Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    Duet 3 SBC DCS has stopped

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
    8
    80
    4.5k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • dhusoloundefined
      dhusolo @Phaedrux
      last edited by

      @Phaedrux Correct. Just making sure I'm doing it right, Is there a different way to erase the firmware on the board besides the erase jumpers or would even using a different SD card do the trick?

      1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        Well you normally don't need to erase the firmware, but yes the jumper is the way to do that. Once erased you will need to use usb to flash a firmware again.

        A different SD card won't help since the firmware is flashed to the board itself. The firmware bin file on the sd card is just there for storage during in place flashing.

        What version is flashed to the duet right now?
        What version is the Pi running?

        If you're completely back on 3.1.1 right now, are you on the unstable branch for apt-update? How did you originally try to update to the beta?

        Z-Bot CoreXY Build | Thingiverse Profile

        dhusoloundefined 1 Reply Last reply Reply Quote 0
        • dhusoloundefined
          dhusolo @Phaedrux
          last edited by

          @Phaedrux I think I got it back to 3.1.1.

          What's the command to verify version info including DWS and DWC?

          1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator
            last edited by Phaedrux

            From the gcode console send M122 and post the results please.

            Additionally send M122 "DSF"

            Z-Bot CoreXY Build | Thingiverse Profile

            1 Reply Last reply Reply Quote 0
            • dhusoloundefined
              dhusolo
              last edited by

              I haven't loaded my config file but I flashed Duet3Firmware_MB6HC.bin through Bossa. It looks like it's communicating with the RPI again.

              M122

              m122
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
              Used output buffers: 1 of 40 (10 max)
              === RTOS ===
              Static ram: 154604
              Dynamic ram: 161360 of which 20 recycled
              Exception stack ram used: 236
              Never used ram: 76996
              Tasks: NETWORK(ready,1980) HEAT(blocked,1452) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(suspended,252) MAIN(running,5184) IDLE(ready,76)
              Owned mutexes:
              === Platform ===
              Last reset 00:09:59 ago, cause: power up
              Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
              Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
              Error status: 0
              MCU temperature: min 15.0, current 25.8, max 25.9
              Supply voltage: min 0.2, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
              12V rail voltage: min 0.1, current 0.1, max 0.2, under voltage events: 0
              Driver 0: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 1: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 2: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 3: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 4: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Driver 5: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
              Date/time: 2020-11-08 14:26:06
              Slowest loop: 2.36ms; fastest: 0.13ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
              Bed compensation in use: none, comp offset 0.000
              === MainDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
              === AuxDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
              === Heat ===
              Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is ready with "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon* is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 1.03ms; fastest: 0.01ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
              HTTP sessions: 0 of 8
              - Ethernet -
              State: disabled
              Error counts: 0 0 0 0 0
              Socket states: 0 0 0 0 0 0 0 0
              === CAN ===
              Messages sent 0, longest wait 0ms for type 0
              === Linux interface ===
              State: 0, failed transfers: 0
              Last transfer: 12ms ago
              RX/TX seq numbers: 19460/19461
              SPI underruns 0, overruns 0
              Number of disconnects: 0
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.1.1
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 5.64
              

              M122 DSF

              m122 DSF
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
              Used output buffers: 1 of 40 (12 max)
              === RTOS ===
              Static ram: 154604
              Dynamic ram: 161360 of which 20 recycled
              Exception stack ram used: 236
              Never used ram: 76996
              Tasks: NETWORK(ready,1980) HEAT(blocked,1452) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(suspended,252) MAIN(running,4512) IDLE(ready,76)
              Owned mutexes:
              === Platform ===
              Last reset 00:12:41 ago, cause: power up
              Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
              Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
              Error status: 0
              MCU temperature: min 25.6, current 25.8, max 26.0
              Supply voltage: min 0.3, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
              12V rail voltage: min 0.1, current 0.2, max 0.2, under voltage events: 0
              Driver 0: ok, reads 0, writes 0 timeouts 0, SG min/max not available
              Driver 1: ok, reads 0, writes 0 timeouts 0, SG min/max not available
              Driver 2: ok, reads 0, writes 0 timeouts 0, SG min/max not available
              Driver 3: ok, reads 0, writes 0 timeouts 0, SG min/max not available
              Driver 4: ok, reads 0, writes 0 timeouts 0, SG min/max not available
              Driver 5: ok, reads 0, writes 0 timeouts 0, SG min/max not available
              Date/time: 2020-11-08 14:28:49
              Slowest loop: 1.97ms; fastest: 0.13ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
              Bed compensation in use: none, comp offset 0.000
              === MainDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
              === AuxDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
              === Heat ===
              Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is ready with "M122 D0 S0 F0" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon* is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 1.03ms; fastest: 0.01ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
              HTTP sessions: 0 of 8
              - Ethernet -
              State: disabled
              Error counts: 0 0 0 0 0
              Socket states: 0 0 0 0 0 0 0 0
              === CAN ===
              Messages sent 0, longest wait 0ms for type 0
              === Linux interface ===
              State: 0, failed transfers: 0
              Last transfer: 12ms ago
              RX/TX seq numbers: 24793/24794
              SPI underruns 0, overruns 0
              Number of disconnects: 0
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.1.1
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 32.80
              
