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    Scheduled Pinned Locked Moved Solved
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    • KCMARINEundefined
      KCMARINE @KCMARINE
      last edited by

      @gloomyandy - recap to answer your questions

      Are you using an SBC setup?

      Yes, I downloaded https://pkg.duet3d.com/DuetPi.zip and flashed the SD card.

      Did you deliberately install the beta?

      Yes, did make the upgrade

      What steps did you use to do that?

      I made the upgrade by downloading the 3.5 beta from the git repo and uploaded to DWC then installed it unknowingly that it may conflict with the SBC 3.4.5

      Can you still talk to the board using DWC after you tried to install 3.4.5?
      .Yes, however SPI connection reset and timeouts are still happening

      It looks like you are still on DSF 3.4.5

      Yes, now I have downgraded all firmware to match the Pi SBC and problems still remain

      gloomyandyundefined 1 Reply Last reply Reply Quote 0
      • gloomyandyundefined
        gloomyandy @KCMARINE
        last edited by

        @KCMARINE So you are now on 3.4.5 on for both DSF and RRF (at least that is what your last posted M122 shows). Can you post another one just so we can be sure. What SBC are you using? Is it a raspberry Pi (which model) or something else?

        KCMARINEundefined 1 Reply Last reply Reply Quote 0
        • KCMARINEundefined
          KCMARINE @gloomyandy
          last edited by

          @gloomyandy thanks. I can confirm the following:

          SBC is Raspberry Pi 4 Model B

          and M122

          1/22/2023, 5:53:12 PM	m122
          === Diagnostics ===
          RepRapFirmware for Duet 3 MB6HC version 3.4.5 (2022-11-30 19:35:23) running on Duet 3 MB6HC v1.01 (SBC mode)
          Board ID: 08DJM-9P63L-DJ3T8-6J9DD-3SJ6N-9B7ZA
          Used output buffers: 1 of 40 (19 max)
          === RTOS ===
          Static ram: 152760
          Dynamic ram: 67576 of which 16 recycled
          Never used RAM 130320, free system stack 200 words
          Tasks: SBC(ready,0.6%,461) HEAT(notifyWait,0.0%,322) Move(notifyWait,0.0%,351) CanReceiv(notifyWait,0.0%,774) CanSender(notifyWait,0.0%,336) CanClock(delaying,0.0%,339) TMC(notifyWait,7.6%,91) MAIN(running,90.9%,923) IDLE(ready,0.9%,30), total 100.0%
          Owned mutexes: HTTP(MAIN)
          === Platform ===
          Last reset 00:04:22 ago, cause: power up
          Last software reset time unknown, reason: MemoryProtectionFault mmarValid daccViol, GCodes spinning, available RAM 132888, slot 0
          Software reset code 0x4163 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x00400804 BFAR 0x0000633a SP 0x2041b450 Task MAIN Freestk 1628 ok
          Stack: 2042a370 00000000 20418198 0000632e 00000000 00489db5 00489de6 21030000 2042c550 00000000 00000000 0048922f 00000000 00000000 00000000 0000000a 00000000 2042c550 20419a84 2042d1ac 00000000 00000001 00000000 00488ee7 00000001 00489db5 00000000
          Error status: 0x00
          Aux0 errors 0,0,0
          Step timer max interval 135
          MCU temperature: min 35.9, current 44.9, max 44.9
          Supply voltage: min 24.3, current 24.3, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
          12V rail voltage: min 12.2, current 12.3, max 12.3, under voltage events: 0
          Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
          Events: 0 queued, 0 completed
          Driver 0: standstill, SG min 0, mspos 8, reads 22115, writes 14 timeouts 0
          Driver 1: standstill, SG min 0, mspos 8, reads 22115, writes 14 timeouts 0
          Driver 2: standstill, SG min 0, mspos 8, reads 22115, writes 14 timeouts 0
          Driver 3: standstill, SG min 0, mspos 8, reads 22115, writes 14 timeouts 0
          Driver 4: standstill, SG min 0, mspos 8, reads 22115, writes 14 timeouts 0
          Driver 5: standstill, SG min 0, mspos 8, reads 22115, writes 14 timeouts 0
          Date/time: 2023-01-22 09:53:11
          Slowest loop: 2.22ms; fastest: 0.03ms
          === Storage ===
          Free file entries: 10
          SD card 0 not detected, interface speed: 37.5MBytes/sec
          SD card longest read time 0.0ms, write time 0.0ms, max retries 0
          === Move ===
          DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
          === MainDDARing ===
          Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
          === AuxDDARing ===
          Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
          === Heat ===
          Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
          Heater 1 is on, I-accum = 0.0
          === GCodes ===
          Segments left: 0
          Movement lock held by null
          HTTP* is doing "M122" in state(s) 0
          Telnet is idle in state(s) 0
          File is idle in state(s) 0
          USB is idle in state(s) 0
          Aux is idle in state(s) 0
          Trigger* is idle in state(s) 0
          Queue is idle in state(s) 0
          LCD is idle in state(s) 0
          SBC is idle in state(s) 0
          Daemon is idle in state(s) 0
          Aux2 is idle in state(s) 0
          Autopause is idle in state(s) 0
          Code queue is empty
          === CAN ===
          Messages queued 2265, received 2101, lost 0, boc 0
          Longest wait 0ms for reply type 0, peak Tx sync delay 6, free buffers 50 (min 49), ts 1311/1310/0
          Tx timeouts 0,0,0,0,0,0
          === SBC interface ===
          Transfer state: 5, failed transfers: 0, checksum errors: 0
          RX/TX seq numbers: 11230/11230
          SPI underruns 0, overruns 0
          State: 5, disconnects: 0, timeouts: 0 total, 0 by SBC, IAP RAM available 0x2ad48
          Buffer RX/TX: 0/0-0, open files: 0
          === Duet Control Server ===
          Duet Control Server v3.4.5
          Code buffer space: 4096
          Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 0
          Full transfers per second: 0.61, max time between full transfers: 425.3ms, max pin wait times: 44.1ms/51.4ms
          Codes per second: 0.00
          Maximum length of RX/TX data transfers: 6196/836
          
