Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    Short to ground on drivers 0123

    Scheduled Pinned Locked Moved Unsolved
    Duet Hardware and wiring
    8
    63
    2.7k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • Phaedruxundefined
      Phaedrux Moderator @Touchthebitum
      last edited by

      @Touchthebitum said in Short to ground on drivers 0123:

      I forgot to mention that the error message is present without the motors plugged ...
      It is the Duet3 V1.01

      Here is a photo of the plug. I tested the phase before plugging it.

      Tape is provisory.

      driver 0.jpg

      What role does the tape play there? Is it possible the crimp was bad from the start and making a bad connection?

      Were you getting the error before plugging anything in or only after?

      Z-Bot CoreXY Build | Thingiverse Profile

      Touchthebitumundefined 1 Reply Last reply Reply Quote 0
      • Touchthebitumundefined
        Touchthebitum @Phaedrux
        last edited by Touchthebitum

        @Phaedrux Tape is only a protection to avoid shorts contact. Contacts were good since I made continuity tests and resistance tests and I always had signal.

        1 Reply Last reply Reply Quote 0
        • Phaedruxundefined
          Phaedrux Moderator
          last edited by

          Were there any other error messages along with the short to ground errors?

          Z-Bot CoreXY Build | Thingiverse Profile

          Touchthebitumundefined 1 Reply Last reply Reply Quote 0
          • Touchthebitumundefined
            Touchthebitum @Phaedrux
            last edited by Touchthebitum

            @Phaedrux No, M122 had not error messages. Only those ground-short messages

            1 Reply Last reply Reply Quote 0
            • Phaedruxundefined
              Phaedrux Moderator
              last edited by

              When are where was the Duet 3 purchased?

              Z-Bot CoreXY Build | Thingiverse Profile

              Touchthebitumundefined 1 Reply Last reply Reply Quote 0
              • Touchthebitumundefined
                Touchthebitum @Phaedrux
                last edited by Touchthebitum

                @Phaedrux www.3dware.ch

                1 Reply Last reply Reply Quote 0
                • dc42undefined
                  dc42 administrators
                  last edited by

                  Please send M122 and post the resulting output here.

                  Duet WiFi hardware designer and firmware engineer
                  Please do not ask me for Duet support via PM or email, use the forum
                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                  Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                  • Touchthebitumundefined
                    Touchthebitum @dc42
                    last edited by

                    @dc42

                    m122
                    === Diagnostics ===
                    RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                    Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                    Used output buffers: 1 of 40 (10 max)
                    === RTOS ===
                    Static ram: 154604
                    Dynamic ram: 162592 of which 44 recycled
                    Exception stack ram used: 224
                    Never used ram: 75752
                    Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,204) MAIN(running,4952) IDLE(ready,76)
                    Owned mutexes:
                    === Platform ===
                    Last reset 00:00:44 ago, cause: power up
                    Last software reset at 2020-07-27 15:14, reason: User, spinning module LinuxInterface, available RAM 75704 bytes (slot 0)
                    Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                    Error status: 0
                    MCU temperature: min 19.4, current 27.7, max 27.8
                    Supply voltage: min 24.0, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                    12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                    Driver 0: standstill, reads 22474, writes 14 timeouts 0, SG min/max 0/0
                    Driver 1: standstill, reads 22474, writes 14 timeouts 0, SG min/max 0/0
                    Driver 2: standstill, reads 22475, writes 14 timeouts 0, SG min/max 0/0
                    Driver 3: standstill, reads 22475, writes 14 timeouts 0, SG min/max 0/0
                    Driver 4: standstill, reads 22478, writes 11 timeouts 0, SG min/max 0/0
                    Driver 5: standstill, reads 22479, writes 11 timeouts 0, SG min/max 0/0
                    Date/time: 2020-07-27 15:15:01
                    Slowest loop: 3.63ms; fastest: 0.14ms
                    === Storage ===
                    Free file entries: 10
                    SD card 0 not detected, interface speed: 37.5MBytes/sec
                    SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                    === Move ===
                    Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                    Bed compensation in use: none, comp offset 0.000
                    === MainDDARing ===
                    Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                    === AuxDDARing ===
                    Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                    === Heat ===
                    Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                    === GCodes ===
                    Segments left: 0
                    Movement lock held by null
                    HTTP* is ready with "M122" in state(s) 0
                    Telnet is idle in state(s) 0
                    File is idle in state(s) 0
                    USB is idle in state(s) 0
                    Aux is idle in state(s) 0
                    Trigger* is idle in state(s) 0
                    Queue is idle in state(s) 0
                    LCD is idle in state(s) 0
                    SBC is idle in state(s) 0
                    Daemon* is idle in state(s) 0
                    Aux2 is idle in state(s) 0
                    Autopause is idle in state(s) 0
                    Code queue is empty.
                    === Network ===
                    Slowest loop: 1.02ms; fastest: 0.01ms
                    Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                    HTTP sessions: 0 of 8

