last edited by

                @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                Z-Bot CoreXY Build | Thingiverse Profile

                A Former User dhusolo 2 Replies Last reply Reply Quote 0
                • A Former User
                  A Former User @Phaedrux last edited by

                  @Phaedrux said in Duet 3 SBC DCS has stopped:

                  @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                  Oh the irony.....

                  Phaedrux 1 Reply Last reply Reply Quote 0
                  • dhusolo
                    dhusolo @Phaedrux last edited by

                    @Phaedrux I'm going to attempt to go back to RRF 3.1.1 with RPI since issues with connecting are resolved. Doesn't make a lot of sense that it was working previously for 3 months without any issue.

                    If that brings the same symptoms I'll run it in standalone until RRF 3.2 is stable. At least I know the board isn't bad

                    1 Reply Last reply Reply Quote 0
                    • Phaedrux
                      Phaedrux Moderator @Guest last edited by

                      @CaLviNx It's not irony because no one ever disagreed with you.

                      Z-Bot CoreXY Build | Thingiverse Profile

                      A Former User 1 Reply Last reply Reply Quote 0
                      • dhusolo
                        dhusolo last edited by

                        Can confirm going back to 3.1.1. the bug is still present. No idea why it appeared months after the original upload and weeks after any update to my config.

                        I did notice under Linux interface it shows a failed transfer, some bit loss and a SPI underrun

                        	M122
                        === Diagnostics ===
                        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                        Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                        Used output buffers: 1 of 40 (12 max)
                        === RTOS ===
                        Static ram: 154604
                        Dynamic ram: 163392 of which 140 recycled
                        Exception stack ram used: 584
                        Never used ram: 74496
                        Tasks: NETWORK(ready,1968) HEAT(blocked,1188) CanReceiv(suspended,3820) CanSender(suspended,1384) CanClock(blocked,1436) TMC(blocked,60) MAIN(running,2672) IDLE(ready,76)
                        Owned mutexes:
                        === Platform ===
                        Last reset 03:06:26 ago, cause: power up
                        Last software reset at 2020-11-09 16:57, reason: User, spinning module LinuxInterface, available RAM 77008 bytes (slot 1)
                        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                        Error status: 0
                        MCU temperature: min 34.4, current 37.6, max 39.2
                        Supply voltage: min 24.2, current 24.5, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                        12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
                        Driver 0: standstill, reads 55804, writes 22 timeouts 0, SG min/max 0/193
                        Driver 1: standstill, reads 55797, writes 30 timeouts 0, SG min/max 0/1023
                        Driver 2: standstill, reads 55797, writes 30 timeouts 0, SG min/max 0/1023
                        Driver 3: standstill, reads 55794, writes 34 timeouts 0, SG min/max 0/1023
                        Driver 4: standstill, reads 55794, writes 34 timeouts 0, SG min/max 0/1023
                        Driver 5: standstill, reads 55795, writes 34 timeouts 0, SG min/max 0/1023
                        Date/time: 2020-11-09 20:05:07
                        Slowest loop: 9.46ms; fastest: 0.14ms
                        === Storage ===
                        Free file entries: 10
                        SD card 0 not detected, interface speed: 37.5MBytes/sec
                        SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                        === Move ===
                        Hiccups: 0(0), FreeDm: 375, MinFreeDm: 317, MaxWait: 669637ms
                        Bed compensation in use: mesh, comp offset -0.024
                        === MainDDARing ===
                        Scheduled moves: 169139, completed moves: 169139, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                        === AuxDDARing ===
                        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
                        === Heat ===
                        Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                        === GCodes ===
                        Segments left: 0
                        Movement lock held by null
                        HTTP* is ready with "M122" in state(s) 0
                        Telnet is idle in state(s) 0
                        File* is idle in state(s) 0
                        USB is idle in state(s) 0
                        Aux is idle in state(s) 0
                        Trigger* is idle in state(s) 0
                        Queue* is idle in state(s) 0
                        LCD is idle in state(s) 0
                        SBC is idle in state(s) 0
                        Daemon* is idle in state(s) 0
                        Aux2 is idle in state(s) 0
                        Autopause is idle in state(s) 0
                        Code queue is empty.
                        === Network ===
                        Slowest loop: 1.44ms; fastest: 0.01ms
                        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                        HTTP sessions: 0 of 8
                        - Ethernet -
                        State: disabled
                        Error counts: 0 0 0 0 0
                        Socket states: 0 0 0 0 0 0 0 0
                        === Filament sensors ===
                        Extruder 0 sensor: ok
                        === CAN ===
                        Messages sent 44905, longest wait 0ms for type 0
                        === Linux interface ===
                        State: 0, failed transfers: 1
                        Last transfer: 17ms ago
                        RX/TX seq numbers: 36691/32296
                        SPI underruns 1, overruns 0
                        Number of disconnects: 0
                        Buffer RX/TX: 0/0-0
                        === Duet Control Server ===
                        Duet Control Server v3.1.1
                        Daemon:
                        Finishing macro daemon.g, started by system
                        > Next stack level
                        Code buffer space: 4096
                        Configured SPI speed: 8000000 Hz
                        Full transfers per second: 32.48
                        
