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    Error when setting up independent motor bed levelling on CoreXY

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    • equanimity8undefined
      equanimity8
      last edited by

      @mrehorstdmd Thanks for your thoughts. I'm familiar with your work and I value your opinion. The reason I'm trying to go with it in this way is that I wanted to experiment with belts instead of leadscrews on Z - I have certain parts on my hands and I'm trying to validate my premise using them, that's not meant to be a long-term solution.

      I'm still vexed by this error though, thus I welcome suggestions.

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      • sebkritikelundefined
        sebkritikel @equanimity8
        last edited by sebkritikel

        @equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:

        Hi all,

        I'm working on a CoreXY that uses piezo to home and bed level. The setup consists of three motors in total but since I ran out of drivers I want to connect two motors to the Z driver and one to the E1 driver, effectively performing bed leveling using two independent motors.

        I followed the documentation and read previous threads on the topic but I'm getting an error even though the setup seems logical to me, thus I think I'm skipping a step somewhere and that's what's throwing me off.

        Both when I try to AutoHome and run G32 I get the error

        g32
        Error: G0/G1: insufficient axes homed
        

        My config.g is:

        ;Independent motors leveling
        M584 X0 Y1 Z2:4 E3; two Z motors connected to driver outputs Z and E1
        M671 X105:105 Y0:150 S1 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis
        
        ; Endstops
        M574 X1 Y1 Z0 S0
        
        ; Z-Probe
        ;M558 P1 I1 R0.4 F300 X0 Y0 Z0
        M558 P8 H10 I1 R1 F600 X0 Y0 Z1
        G31 X0 Y0 Z-0.25 P600
        

        my bed.g is:

        M561 ; clear any bed transform
        
        G28 ; home
        G30 P0 X105 Y0 Z-99999 ; probe near a leadscrew, half way along Y axis
        G30 P1 X105 Y150 Z-99999 S2 ; probe near a leadscrew and calibrate 2 motors
        

        and my homeall.g is:

        ;Home X and Y
        G91                     	; relative positioning
        G1 Z5 F420 S2        		; Lower bed 5mm to ensure it is below the switch trigger height
        M913 X100 Y100	 		; set X Y motors to 50% of their normal current for homing
        G1 S1 X-375 Y-305 F600   	; course home X or Y
        G1 S1 X-375 F600              	; course home X
        G1 S1 Y-305 F600              	; course home Y
        G1 X5 Y5 F600             	; move away from the endstops
        G1 S1 X-10 F200           	; fine home X
        G1 S1 Y-10 F200               	; fine home Y
        G1 X5 Y5 F600  			; go to origin
        M913 X100 Y100	 		; set X Y motors to 100% of their normal current
        
        ;Home Z
        G90              ; absolute positioning
        G1 X30 Y30 F600  ; go to first probe point
        G30              ; home Z by probing the bed
        G91              ; relative positioning
        G1 Z5 F420       ; lift Z relative to current position
        G90              ; absolute positioning
        
        ;Load height map
        G29 S1
        

        Best!

        A small step, but can you place M400 directly before any M913 commands? I do see that you have both set to XC100 and Y100, perhaps while trouble shooting.

        https://forum.duet3d.com/topic/15952/release-3-01-rc10/62?_=1602439079914

        Could you also try using "home all" with G29 S1 commented out as a test?

        Also, which firmware version are you running?

        Large(ish?) IDEX - 6HC, 1HCL
        Stratasys Dimension 1200es to 6HC Conversion

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        • equanimity8undefined
          equanimity8
          last edited by equanimity8

          @sebkritikel Thanks for your suggestions! I have fixed the mistake you found in row 4 of homeall.g it and it has made no difference (it was working correctly like that before) - it's not something I have changed while trying to make the conversion happen. The way homeall.g looks is the exact way I used it before, I have made changes to only to bed.g and config.g but I added homeall.g too for completeness' sake. Further, I tried to execute homeall.g with and without M400 before M913 as well as with G29 S1 commented out and not and there is no change in behaviour.

