I share my dumb adventure to hopefully help others.
I have been printing a lot of material lately and the printer is working great (thanks SZP!). I started a new project and suddenly I was getting random heater faults. I had changed nothing on the printer, same hardware, same firmware, same config files. Literally KGs of filament had been printed fine. So I assumed some hw starting to fail, like a wire. I could just clear the fault and hit resume and it would print fine for a bit then fault again.
I noticed the first layer (slow) would go down fine and then when it sped up for the remaining layers I would get random faults. So I slowed the prints down and that helped! I also lowered the print cooling fan rate. I could sometimes get through a whole print without a fault, but not always. I checked the wires and thermistor and all was fine. So what changed? I was now printing PLA. I had been printing ASA. I have printed lots of PLA before without issue.
That's when I figured it out. The ASA I was printing was CF and GF so I had switched to a vanadium nozzle (this is a long while back at this point). Importantly, ASA requires a heated chamber. The thermal conductivity of vanadium is lower than brass. I had not retuned PID! But the higher ambient temperature of the heated chamber made that moot. I had gotten away with it. When I switched back to PLA for the current project I did not change the nozzle back. Now I was apparently right on the edge of PID control with normal ambients. When I slowed the print down the lower plastic rate cooled the nozzle a bit less which helped.
I switched back to the brass nozzle and printing fine again. I could instead have run PID tuning on the vanadium nozzle. Lesson: I was sure I had changed nothing, but in fact I had made a change a while ago and had gotten away with it.