                        1 Reply Last reply Reply Quote 0
                        • A Former User
                          A Former User @Phaedrux last edited by

                          @Phaedrux said in Duet 3 SBC DCS has stopped:

                          @CaLviNx It's not irony because no one ever disagreed with you.

                          The irony is that time and effort has been needlessly expended in a vain attempt to fix an issue that the reason for (at this point of time) is evidently unknown when, instead of trying to fix it, the smart approach would have been to just go standalone in the first place which would have resulted in getting the machine printing again, and printing is the whole point of the exercise.

                          Phaedrux dhusolo 2 Replies Last reply Reply Quote 0
                          • Phaedrux
                            Phaedrux Moderator @Guest last edited by

                            @CaLviNx It must be difficult going through life with such superior intellect. How do you manage to survive amongst us?

                            Z-Bot CoreXY Build | Thingiverse Profile

                            A Former User 1 Reply Last reply Reply Quote 0
                            • dhusolo
                              dhusolo @Guest last edited by

                              @CaLviNx seriously stop commenting. I do beta testing and bug fixing for a living. I took the steps I did for a reason. Everyone else has been trying to help while all you've been doing is throwing jabs in and out of this thread. I don't need you to tell me what the "smart approach" is because "the whole point of the exercise" is to figure out what happened and to see if I could fix it, not applying a band-aid.

                              1 Reply Last reply Reply Quote 2
                              • chrishamm
                                chrishamm administrators last edited by

                                To get back to the topic: I think the previously reported problems should be fixed in 3.2.0-b3.2. Feel free to test this again.

                                Duet software engineer

                                dhusolo 1 Reply Last reply Reply Quote 0
                                • A Former User
                                  A Former User @Phaedrux last edited by

                                  @Phaedrux said in Duet 3 SBC DCS has stopped:

                                  @CaLviNx It must be difficult going through life with such superior intellect. How do you manage to survive amongst us?

                                  Trust me dealing with such stupidity on a daily basis is tiresome.....

                                  1 Reply Last reply Reply Quote 0
                                  • dhusolo
                                    dhusolo @chrishamm last edited by

                                    @chrishamm That did fix the issue but after updating to 3.2.b3 I started to have jerky movements while printing that wasn't present before the update

                                    chrishamm 1 Reply Last reply Reply Quote 0
                                    • chrishamm
                                      chrishamm administrators @dhusolo last edited by

                                      @dhusolo Please confirm that the installed RRF version is 3.2.0-beta3.2 and not 3.2.0-beta3.

                                      Duet software engineer

                                      dhusolo 1 Reply Last reply Reply Quote 0
                                      • dhusolo
                                        dhusolo @chrishamm last edited by