          Other than that I run RRF 2.05.1. Not sure how I missed to mention that (facepalm).

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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            It's tilt correction with 2 motors rather than actual leveling, but that's fine.

            Can you post your full config.g and the results of M122 and M98 P"config.g"?

            Definitely have M400 before M913

            I don't see anything in your bed.g that would cause that insufficient axes homed error on 2.05.

            Both when I try to AutoHome and run G32 I get the error

            What do you mean by autohome?

            Z-Bot CoreXY Build | Thingiverse Profile

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            • equanimity8undefined
              equanimity8
              last edited by equanimity8

              @Phaedrux I concur, tilt correction is a more accurate term.

              The console output when I run M122 and M98 P"config.g" in succession:

              10/12/2020, 8:00:19 AM	M98 P"config.g"
              10/12/2020, 8:00:07 AM	M122
              === Diagnostics ===
              RepRapFirmware for Duet 2 WiFi/Ethernet version 2.05.1 running on Duet WiFi 1.02 or later
              Board ID: 08DDM-9FAM2-LW4SD-6J9DL-3S46L-K0XHW
              Used output buffers: 1 of 24 (6 max)
              === RTOS ===
              Static ram: 25712
              Dynamic ram: 93080 of which 476 recycled
              Exception stack ram used: 272
              Never used ram: 11532
              Tasks: NETWORK(ready,676) HEAT(blocked,1232) MAIN(running,3800) IDLE(ready,160)
              Owned mutexes:
              === Platform ===
              Last reset 00:00:43 ago, cause: power up
              Last software reset at 2020-10-11 22:12, reason: User, spinning module GCodes, available RAM 11156 bytes (slot 2)
              Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
              Error status: 0
              Free file entries: 10
              SD card 0 detected, interface speed: 20.0MBytes/sec
              SD card longest block write time: 0.0ms, max retries 0
              MCU temperature: min 21.3, current 25.9, max 26.5
              Supply voltage: min 11.9, current 12.0, max 12.1, under voltage events: 0, over voltage events: 0, power good: yes
              Driver 0: standstill, SG min/max not available
              Driver 1: standstill, SG min/max not available
              Driver 2: standstill, SG min/max not available
              Driver 3: standstill, SG min/max not available
              Driver 4: standstill, SG min/max not available
              Date/time: 2020-10-12 08:00:06
              Cache data hit count 107691558
              Slowest loop: 5.54ms; fastest: 0.06ms
              I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
              === Move ===
              Hiccups: 0, FreeDm: 160, MinFreeDm: 160, MaxWait: 0ms
              Bed compensation in use: none, comp offset 0.000
              === DDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
              === Heat ===
              Bed heaters = -1 -1 -1 -1, chamberHeaters = -1 -1
              === GCodes ===
              Segments left: 0
              Stack records: 1 allocated, 0 in use
              Movement lock held by null
              http is idle in state(s) 0
              telnet is idle in state(s) 0
              file is idle in state(s) 0
              serial is idle in state(s) 0
              aux is idle in state(s) 0
              daemon is idle in state(s) 0
              queue is idle in state(s) 0
              autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 15.73ms; fastest: 0.00ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
              HTTP sessions: 1 of 8
              - WiFi -
              Network state is running
              WiFi module is connected to access point 
              Failed messages: pending 0, notready 0, noresp 0
              WiFi firmware version 1.23
              WiFi MAC address 2c:3a:e8:0b:1c:bb
              WiFi Vcc 3.34, reset reason Turned on by main processor
              WiFi flash size 4194304, free heap 23440
              WiFi IP address 192.168.137.156
              WiFi signal strength -53dBm, reconnections 1, sleep mode modem
              Socket states: 0 0 0 0 0 0 0 0
              

              Also my full config.g:

              ; General preferences
              G90                            ; Send absolute coordinates...
              M83                            ; ...but relative extruder moves
              