          jay_s_ukundefined KCMARINEundefined gloomyandyundefined 3 Replies Last reply Reply Quote 0
          • jay_s_ukundefined
            jay_s_uk @KCMARINE
            last edited by

            @KCMARINE are you using the supplied cable between the pi and the duet? Can you post a photo of it's routing so we can see what's near it etc?

            Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

            1 Reply Last reply Reply Quote 1
            • KCMARINEundefined
              KCMARINE @KCMARINE
              last edited by

              @gloomyandy

              IMG_3158.jpg

              1 Reply Last reply Reply Quote 0
              • gloomyandyundefined
                gloomyandy @KCMARINE
                last edited by

                @KCMARINE Yep both versions match. Could you also post a picture showing how the two boards are connected. After that I think this is one for @chrishamm

                gloomyandyundefined KCMARINEundefined 2 Replies Last reply Reply Quote 0
                • gloomyandyundefined
                  gloomyandy @gloomyandy
                  last edited by

                  @gloomyandy Ha Jay got there first!

                  1 Reply Last reply Reply Quote 0
                  • KCMARINEundefined
                    KCMARINE @gloomyandy
                    last edited by

                    @gloomyandy

                    IMG_3160.jpg IMG_3159.jpg IMG_3161.jpg

                    KCMARINEundefined 1 Reply Last reply Reply Quote 0
                    • KCMARINEundefined
                      KCMARINE @KCMARINE
                      last edited by

                      @gloomyandy

                      Thanks for the help - I appreciate all that you do

                      I am out of ideas.

                      My last attempt/thought is to flash another SD card with a new copy of DuetPi.zip and see what happens!

                      KCMARINEundefined 1 Reply Last reply Reply Quote 0
                      • KCMARINEundefined
                        KCMARINE @KCMARINE
                        last edited by

                        @gloomyandy @droftarts @jay_s_uk

                        Success - after flashing a new SD card with DuetPi.zip I am happy to report that I have no more communication errors and I can print my first calibration cube.

                        I believe that the issue may have been caused by the additional motion installation for the Logitech webcam

                        https://www.instructables.com/How-to-Make-Raspberry-Pi-Webcam-Server-and-Stream-/

                        The strange thing is I have this running on another SBC Pi 4 and MB6HC running 3.4.5 on a delta with no issues, guessing it could be a compatibility issue with 3.5 upgrades and then a downgrade, just a stab in the dark.

                        Thanks again for your support gents - very much appreciated.

                        jay_s_ukundefined 1 Reply Last reply Reply Quote 1
                        • jay_s_ukundefined
                          jay_s_uk @KCMARINE
                          last edited by

                          @KCMARINE glad you got sorted. I was going to suggest that running all those cables next to the ribbon may be the cause but as you've fixed it I wouldn't worry. If it does however happen again I would consider revisiting your cable routing

                          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                          1 Reply Last reply Reply Quote 1
                          • Phaedruxundefined Phaedrux marked this topic as a question
                          • Phaedruxundefined Phaedrux has marked this topic as solved
                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            I'll mark as solved, but let us know if you continue to have issues.