              Phaedruxundefined 2 Replies Last reply Reply Quote 1
              • Phaedruxundefined
                Phaedrux Moderator @dhusolo
                last edited by

                @dhusolo said in Duet 3 SBC DCS has stopped:

                M122 DSF

                I think the quotes around DSF are required. I'll admit I haven't used that command yet.

                Z-Bot CoreXY Build | Thingiverse Profile

                dhusoloundefined 1 Reply Last reply Reply Quote 0
                • dhusoloundefined
                  dhusolo @Phaedrux
                  last edited by

                  @Phaedrux

                  m122 "DSF"
                  === Duet Control Server ===
                  Duet Control Server v3.1.1
                  Daemon:
                  Finishing macro daemon.g, started by system
                  > Next stack level
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 32.83
                  
                  1 Reply Last reply Reply Quote 0
                  • Phaedruxundefined
                    Phaedrux Moderator @dhusolo
                    last edited by

                    @dhusolo said in Duet 3 SBC DCS has stopped:

                    === Duet Control Server === Duet Control Server v3.1.1

                    Regardless, I think you're on 3.1.1 across the board now.

                    Z-Bot CoreXY Build | Thingiverse Profile

                    1 Reply Last reply Reply Quote 0
                    • dhusoloundefined
                      dhusolo
                      last edited by

                      but to your earlier question I tried updating to the beta following this and updating the source list to use unstable version

                      1 Reply Last reply Reply Quote 0
                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        Would you be willing to test beta 3 once again?

                        Z-Bot CoreXY Build | Thingiverse Profile

                        1 Reply Last reply Reply Quote 0
                        • dhusoloundefined
                          dhusolo
                          last edited by

                          Sure. Should I use the getting started link or manually flash? I've tried compiling the firmware myself but with no success which is why I used the instructions in the link

                          jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                          • jay_s_ukundefined
                            jay_s_uk @dhusolo
                            last edited by jay_s_uk

                            @dhusolo that should be all you need to follow to move over to the unstable branch.
                            There's no need to use the erase button to load the firmware as it will be updated as part of the upgrade process

                            Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                            1 Reply Last reply Reply Quote 1
                            • dhusoloundefined
                              dhusolo
                              last edited by