                                        @chrishamm can confirm it was 3.2.b3

                                        M122
                                        === Diagnostics ===
                                        RepRapFirmware for Duet 3 MB6HC version 3.2-beta3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                        Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                                        Used output buffers: 1 of 40 (10 max)
                                        === RTOS ===
                                        Static ram: 122236
                                        Dynamic ram: 139164 of which 24 recycled
                                        Never used RAM 130768, free system stack 200 words
                                        Tasks: Linux(ready,97) HEAT(blocked,296) CanReceiv(blocked,948) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,54) MAIN(running,1189) IDLE(ready,19)
                                        Owned mutexes: HTTP(MAIN)
                                        === Platform ===
                                        Last reset 00:00:20 ago, cause: software
                                        Last software reset at 2020-11-16 16:14, reason: User, GCodes spinning, available RAM 130768, slot 0
                                        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0xffffffff Task Linu
                                        Error status: 0x00
                                        MCU temperature: min 38.3, current 38.7, max 38.8
                                        Supply voltage: min 24.6, current 24.7, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                                        12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                        Driver 0: position 0, standstill, reads 35729, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 1: position 0, standstill, reads 35730, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 2: position 0, standstill, reads 35731, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 3: position 0, standstill, reads 35732, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 4: position 0, standstill, reads 35733, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 5: position 0, standstill, reads 35733, writes 14 timeouts 0, SG min/max 0/0
                                        Date/time: 2020-11-16 16:14:56
                                        Slowest loop: 1.42ms; fastest: 0.19ms
                                        === Storage ===
                                        Free file entries: 10
                                        SD card 0 not detected, interface speed: 37.5MBytes/sec
                                        SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                        === Move ===
                                        Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                                        Bed compensation in use: none, comp offset 0.000
                                        === MainDDARing ===
                                        Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                        === AuxDDARing ===
                                        Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                        === Heat ===
                                        Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                        === GCodes ===
                                        Segments left: 0
                                        Movement lock held by null
                                        HTTP* is doing "M122" in state(s) 0
                                        Telnet is idle in state(s) 0
                                        File is idle in state(s) 0
                                        USB is idle in state(s) 0
                                        Aux is idle in state(s) 0
                                        Trigger* is idle in state(s) 0
                                        Queue is idle in state(s) 0
                                        LCD is idle in state(s) 0
                                        SBC is idle in state(s) 0
                                        Daemon is idle in state(s) 0
                                        Aux2 is idle in state(s) 0
                                        Autopause is idle in state(s) 0
                                        Code queue is empty.
                                        === Filament sensors ===
                                        Extruder 0 sensor: ok
                                        === CAN ===
                                        Messages sent 55, send timeouts 55, longest wait 0ms for type 0, free CAN buffers 47
                                        === SBC interface ===
                                        State: 0, failed transfers: 0
                                        Last transfer: 20ms ago
                                        RX/TX seq numbers: 440/442
                                        SPI underruns 0, overruns 0
                                        Number of disconnects: 0, IAP RAM available 0x20a30
                                        Buffer RX/TX: 0/0-0
                                        === Duet Control Server ===
                                        Duet Control Server v3.2.0-beta3
                                        Code buffer space: 4096
                                        Configured SPI speed: 8000000 Hz
                                        Full transfers per second: 30.36
                                        
                                        chrishamm 1 Reply Last reply Reply Quote 0
                                        • chrishamm
                                          chrishamm administrators @dhusolo last edited by

                                          @dhusolo What triggers are you using? Can you share the corresponding macro files?

                                          Duet software engineer

                                          dhusolo 2 Replies Last reply Reply Quote 0
                                          • dhusolo
                                            dhusolo @chrishamm last edited by

                                            @chrishamm Actually I'm not actively using the trigger anymore. That was originally configured for RRF2 as a shutdown button. trigger2.g might exist but it's not defined in config.g.

                                            I've tried printing with 3.2.b3 to see if the jerky movements come back. So far it hasn't. It's a different model and it's slower speeds so i'm wondering if the print speeds had been related to why it was doing it. I'm going to try that other file again to see if I can replicate it. If I can at my normal print speeds I'll slow it down to see if it happens again.

                                            1 Reply Last reply Reply Quote 0
                                            • dhusolo
                                              dhusolo @chrishamm last edited by

                                              @chrishamm I ran the print that had the jerky movement after updating and it seemed like it printed normally.

                                              I made sure I followed the getting started link verbatim. Originally I didn't use Etcher or the Raspberry Pi Imager program to write the image. I used a program called USB Image Tool because i've been using it for years. This time I used the Raspberry Pi Imager. The only other thing I can think I did different was I don't remember changing the buffer size before

                                              echo "options spidev bufsiz=8192" | sudo tee /etc/modprobe.d/spidev.conf
                                              
                                              1 Reply Last reply Reply Quote 0
                                              • dhusolo
                                                dhusolo last edited by

                                                Well it happened again while running 3.2.b3. It has been printing pretty good the last week. Over night the print cancelled but it just stopped printing. The heaters are still at temp and the head was in the same position on the print, it didn't run pause.g.

