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    Short to ground on drivers 0123

    Scheduled Pinned Locked Moved Unsolved
    Duet Hardware and wiring
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    • Touchthebitumundefined
      Touchthebitum @Phaedrux
      last edited by Touchthebitum

      @Phaedrux No, M122 had not error messages. Only those ground-short messages

      1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        When are where was the Duet 3 purchased?

        Z-Bot CoreXY Build | Thingiverse Profile

        Touchthebitumundefined 1 Reply Last reply Reply Quote 0
        • Touchthebitumundefined
          Touchthebitum @Phaedrux
          last edited by Touchthebitum

          @Phaedrux www.3dware.ch

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          • dc42undefined
            dc42 administrators
            last edited by

            Please send M122 and post the resulting output here.

            Duet WiFi hardware designer and firmware engineer
            Please do not ask me for Duet support via PM or email, use the forum
            http://www.escher3d.com, https://miscsolutions.wordpress.com

            Touchthebitumundefined 1 Reply Last reply Reply Quote 0
            • Touchthebitumundefined
              Touchthebitum @dc42
              last edited by

              @dc42

              m122
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
              Used output buffers: 1 of 40 (10 max)
              === RTOS ===
              Static ram: 154604
              Dynamic ram: 162592 of which 44 recycled
              Exception stack ram used: 224
              Never used ram: 75752
              Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,204) MAIN(running,4952) IDLE(ready,76)
              Owned mutexes:
              === Platform ===
              Last reset 00:00:44 ago, cause: power up
              Last software reset at 2020-07-27 15:14, reason: User, spinning module LinuxInterface, available RAM 75704 bytes (slot 0)
              Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
              Error status: 0
              MCU temperature: min 19.4, current 27.7, max 27.8
              Supply voltage: min 24.0, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
              12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
              Driver 0: standstill, reads 22474, writes 14 timeouts 0, SG min/max 0/0
              Driver 1: standstill, reads 22474, writes 14 timeouts 0, SG min/max 0/0
              Driver 2: standstill, reads 22475, writes 14 timeouts 0, SG min/max 0/0
              Driver 3: standstill, reads 22475, writes 14 timeouts 0, SG min/max 0/0
              Driver 4: standstill, reads 22478, writes 11 timeouts 0, SG min/max 0/0
              Driver 5: standstill, reads 22479, writes 11 timeouts 0, SG min/max 0/0
              Date/time: 2020-07-27 15:15:01
              Slowest loop: 3.63ms; fastest: 0.14ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
              Bed compensation in use: none, comp offset 0.000
              === MainDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
              === AuxDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
              === Heat ===
              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is ready with "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon* is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 1.02ms; fastest: 0.01ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
              HTTP sessions: 0 of 8

              • Ethernet -
                State: disabled
                Error counts: 0 0 0 0 0
                Socket states: 0 0 0 0 0 0 0 0
                === CAN ===
                Messages sent 72, longest wait 0ms for type 0
                === Linux interface ===
                State: 0, failed transfers: 0
                Last transfer: 18ms ago
                RX/TX seq numbers: 583/584
                SPI underruns 0, overruns 0
                Number of disconnects: 0
                Buffer RX/TX: 0/0-0
                === Duet Control Server ===
                Duet Control Server v3.1.1
                Code buffer space: 4096
                Configured SPI speed: 8000000 Hz
                Full transfers per second: 30.27
              1 Reply Last reply Reply Quote 0
              • dc42undefined
                dc42 administrators
                last edited by

                Thanks. Please try commanding the motors to move (without any motors connected) and repeat that. I am looking for the driver status to change.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

                Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                • Touchthebitumundefined
                  Touchthebitum @dc42
                  last edited by

