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    Duet 3 SBC DCS has stopped

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      Well you normally don't need to erase the firmware, but yes the jumper is the way to do that. Once erased you will need to use usb to flash a firmware again.

      A different SD card won't help since the firmware is flashed to the board itself. The firmware bin file on the sd card is just there for storage during in place flashing.

      What version is flashed to the duet right now?
      What version is the Pi running?

      If you're completely back on 3.1.1 right now, are you on the unstable branch for apt-update? How did you originally try to update to the beta?

      Z-Bot CoreXY Build | Thingiverse Profile

      dhusoloundefined 1 Reply Last reply Reply Quote 0
      • dhusoloundefined
        dhusolo @Phaedrux
        last edited by

        @Phaedrux I think I got it back to 3.1.1.

        What's the command to verify version info including DWS and DWC?

        1 Reply Last reply Reply Quote 0
        • Phaedruxundefined
          Phaedrux Moderator
          last edited by Phaedrux

          From the gcode console send M122 and post the results please.

          Additionally send M122 "DSF"

          Z-Bot CoreXY Build | Thingiverse Profile

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          • dhusoloundefined
            dhusolo
            last edited by

            I haven't loaded my config file but I flashed Duet3Firmware_MB6HC.bin through Bossa. It looks like it's communicating with the RPI again.

            M122

            m122
            === Diagnostics ===
            RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
            Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
            Used output buffers: 1 of 40 (10 max)
            === RTOS ===
            Static ram: 154604
            Dynamic ram: 161360 of which 20 recycled
            Exception stack ram used: 236
            Never used ram: 76996
            Tasks: NETWORK(ready,1980) HEAT(blocked,1452) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(suspended,252) MAIN(running,5184) IDLE(ready,76)
            Owned mutexes:
            === Platform ===
            Last reset 00:09:59 ago, cause: power up
            Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
            Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
            Error status: 0
            MCU temperature: min 15.0, current 25.8, max 25.9
            Supply voltage: min 0.2, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
            12V rail voltage: min 0.1, current 0.1, max 0.2, under voltage events: 0
            Driver 0: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
            Driver 1: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
            Driver 2: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
            Driver 3: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
            Driver 4: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
            Driver 5: ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
            Date/time: 2020-11-08 14:26:06
            Slowest loop: 2.36ms; fastest: 0.13ms
            === Storage ===
            Free file entries: 10
            SD card 0 not detected, interface speed: 37.5MBytes/sec
            SD card longest read time 0.0ms, write time 0.0ms, max retries 0
            === Move ===
            Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
            Bed compensation in use: none, comp offset 0.000
            === MainDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
            === AuxDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
            === Heat ===
            Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP* is ready with "M122" in state(s) 0
            Telnet is idle in state(s) 0
            File is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger* is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            SBC is idle in state(s) 0
            Daemon* is idle in state(s) 0
            Aux2 is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === Network ===
            Slowest loop: 1.03ms; fastest: 0.01ms
            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
            HTTP sessions: 0 of 8
            - Ethernet -
            State: disabled
            Error counts: 0 0 0 0 0
            Socket states: 0 0 0 0 0 0 0 0
            === CAN ===
            Messages sent 0, longest wait 0ms for type 0
            === Linux interface ===
            State: 0, failed transfers: 0
            Last transfer: 12ms ago
            RX/TX seq numbers: 19460/19461
            SPI underruns 0, overruns 0
            Number of disconnects: 0
            Buffer RX/TX: 0/0-0
            === Duet Control Server ===
            Duet Control Server v3.1.1
            Code buffer space: 4096
            Configured SPI speed: 8000000 Hz
            Full transfers per second: 5.64
            