                                                When I started DWC on my PC the print status was still printing. I pressed pause and that's when it ran pause.g. I tried to resume the print and it said cannot print no file selected

                                                m122
                                                === Diagnostics ===
                                                RepRapFirmware for Duet 3 MB6HC version 3.2-beta3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                                Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                                                Used output buffers: 1 of 40 (12 max)
                                                === RTOS ===
                                                Static ram: 122236
                                                Dynamic ram: 139788 of which 64 recycled
                                                Never used RAM 130104, free system stack 118 words
                                                Tasks: Linux(ready,67) HEAT(blocked,295) CanReceiv(blocked,948) CanSender(blocked,343) CanClock(blocked,352) TMC(blocked,18) MAIN(running,669) IDLE(ready,19)
                                                Owned mutexes: HTTP(MAIN)
                                                === Platform ===
                                                Last reset 14:24:35 ago, cause: software
                                                Last software reset at 2020-11-22 19:53, reason: User, GCodes spinning, available RAM 130104, slot 2
                                                Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0xffffffff Task Linu
                                                Error status: 0x00
                                                MCU temperature: min 35.4, current 37.2, max 38.3
                                                Supply voltage: min 24.2, current 24.6, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
                                                12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
                                                Driver 0: position 200, standstill, reads 25360, writes 21 timeouts 0, SG min/max 0/202
                                                Driver 1: position -200, standstill, reads 25349, writes 33 timeouts 0, SG min/max 0/1023
                                                Driver 2: position 5843, standstill, reads 25350, writes 33 timeouts 0, SG min/max 0/1023
                                                Driver 3: position 0, standstill, reads 25350, writes 33 timeouts 0, SG min/max 0/1023
                                                Driver 4: position 0, standstill, reads 25351, writes 33 timeouts 0, SG min/max 0/1023
                                                Driver 5: position 0, standstill, reads 25352, writes 33 timeouts 0, SG min/max 0/1023
                                                Date/time: 2020-11-23 10:17:46
                                                Slowest loop: 278.17ms; fastest: 0.09ms
                                                === Storage ===
                                                Free file entries: 10
                                                SD card 0 not detected, interface speed: 37.5MBytes/sec
                                                SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                                === Move ===
                                                Hiccups: 0(0), FreeDm: 375, MinFreeDm: 354, MaxWait: 10418300ms
                                                Bed compensation in use: mesh, comp offset 0.000
                                                === MainDDARing ===
                                                Scheduled moves 480277, completed moves 480277, StepErrors 0, LaErrors 0, Underruns [0, 0, 3], CDDA state -1
                                                === AuxDDARing ===
                                                Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                                === Heat ===
                                                Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                                === GCodes ===
                                                Segments left: 0
                                                Movement lock held by null
                                                HTTP* is doing "M122" in state(s) 0
                                                Telnet is idle in state(s) 0
                                                File* is idle in state(s) 0
                                                USB is idle in state(s) 0
                                                Aux is idle in state(s) 0
                                                Trigger* is idle in state(s) 0
                                                Queue* is idle in state(s) 0
                                                LCD is idle in state(s) 0
                                                SBC is idle in state(s) 0
                                                Daemon is idle in state(s) 0
                                                Aux2 is idle in state(s) 0
                                                Autopause is idle in state(s) 0
                                                Code queue is empty.
                                                === Filament sensors ===
                                                Extruder 0 sensor: ok
                                                === CAN ===
                                                Messages sent 207659, send timeouts 207659, longest wait 0ms for type 0, free CAN buffers 47
                                                === SBC interface ===
                                                State: 0, failed transfers: 1
                                                Last transfer: 19ms ago
                                                RX/TX seq numbers: 27088/26081
                                                SPI underruns 3, overruns 0
                                                Number of disconnects: 0, IAP RAM available 0x20a30
                                                Buffer RX/TX: 0/0-0
                                                === Duet Control Server ===
                                                Duet Control Server v3.2.0-beta3
                                                Code buffer space: 4096
                                                Configured SPI speed: 8000000 Hz
                                                Full transfers per second: 32.32
                                                
                                                chrishamm 1 Reply Last reply Reply Quote 0
                                                • chrishamm
                                                  chrishamm administrators @dhusolo last edited by

                                                  @dhusolo Please upgrade to 3.2-b4, it should be fixed in the latest builds.

                                                  Duet software engineer

                                                  1 Reply Last reply Reply Quote 0
                                                  • medicusdkfz
                                                    medicusdkfz last edited by

                                                    Same here with 3.2beta4 on a Duet3 6HC/3HC: Freezing during the print without a pause command... Only solution is to close any web connection in the browser (on a Macbook Pro tested with Safari/Edge/Chrome - it doesn't matter). Also problems with more than one browser connection to the board...