                    • Ethernet -
                      State: disabled
                      Error counts: 0 0 0 0 0
                      Socket states: 0 0 0 0 0 0 0 0
                      === CAN ===
                      Messages sent 72, longest wait 0ms for type 0
                      === Linux interface ===
                      State: 0, failed transfers: 0
                      Last transfer: 18ms ago
                      RX/TX seq numbers: 583/584
                      SPI underruns 0, overruns 0
                      Number of disconnects: 0
                      Buffer RX/TX: 0/0-0
                      === Duet Control Server ===
                      Duet Control Server v3.1.1
                      Code buffer space: 4096
                      Configured SPI speed: 8000000 Hz
                      Full transfers per second: 30.27
                    1 Reply Last reply Reply Quote 0
                    • dc42undefined
                      dc42 administrators
                      last edited by

                      Thanks. Please try commanding the motors to move (without any motors connected) and repeat that. I am looking for the driver status to change.

                      Duet WiFi hardware designer and firmware engineer
                      Please do not ask me for Duet support via PM or email, use the forum
                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                      Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                      • Touchthebitumundefined
                        Touchthebitum @dc42
                        last edited by

                        @dc42

                        Error: short-to-ground reported by driver(s) 0 1
                        27/07/2020 à 21:40:14 m122
                        === Diagnostics ===
                        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                        Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                        Used output buffers: 1 of 40 (10 max)
                        === RTOS ===
                        Static ram: 154604
                        Dynamic ram: 162592 of which 44 recycled
                        Exception stack ram used: 280
                        Never used ram: 75696
                        Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1452) TMC(blocked,68) MAIN(running,4952) IDLE(ready,76)
                        Owned mutexes:
                        === Platform ===
                        Last reset 00:00:47 ago, cause: power up
                        Last software reset at 2020-07-27 15:14, reason: User, spinning module LinuxInterface, available RAM 75704 bytes (slot 0)
                        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                        Error status: 0
                        MCU temperature: min 20.8, current 29.0, max 29.1
                        Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                        12V rail voltage: min 12.1, current 12.1, max 12.1, under voltage events: 0
                        Driver 0: short-to-ground standstill, reads 39652, writes 17 timeouts 0, SG min/max 0/0
                        Driver 1: short-to-ground standstill, reads 39652, writes 17 timeouts 0, SG min/max 0/63
                        Driver 2: standstill, reads 39656, writes 14 timeouts 0, SG min/max 0/0
                        Driver 3: standstill, reads 39656, writes 14 timeouts 0, SG min/max 0/0
                        Driver 4: standstill, reads 39660, writes 11 timeouts 0, SG min/max 0/0
                        Driver 5: standstill, reads 39660, writes 11 timeouts 0, SG min/max 0/0
                        Date/time: 2020-07-27 20:36:50
                        Slowest loop: 3.82ms; fastest: 0.14ms
                        === Storage ===
                        Free file entries: 10
                        SD card 0 not detected, interface speed: 37.5MBytes/sec
                        SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                        === Move ===
                        Hiccups: 0(0), FreeDm: 375, MinFreeDm: 373, MaxWait: 34018ms
                        Bed compensation in use: none, comp offset 0.000
                        === MainDDARing ===
                        Scheduled moves: 1, completed moves: 1, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                        === AuxDDARing ===
                        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                        === Heat ===
                        Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                        === GCodes ===
                        Segments left: 0
                        Movement lock held by null
                        HTTP* is ready with "M122" in state(s) 0
                        Telnet is idle in state(s) 0
                        File is idle in state(s) 0
                        USB is idle in state(s) 0
                        Aux is idle in state(s) 0
                        Trigger* is idle in state(s) 0
                        Queue is idle in state(s) 0
                        LCD is idle in state(s) 0
                        SBC is idle in state(s) 0
                        Daemon* is idle in state(s) 0
                        Aux2 is idle in state(s) 0
                        Autopause is idle in state(s) 0
                        Code queue is empty.
                        === Network ===
                        Slowest loop: 0.88ms; fastest: 0.01ms
                        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                        HTTP sessions: 0 of 8

                        • Ethernet -
                          State: disabled
                          Error counts: 0 0 0 0 0
                          Socket states: 0 0 0 0 0 0 0 0
                          === CAN ===
                          Messages sent 100, longest wait 0ms for type 0
                          === Linux interface ===
                          State: 0, failed transfers: 0
                          Last transfer: 17ms ago
                          RX/TX seq numbers: 808/809
                          SPI underruns 0, overruns 0
                          Number of disconnects: 0
                          Buffer RX/TX: 0/0-0
                          === Duet Control Server ===
                          Duet Control Server v3.1.1
                          Code buffer space: 4096
                          Configured SPI speed: 8000000 Hz
                          Full transfers per second: 3.50
                        1 Reply Last reply Reply Quote 0
                        • percybundefined
                          percyb
                          last edited by

                          I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)" on all drive ports with what were working stepper motors. Only possible mistake i made is connect one stepper motor to 3 pins instead of 4 ie offset one pin. Would this cause all drivers to die?