              M667 S1                        ; Select CoreXY mode
              
              ; Network
              M550 PPrinter Extrusions	;machine name
              M552 S1				;start wifi module
              
              ; Drives
              M569 P0 S1                     ; Drive 0 
              M569 P1 S1                     ; Drive 1 
              M569 P2 S0                     ; Drive 2 
              M569 P3 S1                     ; Drive 3 
              M569 P4 S0                     ; Drive 4 
              M350 X16 Y16 Z16 E16 I1        ; Configure microstepping with interpolation
              M92 X80 Y80 Z80 E456         ; Set steps per mm
              M566 X900 Y900 Z1 E120        ; Set maximum instantaneous speed changes (mm/min)
              M203 X9000 Y9000 Z720 E1200    ; Set maximum speeds (mm/min)
              M201 X500 Y500 Z250 E250        ; Set accelerations (mm/s^2)
              M906 X1200 Y1200 Z2200 E1100 I0   ; Set motor currents (mA) and motor idle factor in per cent
              M84 S0                        ; Set idle timeout
              
              ; Axis Limits
              M208 X0 Y0 Z0 S1               ; Set axis minima
              M208 X210 Y150 Z150 S0         ; Set axis maxima
              
              ;Independent motors leveling
              M584 X0 Y1 Z2:4 E3; two Z motors connected to driver outputs Z and E1
              M671 X105:105 Y0:150 S1 ; leadscrews
               
              ; Endstops
              M574 X1 Y1 Z0 S0
               
              ; Z-Probe
              ;M558 P1 I1 R0.4 F300 X0 Y0 Z0
              M558 P8 H10 I1 R1 F600 X0 Y0 Z1
              G31 X0 Y0 Z-0.25 P600
              
              ; Heaters
              M140 H-1                       ; Disable heated bed
              M305 P1 T100000 B4138 C0 R4700 ; Set thermistor + ADC parameters for heater 1
              M143 H1 S280                   ; Set temperature limit for heater 1 to 280C
              
              ; Fans
              M106 P0 H-1			; set fan 1 to be gcode controlled
              M106 P2 S1 I0 T45 H1            ; Set fan 2 value, PWM signal inversion and frequency. Thermostatic control is turned off
              
              ; Tools
              M563 P0 D0 H1                  ; Define tool 0
              G10 P0 X0 Y0 Z0                ; Set tool 0 axis offsets
              G10 P0 R0 S0                   ; Set initial tool 0 active and standby temperatures to 0C
              

              By AutoHome I mean the Home All button in the Dashboard tab. I apologise, I got my RRF and Marlin terms mixed up.

              sebkritikelundefined 1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                Can you manually send each line of your homeall.g in the gcode console from an unhomed state and see where you get the error message?

                Z-Bot CoreXY Build | Thingiverse Profile

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                • sebkritikelundefined
                  sebkritikel @equanimity8
                  last edited by

                  @equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:

                  @Phaedrux I concur, tilt correction is a more accurate term.

                  Also my full config.g:

                  ; Drives
                  M569 P0 S1                     ; Drive 0 
                  M569 P1 S1                     ; Drive 1 
                  M569 P2 S0                     ; Drive 2 
                  M569 P3 S1                     ; Drive 3 
                  M569 P4 S0                     ; Drive 4 
                  M350 X16 Y16 Z16 E16 I1        ; Configure microstepping with interpolation
                  M92 X80 Y80 Z80 E456         ; Set steps per mm
                  M566 X900 Y900 Z1 E120        ; Set maximum instantaneous speed changes (mm/min)
                  M203 X9000 Y9000 Z720 E1200    ; Set maximum speeds (mm/min)
                  M201 X500 Y500 Z250 E250        ; Set accelerations (mm/s^2)
                  M906 X1200 Y1200 Z2200 E1100 I0   ; Set motor currents (mA) and motor idle factor in per cent
                  M84 S0                        ; Set idle timeout
                  