                              I thought i did it correct but I got this error

                              pi@duet3:~ $ sudo apt-get install duetsoftwareframework
                              Reading package lists... Done
                              Building dependency tree       
                              Reading state information... Done
                              The following additional packages will be installed:
                                duetcontrolserver duetruntime duetsd duettools duetwebcontrol duetwebserver
                                reprapfirmware
                              The following packages will be upgraded:
                                duetcontrolserver duetruntime duetsd duetsoftwareframework duettools
                                duetwebcontrol duetwebserver reprapfirmware
                              8 upgraded, 0 newly installed, 0 to remove and 118 not upgraded.
                              Need to get 34.0 MB of archives.
                              After this operation, 0 B of additional disk space will be used.
                              Do you want to continue? [Y/n] y
                              Get:1 https://pkg.duet3d.com unstable/armv7 armhf duetsoftwareframework armhf 3.2.0-beta3 [2,034 B]
                              Get:2 https://pkg.duet3d.com unstable/armv7 armhf duetsd all 1.1.0 [2,102 B]
                              Get:3 https://pkg.duet3d.com unstable/armv7 armhf duettools armhf 3.2.0-beta3 [62.2 kB]
                              Get:4 https://pkg.duet3d.com unstable/armv7 armhf duetcontrolserver armhf 3.2.0-beta3 [226 kB]
                              Get:5 https://pkg.duet3d.com unstable/armv7 armhf duetruntime armhf 3.2.0-beta3 [28.9 MB]
                              Get:6 https://pkg.duet3d.com unstable/armv7 armhf duetwebserver armhf 3.2.0-beta3 [83.9 kB]
                              Get:7 https://pkg.duet3d.com unstable/armv7 armhf duetwebcontrol all 3.2.0-beta3 [3,507 kB]
                              Get:8 https://pkg.duet3d.com unstable/armv7 armhf reprapfirmware all 3.2.0-beta3-1 [1,260 kB]
                              Fetched 34.0 MB in 19s (1,813 kB/s)                                           
                              Reading changelogs... Done
                              (Reading database ... 79179 files and directories currently installed.)
                              Preparing to unpack .../0-duetsoftwareframework_3.2.0-beta3_armhf.deb ...
                              Unpacking duetsoftwareframework (3.2.0-beta3) over (3.1.1) ...
                              Preparing to unpack .../1-duetsd_1.1.0_all.deb ...
                              Unpacking duetsd (1.1.0) over (1.0.6) ...
                              Preparing to unpack .../2-duettools_3.2.0-beta3_armhf.deb ...
                              Unpacking duettools (3.2.0-beta3) over (3.1.1) ...
                              Preparing to unpack .../3-duetcontrolserver_3.2.0-beta3_armhf.deb ...
                              Unpacking duetcontrolserver (3.2.0-beta3) over (3.1.1) ...
                              Preparing to unpack .../4-duetruntime_3.2.0-beta3_armhf.deb ...
                              Unpacking duetruntime (3.2.0-beta3) over (3.1.1) ...
                              Preparing to unpack .../5-duetwebserver_3.2.0-beta3_armhf.deb ...
                              Unpacking duetwebserver (3.2.0-beta3) over (3.1.0) ...
                              Preparing to unpack .../6-duetwebcontrol_3.2.0-beta3_all.deb ...
                              Unpacking duetwebcontrol (3.2.0-beta3) over (3.1.1) ...
                              Preparing to unpack .../7-reprapfirmware_3.2.0-beta3-1_all.deb ...
                              Unpacking reprapfirmware (3.2.0-beta3-1) over (3.1.1-1) ...
                              Setting up duetruntime (3.2.0-beta3) ...
                              Setting up duetcontrolserver (3.2.0-beta3) ...
                              Installing new version of config file /opt/dsf/conf/config.json ...
                              Creating group dsf with gid 995.
                              Creating user dsf (n/a) with uid 995 and gid 995.
                              Setting up duettools (3.2.0-beta3) ...
                              Setting up duetwebserver (3.2.0-beta3) ...
                              Setting up duetsoftwareframework (3.2.0-beta3) ...
                              To modify config files consider adding yourself to the dsf groupd: # usermod -a -G dsf <username>
                              Setting up duetwebcontrol (3.2.0-beta3) ...
                              Setting up duetsd (1.1.0) ...
                              Setting up reprapfirmware (3.2.0-beta3-1) ...
                              Sending update request to DCS... Error: Failed to send update request
                              Unhandled exception. System.Threading.Tasks.TaskCanceledException: A task was canceled.
                                 at DuetAPIClient.BaseConnection.PerformCommand[T](BaseCommand command, CancellationToken cancellationToken) in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetAPIClient/BaseConnection.cs:line 188
                                 at DuetControlServer.Program.CheckForAnotherInstance() in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetControlServer/Program.cs:line 305
                                 at DuetControlServer.Program.Main(String[] args) in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetControlServer/Program.cs:line 84
                                 at DuetControlServer.Program.<Main>(String[] args)
                              
                              
                              jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                              • jay_s_ukundefined
                                jay_s_uk @dhusolo
                                last edited by jay_s_uk

                                @dhusolo
                                Are you still able to connect to the board via DWC?
                                If you can confirm the firmware version using 3.1.1
                                If it's still 3.1.1, send M997 B0
                                I would be interested to see if you get any errors reported

                                Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                dhusoloundefined 1 Reply Last reply Reply Quote 0
                                • dhusoloundefined
                                  dhusolo @jay_s_uk
                                  last edited by

                                  @jay_s_uk
                                  I had to start DCS and DWS manually but I was able to get to the web interface.