                  @dc42

                  Error: short-to-ground reported by driver(s) 0 1
                  27/07/2020 à 21:40:14 m122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                  Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                  Used output buffers: 1 of 40 (10 max)
                  === RTOS ===
                  Static ram: 154604
                  Dynamic ram: 162592 of which 44 recycled
                  Exception stack ram used: 280
                  Never used ram: 75696
                  Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1452) TMC(blocked,68) MAIN(running,4952) IDLE(ready,76)
                  Owned mutexes:
                  === Platform ===
                  Last reset 00:00:47 ago, cause: power up
                  Last software reset at 2020-07-27 15:14, reason: User, spinning module LinuxInterface, available RAM 75704 bytes (slot 0)
                  Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                  Error status: 0
                  MCU temperature: min 20.8, current 29.0, max 29.1
                  Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.1, current 12.1, max 12.1, under voltage events: 0
                  Driver 0: short-to-ground standstill, reads 39652, writes 17 timeouts 0, SG min/max 0/0
                  Driver 1: short-to-ground standstill, reads 39652, writes 17 timeouts 0, SG min/max 0/63
                  Driver 2: standstill, reads 39656, writes 14 timeouts 0, SG min/max 0/0
                  Driver 3: standstill, reads 39656, writes 14 timeouts 0, SG min/max 0/0
                  Driver 4: standstill, reads 39660, writes 11 timeouts 0, SG min/max 0/0
                  Driver 5: standstill, reads 39660, writes 11 timeouts 0, SG min/max 0/0
                  Date/time: 2020-07-27 20:36:50
                  Slowest loop: 3.82ms; fastest: 0.14ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  Hiccups: 0(0), FreeDm: 375, MinFreeDm: 373, MaxWait: 34018ms
                  Bed compensation in use: none, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves: 1, completed moves: 1, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                  === AuxDDARing ===
                  Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                  === Heat ===
                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is ready with "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger* is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon* is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === Network ===
                  Slowest loop: 0.88ms; fastest: 0.01ms
                  Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                  HTTP sessions: 0 of 8

                  • Ethernet -
                    State: disabled
                    Error counts: 0 0 0 0 0
                    Socket states: 0 0 0 0 0 0 0 0
                    === CAN ===
                    Messages sent 100, longest wait 0ms for type 0
                    === Linux interface ===
                    State: 0, failed transfers: 0
                    Last transfer: 17ms ago
                    RX/TX seq numbers: 808/809
                    SPI underruns 0, overruns 0
                    Number of disconnects: 0
                    Buffer RX/TX: 0/0-0
                    === Duet Control Server ===
                    Duet Control Server v3.1.1
                    Code buffer space: 4096
                    Configured SPI speed: 8000000 Hz
                    Full transfers per second: 3.50
                  1 Reply Last reply Reply Quote 0
                  • percybundefined
                    percyb
                    last edited by

                    I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)" on all drive ports with what were working stepper motors. Only possible mistake i made is connect one stepper motor to 3 pins instead of 4 ie offset one pin. Would this cause all drivers to die?

                    Touchthebitumundefined A Former User? 2 Replies Last reply Reply Quote 0
                    • Touchthebitumundefined
                      Touchthebitum @percyb
                      last edited by

                      @percyb said in Short to ground on drivers 0123:

                      I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)" on all drive ports with what were working stepper motors. Only possible mistake i made is connect one stepper motor to 3 pins instead of 4 ie offset one pin. Would this cause all drivers to die?

                      Impossible because I tested all phases before plugging motor and I checked if these big crimps went on the right place when connectind them on the Duet,

                      1 Reply Last reply Reply Quote 0
                      • A Former User?
                        A Former User @percyb
                        last edited by A Former User

                        @percyb said in Short to ground on drivers 0123:

                        I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)"

                        ref https://forum.duet3d.com/post/100507 and you should probably start your own topic if the error persist after disconnecting your motors (when powered down ofc)

                        Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                        • Touchthebitumundefined
                          Touchthebitum @A Former User
                          last edited by

                          @bearer said in Short to ground on drivers 0123:

                          @percyb said in Short to ground on drivers 0123:

                          I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)"

                          ref https://forum.duet3d.com/post/100507 and you should probably start your own topic if the error persist after disconnecting your motors (when powered down ofc)

                          I think we should think about a warranty process. I don't know what to add to the discussion. I repeat, it is not the first printer I build and I'm aware of risks. Before this Duet3 I used a Duet2 and was perfect (no errors messages) with the same motors. This board never worked and I directly plugged the SAME motors that I plugged to my Duet2. So there is a problem.
                          My shop told me to see with this forum, what I did.
                          Now, I choosed a Genuine board because I believe in the right intelectual properties and know-how.
                          Please, give me a clear answer and we can go on.
                          Thanks