                  ; Axis Limits
                  M208 X0 Y0 Z0 S1               ; Set axis minima
                  M208 X210 Y150 Z150 S0         ; Set axis maxima
                  
                  ;Independent motors leveling
                  M584 X0 Y1 Z2:4 E3; two Z motors connected to driver outputs Z and E1
                  M671 X105:105 Y0:150 S1 ; leadscrews
                  

                  You have a M584 command after M350 and M906 commands, which is not recommended. M584 must come before any M350 or M906 commands. https://duet3d.dozuki.com/Wiki/Gcode#Section_M584_Set_drive_mapping

                  After that is fixed, definitely try running each line of homeall.g through the console to see where the issue is.

                  Large(ish?) IDEX - 6HC, 1HCL
                  Stratasys Dimension 1200es to 6HC Conversion

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                  • equanimity8undefined
                    equanimity8
                    last edited by

                    I've put the ;Independent motors leveling section right after the drivers assigning part of config.g and it has made no difference. As a side note, is there a resource I can follow about the recommended sequence of gcode and/or what are good practices when setting up firmware (kind of like M400 before M913 which was discussed above)?

                    I get the error on the "G1 Z5 F420 S2" line.

                    sebkritikelundefined Phaedruxundefined 2 Replies Last reply Reply Quote 0
                    • sebkritikelundefined
                      sebkritikel @equanimity8
                      last edited by

                      @equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:

                      I've put the ;Independent motors leveling section right after the drivers assigning part of config.g and it has made no difference. As a side note, is there a resource I can follow about the recommended sequence of gcode and/or what are good practices when setting up firmware (kind of like M400 before M913 which was discussed above)?

                      I think the M913 and M584 both have notes in the Duet GCODE Wiki saying what other commands to look out for (M913 is a little less clear when it comes to the note on M400). Many other commands have notes/dependencies for other commands.

                      I get the error on the "G1 Z5 F420 S2" line.

                      That... doesn't make sense why it would fail there? For kicks, could you try changing the S2 to H2 instead? For your application, and being on 2.05.1, S2 and H2 should function the same.

                      Large(ish?) IDEX - 6HC, 1HCL
                      Stratasys Dimension 1200es to 6HC Conversion

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                      • equanimity8undefined
                        equanimity8
                        last edited by

                        No change.

                        fcwiltundefined 1 Reply Last reply Reply Quote 0
                        • fcwiltundefined
                          fcwilt @equanimity8
                          last edited by

                          @equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:

                          No change.

                          As a test reboot your printer and enter that command (G1 Z5 H2 F420) in the DWC Console, just to be sure it is generating the "not homed" error.

                          Thanks.

                          Frederick

                          Printers: a small Utilmaker style, a small CoreXY and a E3D MS/TC setup. Various hotends. Using Duet 3 hardware running 3.4.6

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                          • Phaedruxundefined
                            Phaedrux Moderator @equanimity8
                            last edited by

                            @equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:

                            is there a resource I can follow about the recommended sequence of gcode and/or what are good practices when setting up firmware

                            Every gcode is documented here: https://duet3d.dozuki.com/Wiki/Gcode#main

                            It's a good idea to check the relevant gcodes when trouble shooting.

                            @equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:

                            I've put the ;Independent motors leveling section right after the drivers assigning part of config.g and it has made no difference.

                            How is your config.g laid out now? Can you post it again? The M584 should be above the M350.

                            The homing file you've posted is from the /system folder right?

                            Z-Bot CoreXY Build | Thingiverse Profile

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                            • equanimity8undefined
                              equanimity8
                              last edited by equanimity8

                              @fcwilt When I start with (G1 Z5 H2 F420) as per your suggestions I get a little but further, namely to G1 X5 Y5 F600 (line 8 in homeall.g) and I get the same error (Error: G0/G1: insufficient axes homed).

