Warning: Lost connection to Duet - help needed
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@KCMARINE Yep both versions match. Could you also post a picture showing how the two boards are connected. After that I think this is one for @chrishamm
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@gloomyandy Ha Jay got there first!
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Thanks for the help - I appreciate all that you do
I am out of ideas.
My last attempt/thought is to flash another SD card with a new copy of DuetPi.zip and see what happens!
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@gloomyandy @droftarts @jay_s_uk
Success - after flashing a new SD card with DuetPi.zip I am happy to report that I have no more communication errors and I can print my first calibration cube.
I believe that the issue may have been caused by the additional motion installation for the Logitech webcam
https://www.instructables.com/How-to-Make-Raspberry-Pi-Webcam-Server-and-Stream-/
The strange thing is I have this running on another SBC Pi 4 and MB6HC running 3.4.5 on a delta with no issues, guessing it could be a compatibility issue with 3.5 upgrades and then a downgrade, just a stab in the dark.
Thanks again for your support gents - very much appreciated.
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@KCMARINE glad you got sorted. I was going to suggest that running all those cables next to the ribbon may be the cause but as you've fixed it I wouldn't worry. If it does however happen again I would consider revisiting your cable routing
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I'll mark as solved, but let us know if you continue to have issues.
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I spoke too soon - errors returned, and the connection issue continues to drop out, causing prints to fail.
I also followed @jay_s_uk advice and cleaned up the wiring moving everything away from the connecting ribbon cable between the SBC Pi 4 and MB6HC
After a restart M122
m122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.4.5 (2022-11-30 19:35:23) running on Duet 3 MB6HC v1.01 (SBC mode) Board ID: 08DJM-9P63L-DJ3T8-6J9DD-3SJ6N-9B7ZA Used output buffers: 1 of 40 (22 max) === RTOS === Static ram: 152760 Dynamic ram: 67576 of which 16 recycled Never used RAM 127104, free system stack 130 words Tasks: SBC(ready,0.7%,444) HEAT(notifyWait,0.0%,322) Move(notifyWait,0.3%,245) CanReceiv(notifyWait,0.0%,774) CanSender(notifyWait,0.0%,328) CanClock(delaying,0.0%,339) TMC(notifyWait,8.3%,57) MAIN(running,90.5%,923) IDLE(ready,0.2%,30), total 100.0% Owned mutexes: HTTP(MAIN) === Platform === Last reset 00:13:43 ago, cause: power up Last software reset details not available Error status: 0x00 Aux0 errors 0,0,0 Step timer max interval 135 MCU temperature: min 37.5, current 44.5, max 44.7 Supply voltage: min 24.3, current 24.3, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.2, current 12.2, max 12.3, under voltage events: 0 Heap OK, handles allocated/used 99/1, heap memory allocated/used/recyclable 2048/156/104, gc cycles 0 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, mspos 200, reads 35667, writes 33 timeouts 0 Driver 1: standstill, SG min 0, mspos 1016, reads 35667, writes 33 timeouts 0 Driver 2: standstill, SG min 0, mspos 88, reads 35668, writes 33 timeouts 0 Driver 3: standstill, SG min 0, mspos 120, reads 35668, writes 33 timeouts 0 Driver 4: ok, SG min 0, mspos 433, reads 35672, writes 29 timeouts 0 Driver 5: ok, SG min 0, mspos 472, reads 35672, writes 29 timeouts 0 Date/time: 2023-01-23 08:07:44 Slowest loop: 61.47ms; fastest: 0.04ms === Storage === Free file entries: 10 SD card 0 not detected, interface speed: 37.5MBytes/sec SD card longest read time 0.0ms, write time 0.0ms, max retries 0 === Move === DMs created 125, segments created 