Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    BL-Touch - multiple problems -

    Scheduled Pinned Locked Moved Unsolved
    Firmware installation
    5
    60
    2.2k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • duttiundefined
      dutti @Phaedrux
      last edited by

      @Phaedrux
      ok sry.
      I tested the wiring. Its not the problem....
      this is the last problem I have to solve before starting. Thats really bad.

      1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        If that's the case and the wiring is good please update your firmware (as linked above for the Duet + SBC). Send M115 after to verify.

        Then please send M98 Pconfig.g and report any errors.

        Z-Bot CoreXY Build | Thingiverse Profile

        duttiundefined 2 Replies Last reply Reply Quote 0
        • duttiundefined
          dutti @Phaedrux
          last edited by

          @Phaedrux
          M98 Error: Non-empty string expected
          firmware is updated

          Phaedruxundefined 1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @dutti
            last edited by

            That's a weird error. You're sending this exactly?

            M98 Pconfig.g

            Z-Bot CoreXY Build | Thingiverse Profile

            duttiundefined 1 Reply Last reply Reply Quote 0
            • duttiundefined
              dutti @Phaedrux
              last edited by

              @Phaedrux said in BL-Touch - multiple problems -:

              M98 Pconfig.g

              yes

              1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                try M98 P"config.g"

                Z-Bot CoreXY Build | Thingiverse Profile

                1 Reply Last reply Reply Quote 0
                • duttiundefined
                  dutti @Phaedrux
                  last edited by

                  @Phaedrux said in BL-Touch - multiple problems -:

                  M98 Pconfig.g

                  ´´´Response to long, see console´´.
                  I havent connected the expansion board, yet. Is this a problem?

                  dc42undefined 1 Reply Last reply Reply Quote 0
                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    Are you in the DWC gcode console when you send that?

                    Z-Bot CoreXY Build | Thingiverse Profile

                    duttiundefined 1 Reply Last reply Reply Quote 0
                    • duttiundefined
                      dutti @Phaedrux
                      last edited by

                      @Phaedrux yes

                      1 Reply Last reply Reply Quote 0
                      • duttiundefined
                        dutti
                        last edited by

                        I homed z again. It's homing without triggering manual the BL.

                        Also when I go down with the z axis... doesn't care which amount and then homing z, the z motors are turning back always the same amount and it stops.
                        --> I hope that helps

                        1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          I'm not exactly sure what you mean.

                          Looking back over your config.g I notice two things on your M558 command that we can try changing.

                          M558 P9 C"^io7.in" H15 F120 1400

                          First, you're missing the T in front of the 1400 to define the travel speed between probe points.

                          Second, try removing the ^ from in front of io7.in. I think it's only zprobe.in that requires the pullup.

                          I'd still like to see what the gcode console output is from sending M98 P"config.g" It should echo SOMETHING back.

                          Z-Bot CoreXY Build | Thingiverse Profile

                          1 Reply Last reply Reply Quote 0
                          • duttiundefined
                            dutti
                            last edited by

                            M558 P9 C"io7.in" H15 F120 T1400 ----> doesn´t work

                            M98 P"config.g"
                            --> response to long, see console

                            Should I buy a other sensor?
                            My motivation after a few days is down.....

                            JoergS5undefined 1 Reply Last reply Reply Quote 0
                            • JoergS5undefined
                              JoergS5 @dutti
                              last edited by

                              @barbarossa-cologne what does the console say? If you cannot read it, you can download it into a file:
                              https://duet3d.dozuki.com/Wiki/Duet_Web_Control_Manual#Section_G_Code_Console

                              duttiundefined 1 Reply Last reply Reply Quote 0
                              • duttiundefined
                                dutti @JoergS5
                                last edited by