                          Touchthebitumundefined A Former User? 2 Replies Last reply Reply Quote 0
                          • Touchthebitumundefined
                            Touchthebitum @percyb
                            last edited by

                            @percyb said in Short to ground on drivers 0123:

                            I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)" on all drive ports with what were working stepper motors. Only possible mistake i made is connect one stepper motor to 3 pins instead of 4 ie offset one pin. Would this cause all drivers to die?

                            Impossible because I tested all phases before plugging motor and I checked if these big crimps went on the right place when connectind them on the Duet,

                            1 Reply Last reply Reply Quote 0
                            • A Former User?
                              A Former User @percyb
                              last edited by A Former User

                              @percyb said in Short to ground on drivers 0123:

                              I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)"

                              ref https://forum.duet3d.com/post/100507 and you should probably start your own topic if the error persist after disconnecting your motors (when powered down ofc)

                              Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                              • Touchthebitumundefined
                                Touchthebitum @A Former User
                                last edited by

                                @bearer said in Short to ground on drivers 0123:

                                @percyb said in Short to ground on drivers 0123:

                                I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)"

                                ref https://forum.duet3d.com/post/100507 and you should probably start your own topic if the error persist after disconnecting your motors (when powered down ofc)

                                I think we should think about a warranty process. I don't know what to add to the discussion. I repeat, it is not the first printer I build and I'm aware of risks. Before this Duet3 I used a Duet2 and was perfect (no errors messages) with the same motors. This board never worked and I directly plugged the SAME motors that I plugged to my Duet2. So there is a problem.
                                My shop told me to see with this forum, what I did.
                                Now, I choosed a Genuine board because I believe in the right intelectual properties and know-how.
                                Please, give me a clear answer and we can go on.
                                Thanks

                                A Former User? T3P3Tonyundefined 2 Replies Last reply Reply Quote 0
                                • A Former User?
                                  A Former User @Touchthebitum
                                  last edited by

                                  @Touchthebitum said in Short to ground on drivers 0123:

                                  @bearer said in Short to ground on drivers 0123:

                                  @percyb said in Short to ground on drivers 0123:

                                  I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)"

                                  ref https://forum.duet3d.com/post/100507 and you should probably start your own topic if the error persist after disconnecting your motors (when powered down ofc)

                                  I think we should think about a warranty process.

                                  that was not directed at you; I'm sure dc42 is trying to evaluate the information you've provided already

                                  Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                                  • Touchthebitumundefined
                                    Touchthebitum @A Former User
                                    last edited by

                                    @bearer said in Short to ground on drivers 0123:

                                    @Touchthebitum said in Short to ground on drivers 0123:

                                    @bearer said in Short to ground on drivers 0123:

                                    @percyb said in Short to ground on drivers 0123:

                                    I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)"

                                    ref https://forum.duet3d.com/post/100507 and you should probably start your own topic if the error persist after disconnecting your motors (when powered down ofc)

                                    I think we should think about a warranty process.

                                    that was not directed at you; I'm sure dc42 is trying to evaluate the information you've provided already

                                    Thanks 😉

                                    1 Reply Last reply Reply Quote 0
                                    • T3P3Tonyundefined
                                      T3P3Tony administrators @Touchthebitum
                                      last edited by

                                      @Touchthebitum

                                      Thanks for your patience, DC42 is away right now but I can help.

                                      Looking at your latest M122 report it looks like driver 01 and 1 are damaged. its not completely clear if 2 and 3 are damaged - the motors connected to those ones could have an issue.

                                      Can you try the following please

                                      1. check the wiring of one of your stepper with a voltmeter. they should be wired in two pairs, 1-2 and 3-4 (i.e. pin 1 to 2 should read a few Ohms, pin 3 to 4 should read a few ohms but there should be no connection between pin the pairs).

                                      2. with just that motor you have check tried it plugged into Driver 2, command a movement, send M122 and see what it says, we are looking at this part:

                                      Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                                      12V rail voltage: min 12.1, current 12.1, max 12.1, under voltage events: 0
                                      Driver 0: short-to-ground standstill, reads 39652, writes 17 timeouts 0, SG min/max 0/0
                                      Driver 1: short-to-ground standstill, reads 39652, writes 17 timeouts 0, SG min/max 0/63
                                      Driver 2: standstill, reads 39656, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 3: standstill, reads 39656, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 4: standstill, reads 39660, writes 11 timeouts 0, SG min/max 0/0
                                      Driver 5: standstill, reads 39660, writes 11 timeouts 0, SG min/max 0/0
                                      
                                      1. Repeat for driver 3 and driver 4.

                                      Lets see those three excerpts from M122.