15, maxWait 262562ms, bed compensation in use: none, comp offset 0.000 === MainDDARing === Scheduled moves 929, completed 902, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 20], CDDA state 3 === AuxDDARing === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.0 Heater 1 is on, I-accum = 0.4 === GCodes === Segments left: 1 Movement lock held by null HTTP* is doing "M122" in state(s) 0 Telnet is idle in state(s) 0 File* is doing "G1 X189.274002 Y170.934006 E0.224800" in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger* is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty === CAN === Messages queued 8593, received 6595, lost 0, boc 0 Longest wait 1ms for reply type 6042, peak Tx sync delay 10, free buffers 50 (min 48), ts 4118/4117/0 Tx timeouts 0,0,0,0,0,0 === SBC interface === Transfer state: 5, failed transfers: 0, checksum errors: 0 RX/TX seq numbers: 32802/32802 SPI underruns 0, overruns 0 State: 5, disconnects: 0, timeouts: 0 total, 0 by SBC, IAP RAM available 0x2ad48 Buffer RX/TX: 2888/312-4088, open files: 0 === Duet Control Server === Duet Control Server v3.4.5 File /opt/dsf/sd/gcodes/Calibration cube.gcode is selected, processing File: Buffered code: G1 X189.274 Y170.934 E0.2248 Buffered code: G1 X189.156 Y171.547 E0.02675 Buffered code: G1 X192.983 Y175.374 E0.23199 Buffered code: G1 X192.983 Y176.105 E0.03135 Buffered code: G1 X189.037 Y172.159 E0.23919 Buffered code: G1 X188.957 Y172.573 E0.01804 Buffered code: G1 X188.926 Y172.779 E0.00896 Buffered code: G1 X192.983 Y176.836 E0.24594 Buffered code: G1 X192.983 Y177.567 E0.03135 Buffered code: G1 X188.83 Y173.415 E0.25176 Buffered code: G1 X188.734 Y174.05 E0.02754 Buffered code: G1 X192.983 Y178.299 E0.25757 Buffered code: G1 X192.983 Y179.03 E0.03135 Buffered code: G1 X188.645 Y174.692 E0.26295 Buffered code: G1 X188.575 Y175.353 E0.02848 Buffered code: G1 X192.983 Y179.761 E0.26723 Buffered code: G1 X192.983 Y180.492 E0.03135 Buffered code: G1 X188.504 Y176.014 E0.27151 Buffered code: G1 X188.465 Y176.378 E0.01569 Buffered code: G1 X188.447 Y176.688 E0.01332 Buffered code: G1 X192.983 Y181.224 E0.27497 Buffered code: G1 X192.983 Y181.955 E0.03135 Buffered code: G1 X188.406 Y177.379 E0.27742 Buffered code: G1 X188.385 Y177.743 E0.01566 Buffered code: G1 X188.389 Y178.093 E0.01497 Buffered code: G1 X192.983 Y182.686 E0.27848 Buffered code: G1 X192.983 Y183.417 E0.03135 Buffered code: G1 X188.397 Y178.832 E0.27798 Buffered code: G1 X188.4 Y179.044 E0.00906 Buffered code: G1 X188.34 Y179.506 E0.02 Buffered code: G1 X192.983 Y184.149 E0.28144 Buffered code: G1 X192.983 Y184.88 E0.03135 ==> 1536 bytes Code buffer space: 2576 Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 0 Full transfers per second: 35.22, max time between full transfers: 110.3ms, max pin wait times: 55.8ms/13.2ms Codes per second: 1.88 Maximum length of RX/TX data transfers: 2920/1248
PM M115 FIRMWARE_NAME: RepRapFirmware for Duet 3 MB6HC FIRMWARE_VERSION: 3.4.5 ELECTRONICS: Duet 3 MB6HC v1.01 FIRMWARE_DATE: 2022-11-30 19:35:23
M115 B1 Duet EXP3HC rev 1.01 or earlier firmware version 3.4.4 (2022-10-14 11:45:56)
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I have added a second power supply via the USB to SBC Pi4 and running another print - will report results - thanks
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Update -
I have not had a connection issue after upgrading the power to the SBC PI 4 - first, I tested by adding an additional power USB from a separate power source, reran the same print, and no connection issues.
Now I am testing by removing the USB power and adding additional power input wires to the SBC PI4 GPIO Pins 2 and 4 for positive, then pins 14 and 20 for ground.
It looks like the issue is resolved - thanks for the help once again.
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