                          A Former User? T3P3Tonyundefined 2 Replies Last reply Reply Quote 0
                          • A Former User?
                            A Former User @Touchthebitum
                            last edited by

                            @Touchthebitum said in Short to ground on drivers 0123:

                            @bearer said in Short to ground on drivers 0123:

                            @percyb said in Short to ground on drivers 0123:

                            I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)"

                            ref https://forum.duet3d.com/post/100507 and you should probably start your own topic if the error persist after disconnecting your motors (when powered down ofc)

                            I think we should think about a warranty process.

                            that was not directed at you; I'm sure dc42 is trying to evaluate the information you've provided already

                            Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                            • Touchthebitumundefined
                              Touchthebitum @A Former User
                              last edited by

                              @bearer said in Short to ground on drivers 0123:

                              @Touchthebitum said in Short to ground on drivers 0123:

                              @bearer said in Short to ground on drivers 0123:

                              @percyb said in Short to ground on drivers 0123:

                              I have a similar issue, getting "Warning: motor phase A may be disconnected reported by driver(s)"

                              ref https://forum.duet3d.com/post/100507 and you should probably start your own topic if the error persist after disconnecting your motors (when powered down ofc)

                              I think we should think about a warranty process.

                              that was not directed at you; I'm sure dc42 is trying to evaluate the information you've provided already

                              Thanks 😉

                              1 Reply Last reply Reply Quote 0
                              • T3P3Tonyundefined
                                T3P3Tony administrators @Touchthebitum
                                last edited by

                                @Touchthebitum

                                Thanks for your patience, DC42 is away right now but I can help.

                                Looking at your latest M122 report it looks like driver 01 and 1 are damaged. its not completely clear if 2 and 3 are damaged - the motors connected to those ones could have an issue.

                                Can you try the following please

                                1. check the wiring of one of your stepper with a voltmeter. they should be wired in two pairs, 1-2 and 3-4 (i.e. pin 1 to 2 should read a few Ohms, pin 3 to 4 should read a few ohms but there should be no connection between pin the pairs).

                                2. with just that motor you have check tried it plugged into Driver 2, command a movement, send M122 and see what it says, we are looking at this part:

                                Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                                12V rail voltage: min 12.1, current 12.1, max 12.1, under voltage events: 0
                                Driver 0: short-to-ground standstill, reads 39652, writes 17 timeouts 0, SG min/max 0/0
                                Driver 1: short-to-ground standstill, reads 39652, writes 17 timeouts 0, SG min/max 0/63
                                Driver 2: standstill, reads 39656, writes 14 timeouts 0, SG min/max 0/0
                                Driver 3: standstill, reads 39656, writes 14 timeouts 0, SG min/max 0/0
                                Driver 4: standstill, reads 39660, writes 11 timeouts 0, SG min/max 0/0
                                Driver 5: standstill, reads 39660, writes 11 timeouts 0, SG min/max 0/0
                                
                                1. Repeat for driver 3 and driver 4.

                                Lets see those three excerpts from M122.

                                www.duet3d.com

                                Touchthebitumundefined 1 Reply Last reply Reply Quote 0
                                • Touchthebitumundefined
                                  Touchthebitum @T3P3Tony
                                  last edited by Touchthebitum