                                      www.duet3d.com

                                      Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                                      • Touchthebitumundefined
                                        Touchthebitum @T3P3Tony
                                        last edited by Touchthebitum

                                        @T3P3Tony

                                        Hello

                                        I tested pairs and got 2ohms on each pair and nothing between the two pairs
                                        For the moves of drivers 3-4 I made z move on the duet panel Due
                                        For the driver 4 , I don't have yet a connected extruder
                                        Error: short-to-ground reported by driver(s) 2
                                        28/07/2020 à 12:31:08 m122
                                        === Diagnostics ===
                                        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                        Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                                        Used output buffers: 1 of 40 (10 max)
                                        === RTOS ===
                                        Static ram: 154604
                                        Dynamic ram: 162592 of which 44 recycled
                                        Exception stack ram used: 376
                                        Never used ram: 75600
                                        Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,196) MAIN(running,4952) IDLE(ready,76)
                                        Owned mutexes:
                                        === Platform ===
                                        Last reset 00:01:08 ago, cause: power up
                                        Last software reset at 2020-07-27 15:14, reason: User, spinning module LinuxInterface, available RAM 75704 bytes (slot 0)
                                        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                        Error status: 0
                                        MCU temperature: min 20.6, current 29.8, max 29.9
                                        Supply voltage: min 24.0, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                                        12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                        Driver 0: standstill, reads 8684, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 1: standstill, reads 8684, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 2: short-to-ground standstill, reads 8681, writes 17 timeouts 0, SG min/max 0/8
                                        Driver 3: standstill, reads 8685, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 4: standstill, reads 8688, writes 11 timeouts 0, SG min/max 0/0
                                        Driver 5: standstill, reads 8689, writes 11 timeouts 0, SG min/max 0/0

                                        Error: short-to-ground reported by driver(s) 2
                                        28/07/2020 à 12:33:42 M122
                                        === Diagnostics ===
                                        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                        Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                                        Used output buffers: 1 of 40 (13 max)
                                        === RTOS ===
                                        Static ram: 154604
                                        Dynamic ram: 162592 of which 44 recycled
                                        Exception stack ram used: 360
                                        Never used ram: 75616
                                        Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1460) TMC(blocked,68) MAIN(running,4536) IDLE(ready,76)
                                        Owned mutexes:
                                        === Platform ===
                                        Last reset 00:01:04 ago, cause: power up
                                        Last software reset at 2020-07-27 15:14, reason: User, spinning module LinuxInterface, available RAM 75704 bytes (slot 0)
                                        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                        Error status: 0
                                        MCU temperature: min 32.1, current 32.5, max 32.6
                                        Supply voltage: min 23.9, current 24.0, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
                                        12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                        Driver 0: standstill, reads 56891, writes 0 timeouts 0, SG min/max not available
                                        Driver 1: standstill, reads 56890, writes 0 timeouts 0, SG min/max not available
                                        Driver 2: short-to-ground standstill, reads 56888, writes 2 timeouts 0, SG min/max not available
                                        Driver 3: standstill, reads 56890, writes 0 timeouts 0, SG min/max not available
                                        Driver 4: standstill, reads 56890, writes 0 timeouts 0, SG min/max not available
                                        Driver 5: standstill, reads 56890, writes 0 timeouts 0, SG min/max not available
                                        Date/time: 2020-07-28 11:33:45
                                        Slowest loop: 3.63ms; fastest: 0.21ms

                                        Driver number 4 : there is no extruder tool message

                                        1 Reply Last reply Reply Quote 0
                                        • T3P3Tonyundefined
                                          T3P3Tony administrators
                                          last edited by T3P3Tony

                                          Hi @Touchthebitum

                                          you will need to update your configuration temporarily to use the test motor on driver 3, and then again on driver 4 - use the M584 command in config.g:

                                          (To test driver 3) :
                                          M584 X0.0 Y0.1 Z0.3 E0.2 ; Temporary drive mapping to test driver 3 as Z

                                          (To test driver 4) :
                                          M584 X0.0 Y0.1 Z0.4 E0.2 ; Temporary drive mapping to test driver 4 as Z

                                          www.duet3d.com

                                          Touchthebitumundefined 2 Replies Last reply Reply Quote 0
                                          • Touchthebitumundefined
                                            Touchthebitum @T3P3Tony
                                            last edited by

                                            This post is deleted!
                                            1 Reply Last reply Reply Quote 0
                                            • First post
                                              Last post
                                            Unless otherwise noted, all forum content is licensed under CC-BY-SA