            M122 DSF

            m122 DSF
            === Diagnostics ===
            RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
            Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
            Used output buffers: 1 of 40 (12 max)
            === RTOS ===
            Static ram: 154604
            Dynamic ram: 161360 of which 20 recycled
            Exception stack ram used: 236
            Never used ram: 76996
            Tasks: NETWORK(ready,1980) HEAT(blocked,1452) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(suspended,252) MAIN(running,4512) IDLE(ready,76)
            Owned mutexes:
            === Platform ===
            Last reset 00:12:41 ago, cause: power up
            Last software reset at 2020-11-05 20:48, reason: User, spinning module LinuxInterface, available RAM 74612 bytes (slot 3)
            Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
            Error status: 0
            MCU temperature: min 25.6, current 25.8, max 26.0
            Supply voltage: min 0.3, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
            12V rail voltage: min 0.1, current 0.2, max 0.2, under voltage events: 0
            Driver 0: ok, reads 0, writes 0 timeouts 0, SG min/max not available
            Driver 1: ok, reads 0, writes 0 timeouts 0, SG min/max not available
            Driver 2: ok, reads 0, writes 0 timeouts 0, SG min/max not available
            Driver 3: ok, reads 0, writes 0 timeouts 0, SG min/max not available
            Driver 4: ok, reads 0, writes 0 timeouts 0, SG min/max not available
            Driver 5: ok, reads 0, writes 0 timeouts 0, SG min/max not available
            Date/time: 2020-11-08 14:28:49
            Slowest loop: 1.97ms; fastest: 0.13ms
            === Storage ===
            Free file entries: 10
            SD card 0 not detected, interface speed: 37.5MBytes/sec
            SD card longest read time 0.0ms, write time 0.0ms, max retries 0
            === Move ===
            Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
            Bed compensation in use: none, comp offset 0.000
            === MainDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
            === AuxDDARing ===
            Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0  CDDA state: -1
            === Heat ===
            Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP* is ready with "M122 D0 S0 F0" in state(s) 0
            Telnet is idle in state(s) 0
            File is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger* is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            SBC is idle in state(s) 0
            Daemon* is idle in state(s) 0
            Aux2 is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === Network ===
            Slowest loop: 1.03ms; fastest: 0.01ms
            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
            HTTP sessions: 0 of 8
            - Ethernet -
            State: disabled
            Error counts: 0 0 0 0 0
            Socket states: 0 0 0 0 0 0 0 0
            === CAN ===
            Messages sent 0, longest wait 0ms for type 0
            === Linux interface ===
            State: 0, failed transfers: 0
            Last transfer: 12ms ago
            RX/TX seq numbers: 24793/24794
            SPI underruns 0, overruns 0
            Number of disconnects: 0
            Buffer RX/TX: 0/0-0
            === Duet Control Server ===
            Duet Control Server v3.1.1
            Code buffer space: 4096
            Configured SPI speed: 8000000 Hz
            Full transfers per second: 32.80
            
            Phaedruxundefined 2 Replies Last reply Reply Quote 1
            • Phaedruxundefined
              Phaedrux Moderator @dhusolo
              last edited by

              @dhusolo said in Duet 3 SBC DCS has stopped:

              M122 DSF

              I think the quotes around DSF are required. I'll admit I haven't used that command yet.

              Z-Bot CoreXY Build | Thingiverse Profile

              dhusoloundefined 1 Reply Last reply Reply Quote 0
              • dhusoloundefined
                dhusolo @Phaedrux
                last edited by

                @Phaedrux

                m122 "DSF"
                === Duet Control Server ===
                Duet Control Server v3.1.1
                Daemon:
                Finishing macro daemon.g, started by system
                > Next stack level
                Code buffer space: 4096
                Configured SPI speed: 8000000 Hz
                Full transfers per second: 32.83
                
                1 Reply Last reply Reply Quote 0
                • Phaedruxundefined
                  Phaedrux Moderator @dhusolo
                  last edited by

                  @dhusolo said in Duet 3 SBC DCS has stopped:

                  === Duet Control Server === Duet Control Server v3.1.1

                  Regardless, I think you're on 3.1.1 across the board now.