                              @Phaedrux The current config.g:

                              ; General preferences
                              G90                            ; Send absolute coordinates...
                              M83                            ; ...but relative extruder moves
                              
                              M667 S1                        ; Select CoreXY mode
                              
                              ; Network
                              M550 PPrinter Extrusions	;machine name
                              M552 S1				;start wifi module
                              
                              ; Drives
                              M569 P0 S1                     ; Drive 0 goes forwards
                              M569 P1 S1                     ; Drive 1 goes forwards
                              M569 P2 S0                     ; Drive 2 goes forwards
                              M569 P3 S1                     ; Drive 3 goes forwards
                              M569 P4 S0                     ; Drive 4 goes forwards
                              
                              ;Independent motors leveling
                              M584 X0 Y1 Z2:4 E3; two Z motors connected to driver outputs Z and E1
                              M671 X105:105 Y0:150 S1 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis
                              
                              M350 X16 Y16 Z16 E16 I1        ; Configure microstepping with interpolation
                              M92 X80 Y80 Z80 E456         ; Set steps per mm
                              M566 X900 Y900 Z1 E120        ; Set maximum instantaneous speed changes (mm/min)
                              M203 X9000 Y9000 Z720 E1200    ; Set maximum speeds (mm/min)
                              M201 X500 Y500 Z250 E250        ; Set accelerations (mm/s^2)
                              M906 X1200 Y1200 Z2200 E1100 I0   ; Set motor currents (mA) and motor idle factor in per cent
                              M84 S0                        ; Set idle timeout
                              
                              ; Axis Limits
                              M208 X0 Y0 Z0 S1               ; Set axis minima
                              M208 X210 Y150 Z150 S0         ; Set axis maxima
                               
                              ; Endstops
                              M574 X1 Y1 Z0 S0
                               
                              ; Z-Probe
                              ;M558 P1 I1 R0.4 F300 X0 Y0 Z0
                              M558 P8 H10 I1 R1 F600 X0 Y0 Z1
                              G31 X0 Y0 Z-0.25 P600
                              
                              ; Heaters
                              M140 H-1                       ; Disable heated bed
                              M305 P1 T100000 B4138 C0 R4700 ; Set thermistor + ADC parameters for heater 1
                              M143 H1 S280                   ; Set temperature limit for heater 1 to 280C
                              
                              ; Fans
                              M106 P0 H-1			; set fan 1 to be gcode controlled
                              M106 P2 S1 I0 T45 H1            ; Set fan 2 value, PWM signal inversion and frequency. Thermostatic control is turned off
                              
                              ; Tools
                              M563 P0 D0 H1                  ; Define tool 0
                              G10 P0 X0 Y0 Z0                ; Set tool 0 axis offsets
                              G10 P0 R0 S0                   ; Set initial tool 0 active and standby temperatures to 0C
                              

                              Everything that I've pasted is indeed from the System tab under File Management in DWC.

                              fcwiltundefined 1 Reply Last reply Reply Quote 0
                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by Phaedrux

                                It really seems like your endstops are not actually working.

                                Can you confirm what firmware version is installed with M115?

                                And then can you confirm that the status of the endstops changes when you click them by checking with M119?

                                Earlier when you send M98 P"config.g" it didn't seem to echo anything back. Can you try again? There should be at least some response.

                                Z-Bot CoreXY Build | Thingiverse Profile

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                                • equanimity8undefined
                                  equanimity8
                                  last edited by equanimity8

                                  The result of M115:

                                  M115
                                  FIRMWARE_NAME: RepRapFirmware for Duet 2 WiFi/Ethernet FIRMWARE_VERSION: 2.05.1 ELECTRONICS: Duet WiFi 1.02 or later FIRMWARE_DATE: 2020-02-09b
                                  

                                  M119 correctly reports X and Y endstops (first/bottom is homed; then/middle is not; last/top is not for X and Y but I was tapping the nozzle to trigger the piezo):

                                  M119
                                  Endstops - X: not stopped, Y: not stopped, Z: not stopped, Z probe: at min stop
                                  M119
                                  Endstops - X: not stopped, Y: not stopped, Z: not stopped, Z probe: not stopped
                                  M119
                                  Endstops - X: at min stop, Y: at min stop, Z: not stopped, Z probe: not stopped
                                  

                                  No echo on M98 P"config.g" only green background on the message.