                                @JoergS5

                                M98 P"config.g"
                                Error: M569: Response timeout: CAN addr 1, req type 6018, RID=108
                                Error: M569: Response timeout: CAN addr 1, req type 6018, RID=109
                                Error: M569: Response timeout: CAN addr 1, req type 6018, RID=110
                                Error: M350: Response timeout: CAN addr 1, req type 6021, RID=111
                                Response timeout: CAN addr 1, req type 6021, RID=112
                                Response timeout: CAN addr 1, req type 6021, RID=113
                                Error: M906: Response timeout: CAN addr 1, req type 6017, RID=114
                                Response timeout: CAN addr 1, req type 6017, RID=115
                                Response timeout: CAN addr 1, req type 6017, RID=116
                                Error: M557: bad grid definition: Too many grid points; suggest increase spacing to 31.8mm
                                Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
                                Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 404C

                                JoergS5undefined 1 Reply Last reply Reply Quote 0
                                • PaulHewundefined
                                  PaulHew
                                  last edited by

                                  @barbarossa-cologne said in BL-Touch - multiple problems -:

                                  ; Z-Probe
                                  M950 S0 C"io7.out" ; create servo pin 0 for BLTouch
                                  M558 P9 C"^io7.in" H15 F120 1400 ; set Z probe type to bltouch and the dive height + speeds

                                  If this is from your current config.g, you need to swap the lines round. M558 before M950

                                  HTH

                                  Paul

                                  RailCore II - Duet Mini + 1LC, Voron V0.1 - Duet Mini
                                  Voron 2.4 disassembled..... Waiting for the RailCore Mini....

                                  1 Reply Last reply Reply Quote 0
                                  • PaulHewundefined
                                    PaulHew
                                    last edited by

                                    Mine from a DUET2 for comparison

                                    M558 P9 C"^zprobe.in" H5 R1 F120 T6000 A5 S0.02  ;BLTouch connected to Z probe IN pin
                                    M950 S0 C"duex.pwm1"				             ;BLTouch Servo (S0) on duet pwm1
                                    G31 X2 Y42 Z0.513 P25                            ; Customize your offsets appropriately - do a paper test, and put the probed value in the Z value here
                                    

                                    RailCore II - Duet Mini + 1LC, Voron V0.1 - Duet Mini
                                    Voron 2.4 disassembled..... Waiting for the RailCore Mini....

                                    duttiundefined 1 Reply Last reply Reply Quote 0
                                    • JoergS5undefined
                                      JoergS5 @dutti
                                      last edited by JoergS5

                                      @barbarossa-cologne said in BL-Touch - multiple problems -:

                                      Error: M557: bad grid definition: Too many grid points; suggest increase spacing to 31.8mm

                                      I checked it, from 15 to 650 are 21.16 points, so if it is rounded down to 21 it would reach the 441 limit of Duet 2 (limit of Duet 3 is not known to me). So reducing 650 a bit or S bigger than 30 would be the safe side.

                                      1 Reply Last reply Reply Quote 0
                                      • duttiundefined
                                        dutti
                                        last edited by

                                        @JoergS5
                                        I reduced the amount...

                                        @PaulHew
                                        I changed it. Same problem.....

                                        JoergS5undefined 1 Reply Last reply Reply Quote 0
                                        • duttiundefined
                                          dutti
                                          last edited by

                                          The software is homing Z without triggering anything. That´s really confusing for me..

                                          1 Reply Last reply Reply Quote 0
                                          • duttiundefined
                                            dutti @PaulHew
                                            last edited by

                                            @PaulHew
                                            Like this?
                                            ; Endstops
                                            M574 X2 S1 P"!io3.in" ; configure active-high endstop for high end on X via pin !io3.in
                                            M574 Y2 S1 P"!io0.in" ; configure active-high endstop for high end on Y via pin !io0.in

                                            ; Z-Probe
                                            M558 P9 C"^io7.in" H15 F120 T1400 ; set Z probe type to bltouch and the dive height + speeds
                                            M950 S0 C"io7.out" ; create servo pin 0 for BLTouch
                                            G31 P500 X0 Y0 Z2.5 ; set Z probe trigger value, offset and trigger height
                                            M557 X15:650 Y15:650 S30 ; define mesh grid

                                            1 Reply Last reply Reply Quote 0
                                            • First post
                                              Last post
                                            Unless otherwise noted, all forum content is licensed under CC-BY-SA