                  Z-Bot CoreXY Build | Thingiverse Profile

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                  • dhusoloundefined
                    dhusolo
                    last edited by

                    but to your earlier question I tried updating to the beta following this and updating the source list to use unstable version

                    1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Would you be willing to test beta 3 once again?

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • dhusoloundefined
                        dhusolo
                        last edited by

                        Sure. Should I use the getting started link or manually flash? I've tried compiling the firmware myself but with no success which is why I used the instructions in the link

                        jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                        • jay_s_ukundefined
                          jay_s_uk @dhusolo
                          last edited by jay_s_uk

                          @dhusolo that should be all you need to follow to move over to the unstable branch.
                          There's no need to use the erase button to load the firmware as it will be updated as part of the upgrade process

                          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                          1 Reply Last reply Reply Quote 1
                          • dhusoloundefined
                            dhusolo
                            last edited by

                            I thought i did it correct but I got this error

                            pi@duet3:~ $ sudo apt-get install duetsoftwareframework
                            Reading package lists... Done
                            Building dependency tree       
                            Reading state information... Done
                            The following additional packages will be installed:
                              duetcontrolserver duetruntime duetsd duettools duetwebcontrol duetwebserver
                              reprapfirmware
                            The following packages will be upgraded:
                              duetcontrolserver duetruntime duetsd duetsoftwareframework duettools
                              duetwebcontrol duetwebserver reprapfirmware
                            8 upgraded, 0 newly installed, 0 to remove and 118 not upgraded.
                            Need to get 34.0 MB of archives.
                            After this operation, 0 B of additional disk space will be used.
                            Do you want to continue? [Y/n] y
                            Get:1 https://pkg.duet3d.com unstable/armv7 armhf duetsoftwareframework armhf 3.2.0-beta3 [2,034 B]
                            Get:2 https://pkg.duet3d.com unstable/armv7 armhf duetsd all 1.1.0 [2,102 B]
                            Get:3 https://pkg.duet3d.com unstable/armv7 armhf duettools armhf 3.2.0-beta3 [62.2 kB]
                            Get:4 https://pkg.duet3d.com unstable/armv7 armhf duetcontrolserver armhf 3.2.0-beta3 [226 kB]
                            Get:5 https://pkg.duet3d.com unstable/armv7 armhf duetruntime armhf 3.2.0-beta3 [28.9 MB]
                            Get:6 https://pkg.duet3d.com unstable/armv7 armhf duetwebserver armhf 3.2.0-beta3 [83.9 kB]
                            Get:7 https://pkg.duet3d.com unstable/armv7 armhf duetwebcontrol all 3.2.0-beta3 [3,507 kB]