                                  @T3P3Tony

                                  Hello

                                  I tested pairs and got 2ohms on each pair and nothing between the two pairs
                                  For the moves of drivers 3-4 I made z move on the duet panel Due
                                  For the driver 4 , I don't have yet a connected extruder
                                  Error: short-to-ground reported by driver(s) 2
                                  28/07/2020 à 12:31:08 m122
                                  === Diagnostics ===
                                  RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                  Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                                  Used output buffers: 1 of 40 (10 max)
                                  === RTOS ===
                                  Static ram: 154604
                                  Dynamic ram: 162592 of which 44 recycled
                                  Exception stack ram used: 376
                                  Never used ram: 75600
                                  Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,196) MAIN(running,4952) IDLE(ready,76)
                                  Owned mutexes:
                                  === Platform ===
                                  Last reset 00:01:08 ago, cause: power up
                                  Last software reset at 2020-07-27 15:14, reason: User, spinning module LinuxInterface, available RAM 75704 bytes (slot 0)
                                  Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                  Error status: 0
                                  MCU temperature: min 20.6, current 29.8, max 29.9
                                  Supply voltage: min 24.0, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                                  12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                  Driver 0: standstill, reads 8684, writes 14 timeouts 0, SG min/max 0/0
                                  Driver 1: standstill, reads 8684, writes 14 timeouts 0, SG min/max 0/0
                                  Driver 2: short-to-ground standstill, reads 8681, writes 17 timeouts 0, SG min/max 0/8
                                  Driver 3: standstill, reads 8685, writes 14 timeouts 0, SG min/max 0/0
                                  Driver 4: standstill, reads 8688, writes 11 timeouts 0, SG min/max 0/0
                                  Driver 5: standstill, reads 8689, writes 11 timeouts 0, SG min/max 0/0

                                  Error: short-to-ground reported by driver(s) 2
                                  28/07/2020 à 12:33:42 M122
                                  === Diagnostics ===
                                  RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                  Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                                  Used output buffers: 1 of 40 (13 max)
                                  === RTOS ===
                                  Static ram: 154604
                                  Dynamic ram: 162592 of which 44 recycled
                                  Exception stack ram used: 360
                                  Never used ram: 75616
                                  Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1460) TMC(blocked,68) MAIN(running,4536) IDLE(ready,76)
                                  Owned mutexes:
                                  === Platform ===
                                  Last reset 00:01:04 ago, cause: power up
                                  Last software reset at 2020-07-27 15:14, reason: User, spinning module LinuxInterface, available RAM 75704 bytes (slot 0)
                                  Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0443c000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                  Error status: 0
                                  MCU temperature: min 32.1, current 32.5, max 32.6
                                  Supply voltage: min 23.9, current 24.0, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
                                  12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                  Driver 0: standstill, reads 56891, writes 0 timeouts 0, SG min/max not available
                                  Driver 1: standstill, reads 56890, writes 0 timeouts 0, SG min/max not available
                                  Driver 2: short-to-ground standstill, reads 56888, writes 2 timeouts 0, SG min/max not available
                                  Driver 3: standstill, reads 56890, writes 0 timeouts 0, SG min/max not available
                                  Driver 4: standstill, reads 56890, writes 0 timeouts 0, SG min/max not available
                                  Driver 5: standstill, reads 56890, writes 0 timeouts 0, SG min/max not available
                                  Date/time: 2020-07-28 11:33:45
                                  Slowest loop: 3.63ms; fastest: 0.21ms

                                  Driver number 4 : there is no extruder tool message

                                  1 Reply Last reply Reply Quote 0
                                  • T3P3Tonyundefined
                                    T3P3Tony administrators
                                    last edited by T3P3Tony

                                    Hi @Touchthebitum

                                    you will need to update your configuration temporarily to use the test motor on driver 3, and then again on driver 4 - use the M584 command in config.g:

                                    (To test driver 3) :
                                    M584 X0.0 Y0.1 Z0.3 E0.2 ; Temporary drive mapping to test driver 3 as Z

                                    (To test driver 4) :
                                    M584 X0.0 Y0.1 Z0.4 E0.2 ; Temporary drive mapping to test driver 4 as Z

                                    www.duet3d.com

                                    Touchthebitumundefined 2 Replies Last reply Reply Quote 0
                                    • Touchthebitumundefined
                                      Touchthebitum @T3P3Tony
                                      last edited by

                                      This post is deleted!
                                      1 Reply Last reply Reply Quote 0
                                      • Touchthebitumundefined
                                        Touchthebitum @T3P3Tony
                                        last edited by Touchthebitum

                                        @T3P3Tony said in Short to ground on drivers 0123:

                                        M584 X0.0 Y0.1 Z0.3 E0.2 ; Temporary drive mapping to test driver 3 as Z

                                        Driver 3

                                        m122
                                        

                                        === Diagnostics ===
                                        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                        Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                                        Used output buffers: 1 of 40 (10 max)
                                        === RTOS ===
                                        Static ram: 154604
                                        Dynamic ram: 162592 of which 44 recycled
                                        Exception stack ram used: 368
                                        Never used ram: 75608
                                        Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1452) TMC(blocked,204) MAIN(running,4952) IDLE(ready,76)
                                        Owned mutexes:
                                        === Platform ===
                                        Last reset 00:00:31 ago, cause: software
                                        Last software reset at 2020-07-28 13:51, reason: User, spinning module LinuxInterface, available RAM 75720 bytes (slot 3)
                                        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                        Error status: 0
                                        MCU temperature: min 33.6, current 34.2, max 34.4
                                        Supply voltage: min 24.0, current 24.0, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
                                        12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                        Driver 0: standstill, reads 26013, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 1: standstill, reads 26013, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 2: standstill, reads 26013, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 3: short-to-ground standstill, reads 26011, writes 17 timeouts 0, SG min/max 0/8
                                        Driver 4: standstill, reads 26017, writes 11 timeouts 0, SG min/max 0/0
                                        Driver 5: standstill, reads 26018, writes 11 timeouts 0, SG min/max 0/0
                                        Date/time: 2020-07-28 13:52:03
                                        Slowest loop: 4.13ms; fastest: 0.14ms

                                        Driver 4 MOTOR IS MOVING DURING TEST
                                        Error: short-to-ground reported by driver(s) 4
                                        28/07/2020 à 14:54:51 m122
                                        === Diagnostics ===
                                        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                        Board ID: 08DJM-956L2-G43S8-6J9F4-3S46N-TU2QD
                                        Used output buffers: 1 of 40 (10 max)
                                        === RTOS ===
                                        Static ram: 154604
                                        Dynamic ram: 162592 of which 44 recycled
                                        Exception stack ram used: 360
                                        Never used ram: 75616
                                        Tasks: NETWORK(ready,1968) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,4952) IDLE(ready,76)
                                        Owned mutexes:
                                        === Platform ===
                                        Last reset 00:00:50 ago, cause: power up
                                        Last software reset at 2020-07-28 13:53, reason: User, spinning module LinuxInterface, available RAM 75608 bytes (slot 0)
                                        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                        Error status: 0
                                        MCU temperature: min 28.3, current 34.6, max 34.7
                                        Supply voltage: min 23.9, current 24.0, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
                                        12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                        Driver 0: standstill, reads 53146, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 1: standstill, reads 53146, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 2: standstill, reads 53147, writes 14 timeouts 0, SG min/max 0/0
                                        Driver 3: standstill, reads 53150, writes 11 timeouts 0, SG min/max 0/0
                                        Driver 4: short-to-ground standstill, reads 53145, writes 17 timeouts 0, SG min/max 0/160
                                        Driver 5: standstill, reads 53151, writes 11 timeouts 0, SG min/max 0/0
                                        Date/time: 2020-07-28 13:54:55
                                        Slowest loop: 4.15ms; fastest: 0.13ms

                                        It is the first time I see a motor moving on this board

                                        1 Reply Last reply Reply Quote 0
                                        • T3P3Tonyundefined
                                          T3P3Tony administrators
                                          last edited by T3P3Tony

                                          @Touchthebitum said in Short to ground on drivers 0123:

                                          Driver 4: short-to-ground standstill, reads 53145, writes 17 timeouts 0, SG min/max 0/160

                                          OK so it looks like drivers 0-3 are damaged, possibly by the moving pins around earlier but hard to say.

                                          That said there is another issue that is causing a working motor to report short to ground (on driver 4). It may be that the damage to the other drivers is effecting them all. DC42 will have a better idea.

                                          Because of that I will authorise a warranty return. please use reference this thread in the warranty form that your reseller (3dware.ch) will ask you to complete for us and be sure to fill out the serial number so we can match this board to this thread.

                                          When you get your new board please triple check the wiring before powering everything up. I was a little concerned to see the tape holding the crimps on - intermittent disconnection of 1 wire of the 4 driver wires can damage the drivers.

                                          www.duet3d.com

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                                          • Touchthebitumundefined
                                            Touchthebitum @T3P3Tony
                                            last edited by

                                            @T3P3Tony

                                            Ok, thanks for your time and support.
                                            I'll 10x check ;), I want to print 😉

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