                                  M122 "DSF"
                                  === Duet Control Server ===
                                  Duet Control Server v3.2.0-beta3
                                  Code buffer space: 4096
                                  Configured SPI speed: 8000000 Hz
                                  Full transfers per second: 32.68
                                  11/8/2020, 2:58:59 PM```	
                                  
                                  M122
                                  === Diagnostics ===
                                  RepRapFirmware for Duet 3 MB6HC version 3.2-beta3 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                  Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                                  Used output buffers: 1 of 40 (10 max)
                                  === RTOS ===
                                  Static ram: 122124
                                  Dynamic ram: 137508 of which 0 recycled
                                  Never used RAM 132560, free system stack 185 words
                                  Tasks: Linux(ready,131) HEAT(blocked,362) CanReceiv(blocked,948) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,66) MAIN(running,1300) IDLE(ready,19)
                                  Owned mutexes: HTTP(MAIN)
                                  === Platform ===
                                  Last reset 00:09:17 ago, cause: software
                                  Last software reset details not available
                                  Error status: 0x00
                                  MCU temperature: min 25.3, current 26.2, max 26.4
                                  Supply voltage: min 0.3, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
                                  12V rail voltage: min 0.1, current 0.2, max 0.2, under voltage events: 0
                                  Driver 0: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                  Driver 1: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                  Driver 2: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                  Driver 3: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                  Driver 4: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                  Driver 5: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                  Date/time: 2020-11-08 14:58:59
                                  Slowest loop: 743.08ms; fastest: 0.16ms
                                  === Storage ===
                                  Free file entries: 10
                                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                  === Move ===
                                  Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                                  Bed compensation in use: none, comp offset 0.000
                                  === MainDDARing ===
                                  Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                  === AuxDDARing ===
                                  Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                  === Heat ===
                                  Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                  === GCodes ===
                                  Segments left: 0
                                  Movement lock held by null
                                  HTTP* is doing "M122" in state(s) 0
                                  Telnet is idle in state(s) 0
                                  File is idle in state(s) 0
                                  USB is idle in state(s) 0
                                  Aux is idle in state(s) 0
                                  Trigger* is idle in state(s) 0
                                  Queue is idle in state(s) 0
                                  LCD is idle in state(s) 0
                                  SBC is idle in state(s) 0
                                  Daemon is idle in state(s) 0
                                  Aux2 is idle in state(s) 0
                                  Autopause is idle in state(s) 0
                                  Code queue is empty.
                                  === CAN ===
                                  Messages sent 0, send timeouts 0, longest wait 0ms for type 0, free CAN buffers 47
                                  === SBC interface ===
                                  State: 0, failed transfers: 1
                                  Last transfer: 14ms ago
                                  RX/TX seq numbers: 17902/17903
                                  SPI underruns 0, overruns 0
                                  Number of disconnects: 0, IAP RAM available 0x20aa0
                                  Buffer RX/TX: 0/0-0
                                  === Duet Control Server ===
                                  Duet Control Server v3.2.0-beta3
                                  Code buffer space: 4096
                                  Configured SPI speed: 8000000 Hz
                                  Full transfers per second: 32.56
                                  
                                  jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                                  • jay_s_ukundefined
                                    jay_s_uk @dhusolo
                                    last edited by

                                    @dhusolo well at least you're back on the latest firmware.
                                    @chrishamm any comments on the error above whilst updating?

                                    Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                    1 Reply Last reply Reply Quote 0
                                    • dhusoloundefined
                                      dhusolo
                                      last edited by

                                      More of a status update: I've started the same print again but I don't load any filament. I didn't want to waste the filament if it's going to cancel on me again.

                                      However I can now hear some strange jerky movements. I have a coreXY so it's hard to narrow down what stepper it's coming from especially since there's no filament going through it.

                                      Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                      • oliofundefined
                                        oliof
                                        last edited by

                                        I think my recent post about issues with 3.2b3 are very similar to this issue.

                                        <>RatRig V-Minion Fly Super5Pro RRF<> V-Core 3.1 IDEX k*****r <> RatRig V-Minion SKR 2 Marlin<>

                                        1 Reply Last reply Reply Quote 2
                                        • Phaedruxundefined
                                          Phaedrux Moderator @dhusolo
                                          last edited by

                                          @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                                          Z-Bot CoreXY Build | Thingiverse Profile

                                          A Former User? dhusoloundefined 2 Replies Last reply Reply Quote 0
                                          • A Former User?
                                            A Former User @Phaedrux
                                            last edited by

                                            @Phaedrux said in Duet 3 SBC DCS has stopped:

                                            @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                                            Oh the irony.....

                                            Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                            • First post
                                              Last post
                                            Unless otherwise noted, all forum content is licensed under CC-BY-SA