                            Get:8 https://pkg.duet3d.com unstable/armv7 armhf reprapfirmware all 3.2.0-beta3-1 [1,260 kB]
                            Fetched 34.0 MB in 19s (1,813 kB/s)                                           
                            Reading changelogs... Done
                            (Reading database ... 79179 files and directories currently installed.)
                            Preparing to unpack .../0-duetsoftwareframework_3.2.0-beta3_armhf.deb ...
                            Unpacking duetsoftwareframework (3.2.0-beta3) over (3.1.1) ...
                            Preparing to unpack .../1-duetsd_1.1.0_all.deb ...
                            Unpacking duetsd (1.1.0) over (1.0.6) ...
                            Preparing to unpack .../2-duettools_3.2.0-beta3_armhf.deb ...
                            Unpacking duettools (3.2.0-beta3) over (3.1.1) ...
                            Preparing to unpack .../3-duetcontrolserver_3.2.0-beta3_armhf.deb ...
                            Unpacking duetcontrolserver (3.2.0-beta3) over (3.1.1) ...
                            Preparing to unpack .../4-duetruntime_3.2.0-beta3_armhf.deb ...
                            Unpacking duetruntime (3.2.0-beta3) over (3.1.1) ...
                            Preparing to unpack .../5-duetwebserver_3.2.0-beta3_armhf.deb ...
                            Unpacking duetwebserver (3.2.0-beta3) over (3.1.0) ...
                            Preparing to unpack .../6-duetwebcontrol_3.2.0-beta3_all.deb ...
                            Unpacking duetwebcontrol (3.2.0-beta3) over (3.1.1) ...
                            Preparing to unpack .../7-reprapfirmware_3.2.0-beta3-1_all.deb ...
                            Unpacking reprapfirmware (3.2.0-beta3-1) over (3.1.1-1) ...
                            Setting up duetruntime (3.2.0-beta3) ...
                            Setting up duetcontrolserver (3.2.0-beta3) ...
                            Installing new version of config file /opt/dsf/conf/config.json ...
                            Creating group dsf with gid 995.
                            Creating user dsf (n/a) with uid 995 and gid 995.
                            Setting up duettools (3.2.0-beta3) ...
                            Setting up duetwebserver (3.2.0-beta3) ...
                            Setting up duetsoftwareframework (3.2.0-beta3) ...
                            To modify config files consider adding yourself to the dsf groupd: # usermod -a -G dsf <username>
                            Setting up duetwebcontrol (3.2.0-beta3) ...
                            Setting up duetsd (1.1.0) ...
                            Setting up reprapfirmware (3.2.0-beta3-1) ...
                            Sending update request to DCS... Error: Failed to send update request
                            Unhandled exception. System.Threading.Tasks.TaskCanceledException: A task was canceled.
                               at DuetAPIClient.BaseConnection.PerformCommand[T](BaseCommand command, CancellationToken cancellationToken) in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetAPIClient/BaseConnection.cs:line 188
                               at DuetControlServer.Program.CheckForAnotherInstance() in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetControlServer/Program.cs:line 305
                               at DuetControlServer.Program.Main(String[] args) in /home/christian/Duet3D/DuetSoftwareFramework/src/DuetControlServer/Program.cs:line 84
                               at DuetControlServer.Program.<Main>(String[] args)
                            