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                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    I guess your config.g is stripped down enough that some of the usual things like showing HTTP and FTP enabled etc aren't present, so there's nothing getting echoed.

                                    Can you try adding M117 "Loading Config" to the end of config.g and when you save and reboot and send M98 P"config.g" again it should at least echo that.

                                    Ok it looks like endstops are reporting correctly.

                                    Z-Bot CoreXY Build | Thingiverse Profile

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                                    • Phaedruxundefined
                                      Phaedrux Moderator
                                      last edited by

                                      ;Home X and Y
                                      G91                     	; relative positioning
                                      G1 Z5 F420 H2        		; Lower bed 5mm to ensure it is below the switch trigger height
                                      M400
                                      M913 X50 Y50	 		; set X Y motors to 50% of their normal current for homing
                                      G1 H1 X-375 Y-305 F600   	; course home X or Y
                                      G1 H1 X-375 F600              	; course home X
                                      G1 H1 Y-305 F600              	; course home Y
                                      G1 X5 Y5 F600             	; move away from the endstops
                                      G1 H1 X-10 F200           	; fine home X
                                      G1 H1 Y-10 F200               	; fine home Y
                                      G1 X5 Y5 F600  			; go to origin
                                      M400
                                      M913 X100 Y100	 		; set X Y motors to 100% of their normal current
                                       
                                      ;Home Z
                                      G90              ; absolute positioning
                                      G1 X30 Y30 F600  ; go to first probe point
                                      G30              ; home Z by probing the bed
                                      G91              ; relative positioning
                                      G1 Z5 F420       ; lift Z relative to current position
                                      G90              ; absolute positioning
                                       
                                      ;Load height map
                                      G29 S1
                                      

                                      Does your homeall match that now after the corrections?

                                      Z-Bot CoreXY Build | Thingiverse Profile

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                                      • equanimity8undefined
                                        equanimity8
                                        last edited by equanimity8

                                        When I run M98 P"config.g" I get no new messages in the console but I see a "Loading config" floating message in the bottom right part of DWC.

                                        My homeall wasn't matching what you have laid out. The difference was the H1 instead of S1. In any case, there is no change - same behaviour and error. For the sake of completeness I ran that line by line as well and it again fails on G1 X5 Y5 F600 with Error: G0/G1: insufficient axes homed.

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                                        • fcwiltundefined
                                          fcwilt @equanimity8
                                          last edited by

                                          @equanimity8 said in Error when setting up independent motor bed levelling on CoreXY:

                                          @fcwilt When I start with (G1 Z5 H2 F420) as per your suggestions I get a little but further, namely to G1 X5 Y5 F600 (line 8 in homeall.g) and I get the same error (Error: G0/G1: insufficient axes homed).

                                          I don't understand what you mean by "get a little further"?

                                          I just wanted you to execute that one command from the DWC console right after a reboot BEFORE doing anything else.

                                          Frederick

                                          Printers: a small Utilmaker style, a small CoreXY and a E3D MS/TC setup. Various hotends. Using Duet 3 hardware running 3.4.6

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                                          • equanimity8undefined
                                            equanimity8
                                            last edited by

                                            By a little bit further I mean that I manage to execute more lines compared than before i.e. a bit further down the list of lines. I might have misunderstood you then. The (G1 Z5 H2 F420) command executes fine and I'm able to get to G1 X5 Y5 F600 (line 8 in homeall.g) before I get the error.

                                            fcwiltundefined Phaedruxundefined 2 Replies Last reply Reply Quote 0
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