                            Z-Bot CoreXY Build | Thingiverse Profile

                            KCMARINEundefined 1 Reply Last reply Reply Quote 0
                            • KCMARINEundefined
                              KCMARINE @Phaedrux
                              last edited by

                              @Phaedrux

                              I spoke too soon - errors returned, and the connection issue continues to drop out, causing prints to fail.

                              Screenshot 2023-01-23 at 3.44.52 PM.png

                              I also followed @jay_s_uk advice and cleaned up the wiring moving everything away from the connecting ribbon cable between the SBC Pi 4 and MB6HC

                              IMG_3165.jpg

                              After a restart M122

                              m122
                              === Diagnostics ===
                              RepRapFirmware for Duet 3 MB6HC version 3.4.5 (2022-11-30 19:35:23) running on Duet 3 MB6HC v1.01 (SBC mode)
                              Board ID: 08DJM-9P63L-DJ3T8-6J9DD-3SJ6N-9B7ZA
                              Used output buffers: 1 of 40 (22 max)
                              === RTOS ===
                              Static ram: 152760
                              Dynamic ram: 67576 of which 16 recycled
                              Never used RAM 127104, free system stack 130 words
                              Tasks: SBC(ready,0.7%,444) HEAT(notifyWait,0.0%,322) Move(notifyWait,0.3%,245) CanReceiv(notifyWait,0.0%,774) CanSender(notifyWait,0.0%,328) CanClock(delaying,0.0%,339) TMC(notifyWait,8.3%,57) MAIN(running,90.5%,923) IDLE(ready,0.2%,30), total 100.0%
                              Owned mutexes: HTTP(MAIN)
                              === Platform ===
                              Last reset 00:13:43 ago, cause: power up
                              Last software reset details not available
                              Error status: 0x00
                              Aux0 errors 0,0,0
                              Step timer max interval 135
                              MCU temperature: min 37.5, current 44.5, max 44.7
                              Supply voltage: min 24.3, current 24.3, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
                              12V rail voltage: min 12.2, current 12.2, max 12.3, under voltage events: 0
                              Heap OK, handles allocated/used 99/1, heap memory allocated/used/recyclable 2048/156/104, gc cycles 0
                              Events: 0 queued, 0 completed
                              Driver 0: standstill, SG min 0, mspos 200, reads 35667, writes 33 timeouts 0
                              Driver 1: standstill, SG min 0, mspos 1016, reads 35667, writes 33 timeouts 0
                              Driver 2: standstill, SG min 0, mspos 88, reads 35668, writes 33 timeouts 0
                              Driver 3: standstill, SG min 0, mspos 120, reads 35668, writes 33 timeouts 0
                              Driver 4: ok, SG min 0, mspos 433, reads 35672, writes 29 timeouts 0
                              Driver 5: ok, SG min 0, mspos 472, reads 35672, writes 29 timeouts 0
                              Date/time: 2023-01-23 08:07:44
                              Slowest loop: 61.47ms; fastest: 0.04ms
                              === Storage ===
                              Free file entries: 10
                              SD card 0 not detected, interface speed: 37.5MBytes/sec
                              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                              === Move ===
                              DMs created 125, segments created 15, maxWait 262562ms, bed compensation in use: none, comp offset 0.000
                              === MainDDARing ===
                              Scheduled moves 929, completed 902, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 20], CDDA state 3
                              === AuxDDARing ===
                              Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                              === Heat ===
                              Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                              Heater 0 is on, I-accum = 0.0
                              Heater 1 is on, I-accum = 0.4
                              === GCodes ===
                              Segments left: 1
                              Movement lock held by null
                              HTTP* is doing "M122" in state(s) 0
                              Telnet is idle in state(s) 0
                              File* is doing "G1 X189.274002 Y170.934006 E0.224800" in state(s) 0
                              USB is idle in state(s) 0
                              Aux is idle in state(s) 0
                              Trigger* is idle in state(s) 0
                              Queue is idle in state(s) 0
                              LCD is idle in state(s) 0
                              SBC is idle in state(s) 0
                              Daemon is idle in state(s) 0
                              Aux2 is idle in state(s) 0
                              Autopause is idle in state(s) 0
                              Code queue is empty
                              === CAN ===
                              Messages queued 8593, received 6595, lost 0, boc 0
                              Longest wait 1ms for reply type 6042, peak Tx sync delay 10, free buffers 50 (min 48), ts 4118/4117/0
                              Tx timeouts 0,0,0,0,0,0
                              === SBC interface ===
                              Transfer state: 5, failed transfers: 0, checksum errors: 0
                              RX/TX seq numbers: 32802/32802
                              SPI underruns 0, overruns 0
                              State: 5, disconnects: 0, timeouts: 0 total, 0 by SBC, IAP RAM available 0x2ad48
                              Buffer RX/TX: 2888/312-4088, open files: 0
                              === Duet Control Server ===
                              Duet Control Server v3.4.5
                              File /opt/dsf/sd/gcodes/Calibration cube.gcode is selected, processing
                              File:
                              Buffered code: G1 X189.274 Y170.934 E0.2248
                              Buffered code: G1 X189.156 Y171.547 E0.02675
                              Buffered code: G1 X192.983 Y175.374 E0.23199
                              Buffered code: G1 X192.983 Y176.105 E0.03135
                              Buffered code: G1 X189.037 Y172.159 E0.23919
                              Buffered code: G1 X188.957 Y172.573 E0.01804
                              Buffered code: G1 X188.926 Y172.779 E0.00896
                              Buffered code: G1 X192.983 Y176.836 E0.24594
                              Buffered code: G1 X192.983 Y177.567 E0.03135
                              Buffered code: G1 X188.83 Y173.415 E0.25176
                              Buffered code: G1 X188.734 Y174.05 E0.02754
                              Buffered code: G1 X192.983 Y178.299 E0.25757
                              Buffered code: G1 X192.983 Y179.03 E0.03135
                              Buffered code: G1 X188.645 Y174.692 E0.26295
                              Buffered code: G1 X188.575 Y175.353 E0.02848
                              Buffered code: G1 X192.983 Y179.761 E0.26723
                              Buffered code: G1 X192.983 Y180.492 E0.03135
                              Buffered code: G1 X188.504 Y176.014 E0.27151
                              Buffered code: G1 X188.465 Y176.378 E0.01569
                              Buffered code: G1 X188.447 Y176.688 E0.01332
                              Buffered code: G1 X192.983 Y181.224 E0.27497
                              Buffered code: G1 X192.983 Y181.955 E0.03135
                              Buffered code: G1 X188.406 Y177.379 E0.27742
                              Buffered code: G1 X188.385 Y177.743 E0.01566
                              Buffered code: G1 X188.389 Y178.093 E0.01497
                              Buffered code: G1 X192.983 Y182.686 E0.27848
                              Buffered code: G1 X192.983 Y183.417 E0.03135
                              Buffered code: G1 X188.397 Y178.832 E0.27798
                              Buffered code: G1 X188.4 Y179.044 E0.00906
                              Buffered code: G1 X188.34 Y179.506 E0.02
                              Buffered code: G1 X192.983 Y184.149 E0.28144
                              Buffered code: G1 X192.983 Y184.88 E0.03135
                              ==> 1536 bytes
                              Code buffer space: 2576
                              Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 0
                              Full transfers per second: 35.22, max time between full transfers: 110.3ms, max pin wait times: 55.8ms/13.2ms
                              Codes per second: 1.88
                              Maximum length of RX/TX data transfers: 2920/1248
                              