                            
                            jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                            • jay_s_ukundefined
                              jay_s_uk @dhusolo
                              last edited by jay_s_uk

                              @dhusolo
                              Are you still able to connect to the board via DWC?
                              If you can confirm the firmware version using 3.1.1
                              If it's still 3.1.1, send M997 B0
                              I would be interested to see if you get any errors reported

                              Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                              dhusoloundefined 1 Reply Last reply Reply Quote 0
                              • dhusoloundefined
                                dhusolo @jay_s_uk
                                last edited by

                                @jay_s_uk
                                I had to start DCS and DWS manually but I was able to get to the web interface.

                                M122 "DSF"
                                === Duet Control Server ===
                                Duet Control Server v3.2.0-beta3
                                Code buffer space: 4096
                                Configured SPI speed: 8000000 Hz
                                Full transfers per second: 32.68
                                11/8/2020, 2:58:59 PM```	
                                
                                M122
                                === Diagnostics ===
                                RepRapFirmware for Duet 3 MB6HC version 3.2-beta3 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                Board ID: 08DJM-956L2-G43S8-6J9D0-3S46T-9U2LF
                                Used output buffers: 1 of 40 (10 max)
                                === RTOS ===
                                Static ram: 122124
                                Dynamic ram: 137508 of which 0 recycled
                                Never used RAM 132560, free system stack 185 words
                                Tasks: Linux(ready,131) HEAT(blocked,362) CanReceiv(blocked,948) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,66) MAIN(running,1300) IDLE(ready,19)
                                Owned mutexes: HTTP(MAIN)
                                === Platform ===
                                Last reset 00:09:17 ago, cause: software
                                Last software reset details not available
                                Error status: 0x00
                                MCU temperature: min 25.3, current 26.2, max 26.4
                                Supply voltage: min 0.3, current 0.3, max 0.3, under voltage events: 0, over voltage events: 0, power good: no
                                12V rail voltage: min 0.1, current 0.2, max 0.2, under voltage events: 0
                                Driver 0: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                Driver 1: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                Driver 2: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                Driver 3: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                Driver 4: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                Driver 5: position 0, ok, reads 0, writes 0 timeouts 0, SG min/max 0/0
                                Date/time: 2020-11-08 14:58:59
                                Slowest loop: 743.08ms; fastest: 0.16ms
                                === Storage ===
                                Free file entries: 10
                                SD card 0 not detected, interface speed: 37.5MBytes/sec
                                SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                === Move ===
                                Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                                Bed compensation in use: none, comp offset 0.000
                                === MainDDARing ===
                                Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                === AuxDDARing ===
                                Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                === Heat ===
                                Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                === GCodes ===
                                Segments left: 0
                                Movement lock held by null
                                HTTP* is doing "M122" in state(s) 0
                                Telnet is idle in state(s) 0
                                File is idle in state(s) 0
                                USB is idle in state(s) 0
                                Aux is idle in state(s) 0
                                Trigger* is idle in state(s) 0
                                Queue is idle in state(s) 0
                                LCD is idle in state(s) 0
                                SBC is idle in state(s) 0
                                Daemon is idle in state(s) 0
                                Aux2 is idle in state(s) 0
                                Autopause is idle in state(s) 0
                                Code queue is empty.
                                === CAN ===
                                Messages sent 0, send timeouts 0, longest wait 0ms for type 0, free CAN buffers 47
                                === SBC interface ===
                                State: 0, failed transfers: 1
                                Last transfer: 14ms ago
                                RX/TX seq numbers: 17902/17903
                                SPI underruns 0, overruns 0
                                Number of disconnects: 0, IAP RAM available 0x20aa0
                                Buffer RX/TX: 0/0-0
                                === Duet Control Server ===
                                Duet Control Server v3.2.0-beta3
                                Code buffer space: 4096
                                Configured SPI speed: 8000000 Hz
                                Full transfers per second: 32.56
                                
                                jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                                • jay_s_ukundefined
                                  jay_s_uk @dhusolo
                                  last edited by

                                  @dhusolo well at least you're back on the latest firmware.
                                  @chrishamm any comments on the error above whilst updating?

                                  Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                  1 Reply Last reply Reply Quote 0
                                  • dhusoloundefined
                                    dhusolo
                                    last edited by

                                    More of a status update: I've started the same print again but I don't load any filament. I didn't want to waste the filament if it's going to cancel on me again.

                                    However I can now hear some strange jerky movements. I have a coreXY so it's hard to narrow down what stepper it's coming from especially since there's no filament going through it.

                                    Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                    • oliofundefined
                                      oliof
                                      last edited by

                                      I think my recent post about issues with 3.2b3 are very similar to this issue.

                                      <>RatRig V-Minion Fly Super5Pro RRF<> V-Core 3.1 IDEX k*****r <> RatRig V-Minion SKR 2 Marlin<>

                                      1 Reply Last reply Reply Quote 2
                                      • Phaedruxundefined
                                        Phaedrux Moderator @dhusolo
                                        last edited by

                                        @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        A Former User? dhusoloundefined 2 Replies Last reply Reply Quote 0
                                        • A Former User?
                                          A Former User @Phaedrux
                                          last edited by

                                          @Phaedrux said in Duet 3 SBC DCS has stopped:

                                          @dhusolo Thanks for the update. In the meantime are you able to downgrade to 3.1.1 and use standalone mode to get back printing reliably?

                                          Oh the irony.....

                                          Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                          • dhusoloundefined
                                            dhusolo @Phaedrux
                                            last edited by

                                            @Phaedrux I'm going to attempt to go back to RRF 3.1.1 with RPI since issues with connecting are resolved. Doesn't make a lot of sense that it was working previously for 3 months without any issue.

                                            If that brings the same symptoms I'll run it in standalone until RRF 3.2 is stable. At least I know the board isn't bad

                                            1 Reply Last reply Reply Quote 0
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