                                                    M122
                                                    === Diagnostics ===
                                                    RepRapFirmware for Duet 3 MB6HC version 3.2-beta4 running on Duet 3 MB6HC v0.6 or 1.0 (standalone mode)
                                                    Board ID: 08DJM-956L2-G43S8-6J1DJ-3SN6M-9S0YG
                                                    Used output buffers: 1 of 40 (12 max)
                                                    === RTOS ===
                                                    Static ram: 123212
                                                    Dynamic ram: 168800 of which 488 recycled
                                                    Never used RAM 99692, free system stack 180 words
                                                    Tasks: NETWORK(ready,189) ETHERNET(blocked,110) HEAT(blocked,297) CanReceiv(blocked,898) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,51) MAIN(running,1127) IDLE(ready,19)
                                                    Owned mutexes:
                                                    === Platform ===
                                                    Last reset 00:13:05 ago, cause: software
                                                    Last software reset at 2020-12-06 11:17, reason: MemoryProtectionFault mmarValid daccViol, GCodes spinning, available RAM 99652, slot 2
                                                    Software reset code 0x4163 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x0444a804 BFAR 0x00000016 SP 0x2040b928 Task ETHE
                                                    Stack: 20423888 00000000 ffffffff 00000002 204098a4 0040fdf9 004109a2 61000000 204098ec 20423830 2042384c 0040fdf9 2041df64 2041b3cc 2041de94 0040c7a9 20411574 00000000 00000001 2041b3cc 204098a4 00000002 00000002 2041b3cc 20409872 a4b2a8c0 2040ba34
                                                    Error status: 0x00
                                                    MCU temperature: min 36.5, current 36.7, max 39.5
                                                    Supply voltage: min 23.9, current 23.9, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
                                                    12V rail voltage: min 12.1, current 12.2, max 12.3, under voltage events: 0
                                                    Driver 0: position 0, standstill, reads 12266, writes 14 timeouts 0, SG min/max 0/0
                                                    Driver 1: position 0, standstill, reads 12266, writes 14 timeouts 0, SG min/max 0/0
                                                    Driver 2: position 0, standstill, reads 12267, writes 14 timeouts 0, SG min/max 0/0
                                                    Driver 3: position 0, standstill, reads 12268, writes 14 timeouts 0, SG min/max 0/0
                                                    Driver 4: position 0, standstill, reads 12269, writes 14 timeouts 0, SG min/max 0/0
                                                    Driver 5: position 0, standstill, reads 12270, writes 14 timeouts 0, SG min/max 0/0
                                                    Date/time: 2020-12-06 11:30:20
                                                    Slowest loop: 5.04ms; fastest: 0.15ms
                                                    === Storage ===
                                                    Free file entries: 10
                                                    SD card 0 detected, interface speed: 25.0MBytes/sec
                                                    SD card longest read time 2.6ms, write time 0.0ms, max retries 0
                                                    === Move ===
                                                    Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                                                    Bed compensation in use: none, comp offset 0.000
                                                    === MainDDARing ===
                                                    Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                                    === AuxDDARing ===
                                                    Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                                    === Heat ===
                                                    Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                                    === GCodes ===
                                                    Segments left: 0
                                                    Movement lock held by null
                                                    HTTP is idle in state(s) 0
                                                    Telnet is idle in state(s) 0
                                                    File is idle in state(s) 0
                                                    USB is idle in state(s) 0
                                                    Aux is idle in state(s) 0
                                                    Trigger is idle in state(s) 0
                                                    Queue is idle in state(s) 0
                                                    LCD is idle in state(s) 0
                                                    SBC is idle in state(s) 0
                                                    Daemon is idle in state(s) 0
                                                    Aux2 is idle in state(s) 0
                                                    Autopause is idle in state(s) 0
                                                    Code queue is empty.
                                                    === Network ===
                                                    Slowest loop: 6.42ms; fastest: 0.03ms
                                                    Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                                                    HTTP sessions: 1 of 8

                                                    • Ethernet -
                                                      State: active
                                                      Error counts: 0 0 0 0 0
                                                      Socket states: 2 2 2 2 2 0 0 0
                                                      === CAN ===
                                                      Messages queued 3151, send timeouts 0, received 3152, lost 0, longest wait 10ms for reply type 6027, free buffers 47
                                                    chrishamm 1 Reply Last reply Reply Quote 0
                                                    • chrishamm
                                                      chrishamm administrators @medicusdkfz last edited by

                                                      @medicusdkfz You are running in standalone mode and now version 3.2.0-b4.1 is available. Please upgrade to that version first and open a new thread with a fresh dump of M122 if the problem persists.

                                                      Duet software engineer

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