                              
                               PM	M115
                              FIRMWARE_NAME: RepRapFirmware for Duet 3 MB6HC FIRMWARE_VERSION: 3.4.5 ELECTRONICS: Duet 3 MB6HC v1.01 FIRMWARE_DATE: 2022-11-30 19:35:23
                              
                              M115 B1
                              Duet EXP3HC rev 1.01 or earlier firmware version 3.4.4 (2022-10-14 11:45:56)
                              
                              KCMARINEundefined 1 Reply Last reply Reply Quote 1
                              • KCMARINEundefined
                                KCMARINE @KCMARINE
                                last edited by

                                I have added a second power supply via the USB to SBC Pi4 and running another print - will report results - thanks

                                KCMARINEundefined 1 Reply Last reply Reply Quote 0
                                • Phaedruxundefined Phaedrux has marked this topic as unsolved
                                • KCMARINEundefined
                                  KCMARINE @KCMARINE
                                  last edited by

                                  Update -

                                  I have not had a connection issue after upgrading the power to the SBC PI 4 - first, I tested by adding an additional power USB from a separate power source, reran the same print, and no connection issues.

                                  Now I am testing by removing the USB power and adding additional power input wires to the SBC PI4 GPIO Pins 2 and 4 for positive, then pins 14 and 20 for ground.

                                  It looks like the issue is resolved - thanks for the help once again.

                                  1 Reply Last reply Reply Quote 2
                                  • T3P3Tonyundefined T3P3Tony has marked this topic as solved
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